Crash location | Unknown |
Nearest city | Sparrevohn, AK
We couldn't find this city on a map |
Tail number | N702SC |
---|---|
Accident date | 29 Jan 1997 |
Aircraft type | de Havilland DHC-4A |
Additional details: | None |
HISTORY OF THE FLIGHT
On January 29, 1997, about 2310 Alaska standard time, a De Havilland DHC-4A, N702SC, collided with terrain about 2.2 miles west of Sparrevohn Long Range Radar Station (LRRS), Sparrevohn, Alaska. The airplane was being operated as an instrument flight rules (IFR) cargo flight to Kenai, Alaska, under Title 14 CFR Part 135 when the accident occurred. The airplane, operated by South Central Air, Kenai, Alaska, was destroyed. The captain, a certificated commercial pilot, received serious injuries. The first officer, a certificated airline transport pilot, received fatal injuries. Visual meteorological conditions prevailed. An IFR flight plan was filed. The flight originated from St. Mary's, Alaska, about 2105 hours.
The captain reported the crew was involved in transporting mining equipment from Pilot Station, Alaska, to St. Mary's, and had made three trips between the two areas throughout the day. The final load of the day was a large mining air compressor that was secured in the cargo compartment. The flight landed at St. Mary's for fuel and service before departing on the accident flight to Kenai. The captain reported the fuel load was 2,800 pounds, and the cargo weighed 5,300 pounds.
After departure, the first officer was flying the airplane and the flight was progressing at 12,000 feet mean sea level (msl). The intended route of flight was from St. Mary's, via the Sparrevohn VOR, to Kenai. About 10 miles east of the Sparrevohn VOR, the right engine propeller began to overspeed. The captain feathered the right engine, and at 2252:25, the crew declared an emergency with the Anchorage Air Route Traffic Control Center (ARTCC), and reported the flight was diverting to Aniak, Alaska. The captain advised the first officer to perform a 180 turn back to the Sparrevohn VOR, and the flight was cleared by the ARTCC to descend to 6,000 feet. The captain considered making a landing at the Sparrevohn Airport, and requested the ARTCC obtain permission to land at Sparrevohn. The crew requested the weather conditions at Sparrevohn, and the ARTCC controller informed them the wind was calm, the visibility was 10 miles, and the sky condition was 8,000 feet with scattered clouds. At 2254:54, the crew canceled the request for landing at Sparrevohn, stating: "...center, 2SC, yea cancel that request, we'll just go back to Aniak, ah, there's not enough visibility down here to make a visual approach."
En route to Aniak, the captain advanced the power on the left engine, and he reported it began to produce banging and coughing noises. The airplane was unable to maintain altitude, and began descending about 300 feet per minute. At 2258:44, the ARTCC requested the crew change radio frequencies to receive the weather conditions reported in Aniak. The controller asked the crew to verify the flight was descending to 6,000 feet. The crew replied they were unable to maintain altitude. The controller verified the airplane was descending out of 7,700 feet.
At 2302:25, the crew informed the ARTCC of additional engine trouble, and requested the VOR/DME instrument approach to runway 34 at Sparrevohn. The captain took control of the airplane, and with the assistance of the first officer, began preparations for an emergency landing at Sparrevohn. At 2304:40, the crew requested the safest altitude for descent. The controller replied that the minimum altitude within 25 nautical miles is 5,800 feet. At 2305:42, the crew indicated they would fly the published approach and the controller requested the crew advise when they were over the VOR to proceed outbound on the 111 degree radial to intercept the 12 DME arc. At 2305:58, the crew indicated they were unable to maintain 5,800 feet. At 2306:19, the controller advised the crew to report over the VOR and at 2306:54 the controller stated: "...after you pass the VOR and you're established outbound on the 111 radial, the highest terrain is physically 3,436 feet and that is about half way out to the arc that will be on your left."
At 2307:36, the controller indicated that he observed the airplane at 5,400 feet and the crew concurred. At 2307:57, the crew stated: "...center, ah, we can pick up the runway identifier lights from this position, can we go straight in." The controller replied "... affirmative, if you have the runway, you're cleared for the visual approach, try to report your arrival this frequency." The crew replied in the affirmative, and the captain selected 15 degrees of flap and gear down, and began descending toward the airport while attempting to maintain visual contact with the runway.
At 2308:12, the controller inquired: "... 2SC roger, is that your intention and do you have the runway lights now." The crew replied, "...'unintelligible' have the lights and we're going for them 2SC." The controller inquired if the airplane was landing toward the north or toward the south. At 2309:09, the crew replied: "...only one approach to Sparrevohn sir 'unintelligible' north."
The captain reported the airplane encountered severe turbulence from the surrounding mountainous terrain, and he applied full power on the left engine to attempt a climb. During the turbulence encounter, the captain lost visual contact with the runway lights, and at 2309:30, the crew stated to the ARTCC controller: "...get them, can you call Sparrevohn sir and have them turn their lights on pronto." The captain recalled that he called for gear and flaps "up." He observed the left engine manifold gauge indicating 50 inches. The airplane then collided with snow covered, upsloping terrain in an area of high winds and blowing snow.
