Plane crash map Locate crash sites, wreckage and more

N2702M accident description

Florida map... Florida list
Crash location 25.858333°N, 81.394722°W
Nearest city Everglades City, FL
25.860100°N, 81.380357°W
0.9 miles away
Tail number N2702M
Accident date 27 Oct 2013
Aircraft type Piper Pa 28R-201T
Additional details: None

NTSB Factual Report

On October 27, 2013, about 1357 eastern daylight time, a Piper PA-28R-201T, N2702M, registered to Burlingame Financial Advisors LLC, crashed into water during a go-around after touchdown at Everglades Airpark (X01), Everglades City, Florida. Visual meteorological conditions prevailed at the time and no flight plan was filed for the 14 Code of Federal Regulations (CFR) Part 91 personal flight from Grass Roots Airpark (06FD), Groveland, Florida. The airplane sustained substantial damage, and the private pilot and one passenger sustained serious injuries, while 2 passengers sustained minor injuries. The flight originated about 1242 from 06FD.

The pilot stated that before departure he utilized his I-Pad for weather information which also contains VFR sectional charts, but he inadvertently left it behind. He also indicated that he did have sectional charts in his flight bag which was on-board the airplane. He was however using an on-board portable GPS receiver, which provided navigation information and also contained in part an airport database containing frequencies. He reported updating the software for the GPS less than 1 month earlier, while his wife reported by e-mail they, "…didn't have a subscription with Garmin. We didn't think we had to have a 'subscription' because we could update and download information at anytime on our own. Absolutely we believed that when we did an update it would do just that, update any and all new information for navigation and airports."

The pilot further stated that after takeoff while proceeding towards the destination airport he established two-way communications with several air traffic control facilities which included Tampa, Orlando, and Fort Myers Approach Control. No communications difficulties were reported although there was no record that the pilot established contact with Fort Myers Approach Control. The pilot reported that he obtained the common traffic advisory frequency (CTAF) for X01 from his GPS receiver, which was 122.8 MHz. Using that frequency and his GPS receiver for exact position information, he announced when the flight was 20, 10, and 5 miles away from X01 but there was no reply.

The flight continued towards X01, and when closer he observed an airplane on a taxiway near the approach end of runway 15. He stated that he did not understand why the pilot of that airplane did not acknowledge his radio calls, and with the wind from the northeast, entered the downwind leg for landing on runway 33. When the flight was abeam the numbers he again announced his intention on the same frequency but there was no reply. He turned onto base, and then final, and with the flaps fully extended and landing gear extended, he again announced his intention but there was no reply.

He landed left of runway centerline near the numbers and as he touched down, he observed what he reported was a "white shimmer" he attributed to be movement from the airplane that was located in the run-up area near the approach end of runway 15. Because he had not communicated with that pilot and he was not sure what that pilot intended on doing, he added full power to perform a go-around. He later indicated that the engine did respond but the airplane had poor climb performance because the flaps were full down, and he, "…pulled up too hard" during the aborted landing.

When clear of trees, he banked hard to the left, although he was not sure of the bank angle. He did not hear a warning horn, and reported the airplane stalled, which he informed the passengers they were going to crash. He tried to push over, but the airplane went into a flat spin and impacted the water backwards on the left wing. They opened the door, and all exited the airplane. While in the water out of the airplane his wife called 911 using her cell phone; the call occurred at 1358. The pilot later stated that his mistake was that he overreacted to the airplane, but in his mind he did not want a head-on collision. He further stated there was no preimpact failure of malfunction of the airplane or engine that precluded normal operation.

The pilot in the airplane in the run-up area east of the approach end of runway 15 reported that he landed at X01 about 1140, had lunch, and before boarding the airplane for his intended flight, went to the fixed base operator (FBO). He was informed that the wind was from 080 degrees at 7 to 8 knots, and after starting the engine, he taxied to the approach end of runway 15, and was facing westbound with the parking brake applied doing checklist items. He was monitoring 123.075 MHz, and did not hear any radio calls on that frequency from the pilot of the accident airplane. He noticed the accident airplane flying on a close-in downwind leg for runway 33 about 1,000 feet above ground level (agl), and thought the airplane was crossing over the airport going somewhere else. The observed the airplane bank steep to the left going from a downwind to base and final for runway 33 in one turn; the bank angle was between 50 to 60 degrees. He did not perceive the airplane touch down, and when the airplane was about ¼ to ½ way down the runway at less than 100 feet agl with the landing gear extended, he observed the accident airplane bank 50 to 60 degrees left wing low, then it went behind trees. When he did not see the airplane, or about 1 minute later, her turned about 90 degrees to the left and taxied to the ramp where he secured the airplane. While walking towards the FBO an individual from there came out and he advised that individual about the crash. The GPS receiver from his airplane was sent to the NTSB for read-out to the NTSB Vehicle Recorder Laboratory, located in Washington, D.C.

