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N6610D accident description

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Crash location 37.520000°N, 122.511389°W
Nearest city Moss Beach, CA
37.527440°N, 122.513312°W
0.5 miles away
Tail number N6610D
Accident date 18 Nov 2016
Aircraft type Cessna 172N
Additional details: None

NTSB Factual Report

HISTORY OF FLIGHT

On November 18, 2016, about 1117 Pacific standard time, a Cessna 172N, N6610D, was substantially damaged when it impacted terrain while on final approach to Half Moon Bay Airport (HAF), Half Moon Bay, California. The private pilot sustained serious injuries, and the passenger was fatally injured. The personal flight was operated in accordance with 14 Code of Federal Regulations Part 91. Visual meteorological conditions prevailed in the area, and no flight plan was filed for the flight, which originated from Sacramento Executive Airport (SAC), Sacramento, California, about 1015, and was destined for HAF.

The pilot reported that, before departing SAC, he checked the weather for HAF, which indicated winds were from the southwest. He subsequently departed and requested visual flight rules flight following to HAF. The pilot stated that while approaching HAF, he made position reports on the airport's common traffic advisory frequency (CTAF) and requested traffic information. Someone responded that the wind was from the southeast up to 15 knots (kts) and that runway 12 was in use.

The pilot stated that he entered the airport traffic pattern for runway 12, and that as the airplane entered the final leg of the traffic pattern, the visual approach slope indicator (VASI) lights indicated that the airplane was high. At that time, the airplane was at an altitude about 800 ft mean sea level (msl) and at an airspeed of 65 kts when he reduced power to intercept the VASI glideslope.

As the airplane continued on the final approach path with full flaps (30°) at 60 kts and about 500 ft msl, it began to encounter light turbulence. The pilot was concerned that if the turbulence continued during the approach, he would be vulnerable to strong buffeting at normal approach speed, which might lead to a rough landing; as a countermeasure, he elected to land at a higher airspeed. The pilot then retracted the flaps to less than 20° while applying additional power to stay on the glideslope. The pilot added that, immediately after making these adjustments, he felt strong turbulence violently rock the airplane, which caused the wings to "dip," first to the left, and then to the right. He "simultaneously" felt a strong downdraft, and the airplane entered a steep right bank. The pilot stated that he fought to level the wings and gain altitude by applying full power, slight back pressure on the yoke, and then left aileron and rudder, but nothing seemed to correct the descent and right bank attitude. The pilot stated that he observed runway 12 come into view about 90° to his right but could not reach the runway due to the airplane's low altitude. Shortly thereafter, the pilot noticed large trees coming into view. Wanting to avoid trees in his flight path, the pilot stated that he maneuvered and tried to drag the airplane's tail on the ground. He next recalled closing his eyes to protect them, followed by impact.

PERSONNEL INFORMATION

The pilot held a private pilot certificate with ratings for airplane single-engine land and instrument airplane. He reported 1,145 total hours of flight experience, with 884 hours in the accident airplane make and model. Further, the pilot reported that he had flown 16.7 hours, 10.4 hours, and 1 hour in the preceding 90 days, 30 days, and 24 hours respectively. His most recent flight review was conducted on July 21, 2015, in the same make and model as the accident airplane.

The pilot was issued a third-class Federal Aviation Administration (FAA) medical certificate on April 15, 2015, with the limitation that he must have available glasses for near vision.

AIRCRAFT INFORMATION

The airplane was a single-engine, high wing, fixed landing gear, four-seat Cessna 172N, manufactured in 1979. It was powered by a normally aspirated, 180-horsepower Lycoming O-360-A4M engine, serial number RL-12115-36E, that drove a Sensenich, metal, 2-bladed, fixed-pitch propeller. A review of maintenance records revealed that the last annual inspection was accomplished on April 5, 2016, at an engine total time of 1,068.9 hours, and an airframe total time of 5,768 hours. The airplane and engine had accumulated a total of 173.2 hours since its most recent inspection.

METEOROLOGICAL INFORMATION

At 1115, the HAF weather reporting facility, located about ½ nm southeast of the accident site, reported wind from 190° at 10 kts, with gusts to 14 kts, visibility 10 statute miles, sky clear, temperature 17° C, dew point 3° C, and an altimeter setting of 30.03 inches of mercury.

