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N2725V accident description

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Crash location 34.508611°N, 109.387222°W
Nearest city St Johns, AZ
34.470800°N, 109.312600°W
5.0 miles away
Tail number N2725V
Accident date 26 Jun 2011
Aircraft type Cessna 177RG
Additional details: None

NTSB Factual Report

HISTORY OF FLIGHT

On June 26, 2011, about 1340 mountain standard time, a Cessna 177RG, N2725V, collided with terrain in a field following takeoff from St Johns Industrial Air Park (SJN), St Johns, Arizona. The pilot was operating the airplane under the provisions of Title 14 Code of Federal Regulations Part 91. The private pilot and two passengers sustained serious injuries; the airplane sustained substantial damage. The cross-country flight departed SJN about 1340, with a planned destination of Mesquite Metro Airport (HQZ), Mesquite, Texas. Visual meteorological conditions prevailed, and no flight plan had been filed.

The airplane arrived at SJN about 1245, having flown from San Bernardino, California. According to the pilot and passengers, the accident flight was to be the penultimate leg of a journey, which was to ultimately end in Mesquite. The group had originally departed in the accident airplane from the Dallas area about a week prior, and had landed and taken off at multiple airports in the Southwest region during that time.

The pilot reported that after landing at SJN, he had the airplane serviced with fuel, and that they stayed longer than he had planned. He became concerned about the airplane’s performance as the day drew on, and the air temperature began to rise. They eventually boarded, and the pilot performed an uneventful engine run-up.

An airport employee, located in the fixed base operator facility at midfield, observed the pilot and passengers board the airplane, and then taxi to the departure end of runway 21. The airplane then turned onto the runway and began to move at a speed she considered slow, such that she thought the pilot had decided to cancel the takeoff. The airplane then crossed runway 14/32 and its parallel taxiway, and began to accelerate once it progressed to about 1/3 of the runway length. She continued to watch as the airplane accelerated, and eventually rotated 3/4 of the way down the runway. The airplane began to climb, but did not gain altitude once it reached the level of adjacent trees. The airplane continued in a nose-high attitude, and then suddenly descended out of her view.

The witness reported that at the time of departure, the local automated surface observing systems (ASOS) indicated wind from 270 degrees, at 17 knots gusting to 30, with a density altitude of 9,200 feet.

The passengers stated that as the airplane began the ground roll, it appeared to accelerate more slowly and felt more labored than on previous flights. They recalled that the airplane took off further down the runway than before, and once in the air it appeared to "hover". They stated that not long after takeoff, they began to hear the sound of a buzzer, as the airplane began to roll from left to right.

The pilot stated that he could not recall the point at which he began the ground roll, but that the takeoff progressed normally until the airplane reached an altitude of about 200 feet above ground level. At that point, the airplane would no longer climb, and certain that they would not be able to return to the airport, he attempted to maneuver the airplane for a landing in the field ahead.

The airplane came to rest on runway heading, about 1,800 feet beyond the departure end of runway 21. The airplane remained intact, with the entire cabin and fuselage structure sustaining vertical crush damage. The horizontal stabilizer sustained crush damage to its forward surfaces on both sides, and contained fragments of branches and tree limbs. No corresponding damage was noted to the wings.

PERSONNEL INFORMATION

A review of Federal Aviation Administration (FAA) airman records revealed that the pilot held a private pilot certificate with ratings for airplane single-engine land issued in 1998. The pilot reported a total flight time of 681 hours; 350 in the accident make and model.

AIRPLANE INFORMATION

The four-seat, high-wing, retractable-gear airplane, serial number 177RG0672, was manufactured in 1975. It was powered by a Textron Lycoming IO-360-A1B6D engine, serial number L-13497-51A, and equipped with a McCauley two-blade constant speed propeller.

The complete maintenance logbooks were not recovered, and as such, the mechanic who performed the most recent annual inspection provided maintenance records. The last annual inspection was completed on March 18, 2011. At that time, the airframe had accrued a total time of 5190.8 flight hours, with an engine time of 745.5 hours since major overhaul.