The accident occurred during the hours of darkness at latitude 61 degrees, 06.186 minutes north and longitude 155 degrees, 38.346 minutes west.
CREW INFORMATION
The captain holds a commercial pilot certificate with airplane single-engine land, single-engine sea, multi-engine land, and instrument airplane ratings. In addition, the captain holds a mechanic certificate with airframe and powerplant ratings, and a type rating for the DHC-4 airplane. The most recent first-class medical certificate was issued to the pilot on December 13, 1996, and contained no limitations.
The captain is a check airman for all company pilots. He received an FAA proficiency check pilot authorization for DHC-4 airplanes, second-in-command only, on April 16, 1996. The captain received his initial and upgrade training for pilot-in-command in DHC-4 airplanes on September 29, 1995, which included 9 hours of flight training.
According to pilot records provided by the operator, the captain's total aeronautical experience consists of about 4,987 hours, of which about 220 hours were accrued in the accident airplane. In the preceding 90 and 30 days prior to the accident, the captain accrued a total of 120 and 41 hours respectively.
Examination of the captain's flight and duty records revealed he accrued .7 flight hours between 0700 and 1730 on January 27, 1997. On January 28, 1997, the captain's duty hours from 0700 and 1700, did not include any flight time. On the accident date, January 29, 1997, the captain's duty record indicated he reported to work at 0700. The operator reported that company personnel made that entry in error, without the captain's knowledge. The captain indicated he actually started work at 0900. The anticipated arrival time in Kenai for the accident flight was 2400.
The first officer held an airline transport pilot certificate with airplane single-engine land, multi-engine land, and instrument airplane ratings. He also held a flight instructor certificate with airplane single-engine and instrument airplane ratings. In addition, the first officer held a mechanic certificate with airframe and powerplant ratings. The most recent first-class medical certificate was issued to the first officer on August 26, 1996, and contained the limitation that the pilot must wear corrective lenses for near and distant vision.
The first officer was hired by the operator and began initial ground training on August 26, 1996. On August 29, 1996, the first officer concluded his initial flight training and passed a check ride in the DHC-4 airplane with IFR and second-in-command privileges. The first officer's duties also included maintenance work on company airplanes, and as the pilot of Cessna 207 airplanes.
According to the operator, the first officer's total aeronautical experience consisted of about 1,823 hours, of which 589 hours were second-in-command. The first officer had accrued 35 hours in the accident airplane. In the preceding 90 and 30 days prior to the accident, the first officer accrued a total of 37 and 6 hours respectively.
Examination of the first officer's flight and duty records revealed he accrued .7 flight hours between 0800 and 1730 on January 27, 1997. On January 28, 1997, the first officer's duty hours from 0800 and 1700, did not include any flight time. On the accident date, January 29, 1997, the first officer reported to work at 0830.
Title 14, Code of Federal Regulations (FAR) 135.267 Flight time limitations and rest requirements: Unscheduled one and two pilot crews, states, in part: (b) Except as provided in paragraph (c) of this section, during any 24 consecutive hours the total flight time of the assigned flight when added to any other commercial flying by that flight crewmember may not exceed - (1) 8 hours for a flight crew consisting of one pilot; or (2) 10 hours for a flight crew consisting of two pilots qualified under this Part for the operation being conducted. (c) A flight crewmember's flight time may exceed the flight time limits of paragraph (b) of this section if the assigned flight time occurs during a regularly assigned duty period of no more than 14 hours and- (1) If this duty period is immediately preceded by and followed by a required rest period of at least 10 consecutive hours of rest; (2) If flight time is assigned during this period, that total flight time when added to any other commercial flying by the flight crewmember may not exceed - (i) 8 hours for a flight crew consisting of one pilot; or (ii) 10 hours for a flight crew consisting of two pilots; and (3) If the combined duty and rest periods equal 24 hours. (d) Each assignment under paragraph (b) of this section must provide for at least 10 consecutive hours of rest during the 24 hour period that precedes the planned completion time of the assignment.
AIRCRAFT INFORMATION
The airplane was maintained according to an approved aircraft inspection program (AAIP). According to the airplane's maintenance records, a phase A2 inspection was completed on December 30, 1996. At that time, the airplane had accrued 13,922.5 hours. All of the engine and component times listed in this report are calculated from the last inspection.
At the time of the last inspection, the left engine, serial number 107257, had accrued 276.6 hours since being overhauled on August 8, 1995. It was installed on the accident airplane on November 25, 1995.
The right engine, serial number 100893, was installed on the airplane on July 11, 1996, and had accrued 152.5 hours since being overhauled on February 20, 1996.
