Crash location | 35.967223°N, 113.768889°W
Reported location is a long distance from the NTSB's reported nearest city. This often means that the location has a typo, or is incorrect. |
Nearest city | Peach Springs, AZ
35.529159°N, 113.425491°W 35.9 miles away |
Tail number | N155GC |
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Accident date | 10 Feb 2018 |
Aircraft type | Eurocopter EC130 |
Additional details: | None |
On February 10, 2018, about 1715 mountain standard time, an Airbus Helicopters EC130 B4 helicopter, N155GC, was destroyed when it impacted a canyon wash while on an approach to land at Quartermaster landing zone near Peach Springs, Arizona. The commercial pilot and three passengers sustained serious injuries and three passengers were fatally injured. The air-tour flight was operated by Papillon Airways, Inc. under the provisions of 14 Code of Federal Regulations Part 136. The helicopter departed Boulder City Municipal Airport, Boulder City, Nevada at 1635 and had intended to land at Quartermaster landing zone, a group of landing pads within Quartermaster canyon. Visual meteorological conditions prevailed, and a company flight plan had been filed.
A review of the recorded radar data showed that the helicopter departed Boulder City and continued on the Green 4 standard helicopter route prescribed in the Grand Canyon West Special Flight Rules Area 50-2. Witnesses reported that as the helicopter neared the vicinity of Quartermaster, they observed it on a flight path consistent with the pilot aligning to make a downriver-wind landing to a pad on the west. The helicopter began to slow after it passed over the river and maintained a southern course as it entered a canyon wash adjacent to the landing pads. While maintaining the same altitude, the helicopter entered a nose-high attitude and then began a left turn toward the Quartermaster landing zone. During the turn, the helicopter transitioned into a nose-low attitude and as it began to face the landing pads it began to slightly drift aft. The helicopter then maneuvered into a nose-level configuration and continued in the left turn. Subsequently, the helicopter made at least two 360° left turn revolutions as it descended into the wash below where it impacted terrain and a postcrash fire ensued.
The helicopter came to rest upright in rocky terrain about 300 feet below the landing zone on a heading of 222° magnetic. The accident site was compact except for small main rotor blade pieces and small paint chips distributed around the main wreckage site. Most of the wreckage was consumed by the postcrash fire except for the tailboom and fenestron, which had separated from, but were collocated with the main fuselage. The engine, still attached to the engine deck, was found in the main wreckage and had also sustained fire damage. All three main rotor blades remained attached to the main rotor hub and exhibited damage consistent with high rotational energy. The tail stinger, fenestron hub cover, a toe from a skid step, and small pieces of transparent acrylic glass were found on a canyon slope east of the main wreckage.
The 8-seat capacity, fixed landing gear helicopter, serial number 7091, was manufactured in 2010. The accident helicopter was powered by one Safran Helicopter Engines (formerly Turbomeca) Arriel 2B1 turboshaft engine.