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N922XX accident description

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Crash location 34.987777°N, 81.056944°W
Nearest city Rock Hill, SC
34.924867°N, 81.025078°W
4.7 miles away
Tail number N922XX
Accident date 11 Sep 2009
Aircraft type Cirrus SR-22
Additional details: None

NTSB Factual Report

HISTORY OF FLIGHT

On September 11, 2009, about 0715 eastern daylight time, a Cirrus SR-22, N922XX, was destroyed when it impacted terrain while maneuvering after takeoff, at the Rock Hill Airport (UZA), Rock Hill, South Carolina. The certificated private pilot was killed. Visual meteorological conditions prevailed and no flight plan had been filed for the local flight. The personal flight was conducted under the provisions of 14 Code of Federal Regulations Part 91.

The airplane was owned by the pilot through a limited liability company and based at UZA.

According to the pilot's wife, the pilot normally flew with a copilot, who was also a certificated flight instructor (CFI). The pilot, his wife, and the CFI flew to Teterboro Airport (TEB), Teterboro, New Jersey, on September 7, 2009. The pilot and CFI returned to UZA on September 9, 2009, and planned to return to TEB, on September 13, 2009. The pilot's wife stated that the purpose of the accident flight was for the pilot to practice takeoffs and landings by himself.

A witness located at the UZA airport terminal, observed the airplane depart from runway 2, a 5,500-foot-long, 100-foot-wide, asphalt runway. After takeoff, the airplane made a shallow right turn and disappeared from his view. In addition, the witness and another individual both stated that they did not hear any communications from the pilot over the airport's common traffic advisory frequency.

A third witness, who lived near the airport, reported that he heard a "loud" engine noise, looked up, and observed an airplane in a vertical (90-degree bank) left turn. It was traveling "really fast" and the engine sounded "like it was at full-throttle." The airplane disappeared below the tree line and was followed by the sound of a "muffled-boom" and rising smoke.

PERSONNEL INFORMATION

The pilot, age 49, held a private pilot certificate, with a rating for airplane single-engine land. According to Federal Aviation Administration (FAA) records, the pilot received his private pilot certificate on November 21, 2008.

Review of the pilot's logbook revealed entries beginning on March 16, 2008, through August 22, 2009, for approximately 368 hours of total flight experience, of which about 333 hours were logged as "dual received." It was also noted that all flights in the accident airplane, with the exception of a 1.4 hour flight on July 15, 2009, included a flight instructor onboard. It was estimated that at the time of the accident, the pilot had accumulated about 390 hours of total flight experience, all in the same make and model as the accident airplane.

The pilot's most recent FAA second-class medical certificate was issued on February 21, 2008.

AIRCRAFT INFORMATION

The four-seat, low-wing, fixed-gear airplane, serial number 3455, was manufactured in 2009. It was constructed primarily of composite materials, and equipped with a Teledyne Continental Motors IO-550-N, 310-horsepower engine.

According to an FAA bill of sale, the airplane was purchased new by the pilot through a limited liability company during June 2009.

According to maintenance records, the airplane had undergone a 50-hour inspection in accordance with the Cirrus SR22 maintenance manual on August 26, 2009, about 40 hours prior to the accident.

At the time of the accident, the airplane had been operated for approximately 93 hours since new.

METEOROLOGICAL INFORMATION

A weather observation taken at UZA, which was at an elevation of 666 feet mean sea level (msl), at 0705 reported, wind from 020 degrees at 4 knots; visibility 9 statute miles; scattered clouds at 6,000 feet, temperature 16 degrees Celsius (C), dew point 14 degrees C; altimeter 30.20 inches of mercury.

WRECKAGE INFORMATION

The airplane initially impacted the ground about 100 feet below the top of a 20-degree slope, about 150 feet from taxiway "B," and 255 feet right of the extended center line of runway 20. The airplane was destroyed by fire and impact forces. Fragments of right wingtip were located near the initial impact point. A debris path, oriented on a 160-degree magnetic heading, extended for about 400 feet. Evidence of burnt terrain was observed on the left and right side of the debris path, on an embankment leading up to the taxiway.

The airplane was equipped with a Cirrus Airplane Parachutes System (CAPS). The parachute assembly was observed deployed, along the debris path; however, examination of the parachute assembly was consistent with activation due to impact forces.

Both wings and all control surfaces were separated and strewn along the debris path, with the majority of the fuselage structure. The main wreckage was located 205 feet from the initial point of impact, and consisted of a top portion of the fuselage from the "b-pillar," aft to the forward side of the CAPS enclosure. A portion of the fuselage station 222 bulkhead was also located with the main wreckage.

The roll trim motor was observed in an approximate neutral position. The flap actuator corresponded to the "flaps up" position.

All major components of the airplane were accounted for at the accident site.