The airplane utilizes constant speed, full feathering, and reversible propellers. The three bladed assembly utilizes an independent oil control (IOC) unit that supplies hydraulic pressure to change the propeller pitch. The IOC is mounted on the propeller shaft at the front of each engine.
The left engine propeller assembly, serial number 194753, was installed on the left engine on November 25, 1995, and had accrued 2,386.9 hours since being overhauled on February 16, 1993. The left engine IOC, serial number 818, was previously overhauled on January 30, 1996. It was installed on the right engine on February 2, 1996, and then removed from the right engine on July 7, 1996, due to leakage. The maintenance records do not reflect when the IOC was last overhauled, or when it was installed on the left engine.
The right engine propeller assembly, serial number 204615, had accrued 682.5 hours since being overhauled on November 12, 1992. The right engine IOC, serial number 538, was also overhauled on November 12, 1992, and was installed along with the propeller assembly on the right engine on January 5, 1993. At that time, the propeller and the IOC had accrued 16.5 hours since being overhauled. The maintenance records do not reflect when the IOC was removed from the right engine. The records reflect that it was overhauled on June 14, 1996, and was again installed on the right engine with propeller assembly 204615, on July 7, 1996. It then accrued 160.1 hours before the last inspection of December 30, 1996.
The operator provided a reconstruction of the airplane's weight and balance sheet for the accident flight. The operator listed the empty weight of the airplane as 19,630 pounds. Examination of the maintenance records indicated the airplane was weighed on August 12, 1994, with a center of gravity of 353.7 inches. An empty weight of 19,630 pounds was noted in the records at that time. On September 24, 1994, 500 pounds of cargo area flooring was removed, and on September 29, 1994, 150 pounds of cargo area carpeting was installed. This resulted in a 350 pound decrease in the airplane's empty weight to 19,280.
In addition to the operator's reconstructed weight and balance sheet that listed the empty weight as 19, 630 pounds, the cargo, carried in areas 8 through 11, was listed as 5,300 pounds. Seventy-five pounds of cargo was carried in area 12. The crew weight was listed as 350 pounds, a winch as 180 pounds, and fuel as 2,800 pounds. The takeoff weight of the airplane was listed as 28, 335 pounds with a center of gravity as 352.2 inches. The airplane's maximum forward center of gravity is 347.2 inches. The maximum aft limit is 357.1 inches. The airplane's maximum ramp weight is 28,500 pounds. The operator reported the airplane has a fuel burn of about 100 gallons (600 pounds) per hour.
At gross weight, the airplane's single engine service ceiling* is 8,700 feet.
*The altitude at which the airplane is able to sustain a steady rate of climb of 100 feet per minute.
METEOROLOGICAL INFORMATION
The closest official weather observation station is Sparrevohn, Alaska, located 2.2 miles east of the accident site. At 2315, a special automated observation was reporting in part: Wind, 170 degrees (true) at 7 knots; visibility, 10 statute miles; clouds, 4,800 feet scattered, 7,000 feet overcast; temperature, -1.7 degrees C; dew point, -6.1 degrees C; altimeter, 28.71 inHg.
At 2235, a special automated observation was reporting in part: Wind, 290 degrees (true) at 4 knots; visibility, 10 statute miles; clouds, 7,000 feet broken; temperature, -2.8 degrees C; dew point, -5.5 degrees C; altimeter, 28.70 inHg.
Sparrevohn facility and rescue personnel reported high winds near 50 knots, and blowing snow with limited visibility.
AIDS TO NAVIGATION
The Sparrevohn VOR is located 2 statute miles on a 250 degree magnetic bearing from the airport, at an elevation of 2,501 feet msl. The Sparrevohn radome complex is located about 1.5 miles north of the runway, at 3,034 feet msl.
The NDB/VOR DME approach for runway 34 has an initial approach fix at 5,800 feet on the 064 degree radial at 12 DME from the Sparrevohn VOR. The approach proceeds along a 12 mile arc in a right turn to intercept the 347 degree radial inbound toward the airport. The 111 degree radial from the VOR intersects the arc about half way between the initial approach fix and the final approach course. The instrument approach charts for Sparrevohn include a dialog box that states: "Caution: runway surrounded by mountains. Runway located on slope of 3,236 foot mountain. Approach from south only, land runway 34 only. Successful go-around improbable. Caution: Winds in excess of 20 knots (Radome winds 25 knots) may produce severe turbulence."
COMMUNICATIONS
Review of the air-ground radio communications tapes maintained by the FAA at the Kenai Automated Flight Service Station (AFSS) and the Anchorage ARTCC faci
loss of the right engine propeller control oil, which led to an overspeed of the right engine and propeller, and necessitated a shut-down of the right engine; and failure of the pilot to maintain adequate altitude/distance from terrain during visual approach for a precautionary landing at an alternate airport. Factors relating to the accident were: fluctuation of the left engine power, premature lowering of the airplane flaps, and an encounter with adverse weather conditions (including high winds, severe turbulence, and white-out conditions) during the approach.