Crash location | 31.910278°N, 85.370834°W |
Nearest city | Clayton, AL
31.878216°N, 85.449663°W 5.1 miles away |
Tail number | N1631X |
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Accident date | 03 Apr 2014 |
Aircraft type | Cessna T210L |
Additional details: | None |
On April 3, 2014, about 1530 central daylight time, a Cessna T210L, N1631X, was substantially damaged during a forced landing to a road following a total loss of engine power near Clayton, Alabama. The flight instructor (CFI) was not injured and the pilot receiving instruction received minor injuries. Visual meteorological conditions prevailed and an instrument flight rules flight plan had been filed for the instructional flight that was conducted under the provisions of Title 14 Code of Federal Regulations Part 91. The flight departed Valdosta Regional Airport (VLD), Valdosta, Georgia about 80 minutes prior to the accident and was destined for Tuscaloosa Regional Airport (TCL), Tuscaloosa, Alabama.
According to the CFI, after departing from VLD and completing a climb to 6,000 feet above mean sea level, the engine fuel flow was lower than expected for the flight, with relation to the setting of the mixture control. The pilot receiving instruction added that about an hour into the flight the engine "clunked and shuddered." The CFI assumed control of the airplane, maneuvered the airplane towards a nearby airport, and the pilot receiving instruction initiated an unsuccessful restart of the engine. Both pilots reported that the engine oil pressure and propeller rpm both indicated zero, and the manifold pressure was about 17 psi. After determining that the airplane was not going to make the airport, the CFI selected a grass field and then switched to a road after discovering power line wires spanning across the field. The pilot receiving instruction declared an emergency with Air Traffic Control just prior to the CFI executing a forced landing to the road.
Initial examination of the airplane by a Federal Aviation Administration inspector revealed that the engine firewall was crushed aft and that both wings were substantially damaged.
According to FAA records, the airplane was manufactured in 1975 and registered to a corporation in 2004. It was equipped with a Continental Motors Inc. TSIO-520 series, 310 hp, engine. Review of copies of maintenance logbook records showed a 100-hour inspection was completed April 5, 2013, at a recorded tachometer reading of 8377.8 hours, and an engine total time of 892 hours.
According to maintenance records, the No. 2, No. 3, and No. 6 cylinders were removed, reworked, and replaced on January 10, 2014. The entry stated the work was performed in accordance with the TSIO-550 Service Manual, which had the same torque values required for a TSIO-520 series engine according to the engine manufacturer. The engine log entry indicated that "leak checked and ground run satisfactory." In addition, an oil change was performed on April 3, 2014, where the oil was drained, a new oil filter was installed, and 9 quarts of oil were added to the engine. A ground run was performed with "ops normal, no leaks." There was no indication of the oil filter being opened and examined as recommended in the best practices described in Advisory Circular 43.13-1B, Acceptable Methods, Techniques, and Practices - Aircraft Inspection and Repair, Chapter 8, Section 6 – Oil Filter Inspection. Examination of the engine maintenance records revealed that the most recent occurrence of the oil filter was dissected and the element was examined for metal particulate was on January 10, 2014, at the time of the cylinder repair. On the most recent inspection no notation was made.
The engine of the airplane was examined on April 15, 2014, at the salvage facility in Griffin, Georgia, under the supervision of an NTSB investigator. The engine was intact an all accessories remained attached. The spark plugs were removed and all were light grey in color and exhibited normal wear according to the Champion Check-a-plug chart. The magnetos were removed, they both operated and spark was observed on all towers. The crankshaft was rotated utilizing the propeller and crankshaft continuity could not be confirmed. The fuel pump was removed, tested, and operated with no anomalies noted. The oil sump was removed and metal particles were noted. The engine case was separated and the crankshaft, two bearings, and cylinders No. 2 and No. 6 connecting rods were removed and sent to the NTSB Materials Laboratory for examination. Torque values on the crankcase through bolts were not obtained during the disassembly of the engine. According to Continental Motors Service Bulletin (SB 96-7C) the "12 Point-Thru bolt at cylinder flange" was to have a torque value between 790 to 810 inch/pounds.
The NTSB Materials laboratory examination revealed that the crankshaft had fractured at the No. 2 main journal. The aft fracture surface was battered such that most fracture features were obliterated, consistent with post-fracture damage. The mating forward face was damaged but exhibited crack arrest marks along the surface. The adjacent crankshaft journal exhibited circumferential wear scars and the journal surface closest to the aft fracture surface exhibited color changes that ranged from yellow and orange to purple and dark blue, moving aft to forward along the journal surface toward the fracture surface.
The crankshaft fracture surface exhibited fatigue striations consistent with fatigue crack propagation. The initiation sites were smooth, with no indications of material defects such as inclusions, pits, or voids. In addition, there were no machine marks in these areas or along the journal fillet shown to have initiated cracks. Along the bearing journal surface just forward of the fatigue crack initiation sites, were material deposits associated with galling wear. This galled material was consistent with babbitt material typical of bearing materials.
A detailed report documenting the NTSB Materials Laboratory examination is available in the official docket of this investigation.
A review of a similar accident (ERA14LA193), revealed the damage was consistent with the circumstances and damage associated with this event. In that investigation, engine manufacturer personnel indicated that a crankshaft failure associated with a bearing shift will usually fail in fatigue. Examination of that accident revealed that the engine through bolts were not torqued to the required torque setting, which resulted in a bearing shift, oil starvation, and a subsequent fatigue crack failure in the crankshaft.
Maintenance personnel’s failure to properly torque the engine case through bolts, which resulted in the fatigue fracture of the crankshaft and subsequent total loss of engine power.