Following recovery of the accident airplane, inspection of the cockpit and cabin was performed by the Federal Aviation Administration (FAA) inspector-in-charge (IIC). During that inspection, bags behind the passenger seats were inspected which revealed an outdated Miami VFR Sectional Chart. Inspection of that chart revealed the X01 CTAF to be 123.075 MHz. The GPS receiver was removed and sent for read-out to the NTSB Vehicle Recorder Laboratory, located in Washington, D.C.

Also following recovery of the airplane, the point opening of either magneto could not be determined because of internal debris; both magnetos were tight on the accessory case with no evidence of movement/slippage. With NTSB permission, the magnetos were removed, cleaned, and installed on the engine and timed to specification. The engine core and cylinders were flushed of debris, and because the wings were not attached, an alternate fuel supply was plumbed into the fuel system. With FAA oversight, the engine was started and found to operate normally achieving 2,562 rpm maximum; maximum specified red line rpm is 2,575. Each magneto drop was reported to be 50 rpm each. No discrepancies were noted.

Examination of the GPS receiver from the accident airplane revealed that the Americas Aviation Data Cycle history was 0811 effective 20 October 2008 to 20 November 2008. The common traffic advisory frequency for X01 based on the installed Americas Aviation Data Cycle 0811 navigation database was 122.9 MHz. Additionally, the accident flight from takeoff to accident was recorded which included 384 recorded points starting at 1234:03, and ending at 1358:17.

A review of a plot of the recorded points associated with the approach and landing reflect the airplane was west of the runway flying in a southeasterly direction parallel to the runway about 1356:02, consistent with a downwind leg for runway 33, and continued in the same direction followed by left turns onto base and final. The recorded data also indicates the airplane was left of centerline at the approach end of the runway, continued to the left edge of the runway where the minimum GPS altitude of negative 9 feet occurred at 1357:37. The recorded data indicates the airplane bank to the left achieving the maximum GPS altitude of positive 43 feet at 1357:44, followed by decreasing altitude and groundspeed. The last data point associated a groundspeed value consistent with flight was at 1357:44; the groundspeed at that time was recorded to be 71 knots. The next recorded data point 3 seconds later indicates the groundspeed was 15 knots.

Examination of the GPS receiver from the airplane in the run-up area east of the approach end of runway 15 revealed it recorded the taxi beginning about 1352:34, and stopping at 1355:58. No movement was detected until 1358:32, which was 14 seconds after the last data point from the accident airplane, at which time the airplane was taxied down the taxiway to the ramp.

The published CTAF on the date and time of the accident for X01 was 123.075MHz. It was previously 122.9 MHz, but changed in 2009 to 123.075 MHz. The airport manager at X01 reported there was no reported issue with the current CTAF either by pilot's or airport users. Additionally, on the day of the accident between 1350 and 1400 hours, an operations specialist at X01 was temporarily off airport, arriving back at the airport at the same time the first responders arrived on-scene.

Based on the comment from the pilot that he communicated on 122.8 MHz, NTSB contacted Florida Keys Marathon Airport (MTH) and Marco Island (MKY), both of which utilize 122.8 MHz as their published CTAF. There were no reports from either airport of personnel hearing a radio call from the accident pilot on that frequency.

The Pilot's Operating Handbook did not specify balked landing procedures.

NTSB Probable Cause

The pilot’s failure to maintain airplane control and airspeed during a go-around, which resulted in a stall and impact with terrain. Contributing to the accident were the pilot’s inadvertent use of an outdated GPS navigation database, which provided an incorrect common traffic advisory frequency, and the inaccessibility of the visual flight rules sectional chart.

© 2009-2020 Lee C. Baker / Crosswind Software, LLC. For informational purposes only.