A weather study revealed that a weak temperature inversion between 400 and 600 ft msl was present near the accident site at the time of the accident. Between 1100 and 1200 PST, the vertical environment changed from an unstable layer to a stable layer. The study found that the stable layer trapped any updrafts or downdrafts created by the wind flowing over the rise in terrain to the west and southwest of the airport. These changes created an environment favorable for low level wind shear and turbulence below 600 ft msl.

FAA Advisory Circular 00-6B (AC-00-06B), section 17.2.3.1, describes how areas near temperature inversions are favored for wind shear conditions. The AC notes that "Strong wind shears often occur across temperature inversion layers, which can generate turbulence."

WRECKAGE AND IMPACT INFORMATION

The airplane descended into a residential area about 1,822 ft northwest of the HAF runway 12 threshold. The initial point of impact was identified by two parallel rubber tire marks on a street about 245 ft southwest of the main wreckage. The airplane continued in a northeast direction across an open field that was about 100 ft wide, and subsequently struck a wooden fence that separated the field from a home. The airplane then continued on a northeast heading as it impacted the southeast corner of the roof of the home, which was followed by impact with a utility truck. The airplane's right wing tip and a landing gear strut were found in the front yard of the home.

The wreckage path then continued about 60 ft in a northeasterly direction. The nose landing gear was located about 30 ft northeast of the utility truck, and the main wreckage came to rest on the southwest corner of a second home. The lower fuselage came to rest flush against the brick structure of the residence with the engine firewall resting upright on the ground. The empennage separated just behind the rear passenger seats and was folded over and on top of the cabin, with the vertical stabilizer and rudder resting on the ground. The horizontal stabilizer and elevator remained attached to the fuselage. The cabin and cockpit areas were both destroyed by impact forces.

The left wing remained attached to the fuselage; the wing strut remained attached. The left flap and the inboard half of the aileron remained attached to the left wing.

The right wing, which had separated from the fuselage, impacted a white cargo van that was parked in an adjacent driveway about 7 ft from the main wreckage site.

About 4 ft of the outboard right aileron was separated from the wing and located next to the fuselage. The inboard section of the right aileron remained attached to the wing. Additionally, the right flap remained attached to the wing and appeared to be in the fully retracted position. The leading edge of the wing sustained impact damage. About 5 ft of the leading edge skin was separated at the wing's mid-span section. The outboard leading edge exhibited a concave depression.

The engine, propeller, and one of the landing gear struts were located under the right wing. The left and right main landing gear wheels were separated from the wreckage and found about 42 ft north of the fuselage, next to the backyard fence of the second residence.

ADDITIONAL INFORMATION

Performance Study

An airplane performance study based on radar data revealed that the airplane approached HAF from the north and entered at 45° to the upwind leg for runway 12. The airplane's speed was about 86 knots indicated airspeed (KIAS) and its altitude about 1,000 ft mean sea level (msl) when the pilot completed the turn for a left downwind to runway 12.

The airplane slowed to about 80 KIAS and descended to about 700 ft msl on the downwind leg. The airplane then entered a continuous, 180° left turn from the downwind to final legs of the traffic pattern. Radar data indicated that, at 1116:20, the airspeed was about 57 KIAS, the altitude was 500 ft msl (about 440 ft above ground level), and the airplane was at the apex of a 10°-bank left turn to final. At this point, the airplane's pitch angle changed from about 5° nose up to about -3° nose down, and the airplane accelerated as it descended until impact, which occurred about 1117:10.

The airplane's Pilot Operating Handbook (POH) estimates that the airplane will stall between 31 kts calibrated airspeed (KCAS) and 40 KCAS, depending on the airplane's flap position and bank angle. Additionally, the POH recommends "a slightly higher approach speed under turbulent air conditions." This is to compensate for any sudden loss in the headwind component, which would result in a momentary loss of airspeed and could lead to an aerodynamic stall above the published stall speed. Although the POH does not define "slightly higher", the FAA Airplane Flying Handbook recommends adding one-half of the reported surface wind gust to the normal final approach airspeed when landing in turbulent conditions.

The handbook states that the degree to which flaps should be extended during a crosswind approach and landing vary with the airplane's handling characteristics, as well as the wind velocity. Additionally, the handbook advises that retraction of wing flaps during an approach for landing "suddenly decreases lift and causes the airplane to sink rapidly."

NTSB Probable Cause

The pilot's loss of airplane control following an encounter with low level wind shear and turbulence during final approach for landing. Contributing to the loss of control was the pilot's decision to retract the wing flaps on final approach, which resulted in a sudden loss of lift.

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