The engine and engine cowling assembly separated from the airframe and came to rest about 70 feet from the initial impact point. The engine remained attached to the firewall via the control cables. The engine exhibited extensive impact and fire related damage. Portions of the No. 1 and No. 5 cylinder head assemblies were separated. The majority of engine accessories, which included both magnetos, the oil filter, the oil cooler, and both turbochargers were separated from the engine.

A borescope inspection of all engine cylinders did not reveal any preimpact failures. The No.1 cylinder was impact damaged and the exhaust valve seat was separated from the cylinder head. After removing several components from the engine, including the No.1 cylinder, the engine was rotated via the crankshaft propeller flange. Thumb compression and valve train continuity were established on cylinders No.2, 3, 4, and 6. Thumb compression and valve train continuity could not be established on cylinders No.1, and No.5 due to impact related damage. The fuel pump remained attached to the engine and did not exhibit any preimpact failures. Both magnetos were separated from their respective mounting locations and sustained impact and fire damage.

The propeller hub remained attached to the engine and exhibited impact damage. All three composite propeller blades were separated from the propeller hub. They all displayed impact damage with leading edge polishing and chordwise scratching.

The airplane was equipped with a "Garmin Perspective" cockpit instrumentation system, and a remote data module (RDM). The RDM, which was a crash hardened unit installed in the tail of the airplane intended to record flight, engine and autopilot parameters, was located in the debris path and forwarded to the NTSB Vehicle Recorders Laboratory, Washington, D.C., for download.

MEDICAL AND PATHOLOGICAL INFORMATION

An autopsy was performed on the pilot, on September 11, 2009, at Piedmont Medical Center, Rock Hill, South Carolina. The autopsy report indicated the cause of death as "multiple traumatic sharp and blunt force injuries secondary to plane accident."

Toxicological testing performed on the pilot by the FAA Bioaeronautical Science Research Laboratory, Oklahoma City, Oklahoma, was negative for alcohol and positive for Metoprolol detected in the pilot's liver and kidney.

The pilot’s most recent application for a second-class airman medical certificate noted a history of high blood pressure and metabolic syndrome, and the use of the medications omeprazole, atorvastatin, benazepril, metoprolol, aspirin and metformin. No other medications or conditions were noted, and the most recent medical certificate application specifically indicated "No" to "Mental disorders of any sort; depression, anxiety, etc.," "Admission to hospital," and "Other illness, disability, or surgery." Height and weight on that application were noted to be 74 inches and 248 pounds, and blood pressure was noted as 124/72.

The pilot's previous application for a third-class airman medical certificate was dated November 13, 1992. Review of the pilot’s primary care records indicated additional diagnoses, prior to the pilot’s most recent application for an airman medical certificate, of attention deficit disorder (with prior use of the prescription medication amphetamine/dextroamphetamine), depression (with prior use of the prescription medications bupropion and fluoxetine), anxiety (with hospitalization for anxiety in 2001 and use of the prescription medication clonazepam "0.5 mg three times a day as needed"), and ENT surgery in 2006 for severe snoring (with no indications that a sleep study had been performed). The pilot’s weight on a February 10, 2009, physician’s office visit was noted as 265 pounds.

TESTS AND RESEARCH

The RDM was successfully downloaded by an NTSB Vehicle Recorder Specialist. Examination of the RDM data revealed that it recorded about 90 hours of data, which included the accident flight. The data was logged once per second.

Review of the data for the accident flight revealed that the pilot began the takeoff about 0712:11, when the engine rpm was advanced to about 2700 rpm. The airplane proceeded along a heading of about 020 degrees magnetic, consistent with runway 2. Takeoff rotation occurred at an airspeed of 74 knots. At 0712:31, the airplane began a slight right turn. This turn lasted about 35 seconds, and generally varied from about 5 to 8 degrees of right roll, with a peak of about 17 degrees. During the turn, the airspeed and altitude continued to increase. At 0713:06, at an altitude of 1,051 feet msl, about 385 feet above ground level (agl) and a speed of about 133 knots, the right turn transitioned into a left turn. By 0713:15, the roll attitude had reached 46 degrees left wing down. At about the same time, the airplane reached its maximum altitude of 1,241 feet msl (about 575 feet agl). Over the next 20 seconds, the turn continued at about the same roll attitude (40-50 degrees left wing down), with the pitch remaining relatively level (within about 2 degrees up or down) as the speed increased to 158 knots. At 0713:34, the pitch attitude began to decrease toward a peak of 10 degrees nose down. At 0713:40, the roll attitude began a sharp change toward the right, reaching about 70 degrees right wing down by the end of the recorded data. The last recorded data points included the following:

Engine: 2,687 RPM

Heading: 165 degrees magnetic

Indicated Airspeed: 184 knots

Pitch Attitude: 5 degrees nose down

Roll Attitude: 69 degrees right wing down

Vertical Speed: 2064 feet per minute downward

Corrected Altitude 784 feet msl

It was noted that the stall warning parameter indicated "off" (not stalled) for the duration of the flight.

NTSB Probable Cause

The pilot's failure to maintain aircraft control and altitude while maneuvering after takeoff.

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