The airplane underwent an avionics system upgrade in February 2010, which included the replacement of the majority of the original avionics equipment. The upgrade included the addition of a Garmin G500 multi function display, an SL-30 navigation/communication transceiver, and a J P Instruments EDM-930 engine data monitor.

METEOROLOGICAL INFORMATION

An automated surface weather observation at SJN was issued about 25 minutes after the accident. It indicated wind from 250 degrees at 23 knots, gusting to 30 knots; 10 miles visibility; sky clear; temperature 96 degrees Fahrenheit (F); dew point 24 degrees F; and an altimeter setting at 30.04 inches of Mercury. The calculated density altitude, based on these values, was 9,369 feet.

AIRPORT INFORMATION

St Johns Airport is equipped with two intersecting runways. According to the FAA Southwest Airport/Facility Directory (AFD), runway 3/21 is 3,400 feet in length, and located at an elevation of 5,737 feet mean sea level. Runway 14/32 is 5,322 feet in length. The AFD does not make reference to obstacles in the path of runway 3/21. Utilizing a mapping program, the closest obstacle in the departure path of runway 21, was a single-story building, about 800 feet beyond the threshold of runway 3.

TESTS AND RESEARCH

Airframe and Engine Examination

The airplane was recovered, and subsequently examined by the NTSB investigator-in-charge and a representative from Cessna Aircraft.

The examination revealed that the landing gear and flaps were in the fully retracted position. Based on photographic evidence taken at the accident site, the fuel mixture and propeller controls were in the full forward position, with the throttle control about 1/4-inch aft of full forward. The yoke was in the full aft position, and the cowl flap control lever was in the closed position. The elevator and rudder trim positions could not be determined.

The engine sustained minimal damage. The dual magneto remained firmly attached to its mounting pads, and the spark plugs were secure at each position, with their respective leads attached. The top spark plugs were removed, and examined. The electrodes remained mechanically undamaged, coated in light grey deposits, and displayed worn out–normal wear signatures when compared with the Champion Spark Plugs AV-27 Check-A-Plug chart. The exhaust pipes exhibited light grey deposits, and were free of oil residue. The crankshaft turned freely when rotated by hand utilizing the propeller flange, and thumb compression was observed on all cylinders. Mechanical continuity was established throughout the rotating group, valve train and accessory section, and all rocker arms displayed equal amounts of lift. Sparks were observed at the termination of each spark plug lead. Cylinder number two was removed in order to facilitate the examination of the lifting surfaces of the forward camshaft lobes. The lifting surfaces of cylinder number one exhaust cam, cylinder number two exhaust cam, and the shared cylinder number one and two intake cam appeared clean, and free of scratches, gouges, or spalling, with a defined and undamaged profile noted at each point of maximum cam lift.

No evidence of preimpact mechanical malfunction or failure was noted during the examination of the airframe and engine, a complete examination report is contained within the public docket.

Weight and Balance

Fueling records recovered from St John's Airport indicated that the airplane was serviced to capacity with the addition of 41 gallons of 100 low-lead aviation gasoline prior to departure.

An officer from the local Police department responded to the accident site. She recovered and weighed the baggage, which was distributed throughout the cabin, and reported the total weight to be 88 pounds. The airplane's occupants reported their individual weights, and this information was subsequently verified with their driver's license records. The weight of the pilot and the front seat passenger totaled 333 pounds. The passenger located in the aft seat weighed 160 pounds. Based on the airplane's documented empty weight of 1,738 pounds, and a usable fuel load of 61 gallons, the weight at the time of the accident was 2,675 pounds, 125 pounds below the maximum gross weight. Referencing these values against the airplane's weight and balance records revealed that it was loaded within the approved center of gravity envelope at the time of the accident.

Engine Monitor

The EDM-930 engine data monitor was configured to record 21 separate engine parameters. The monitor was sent to the NTSB Vehicle Recorders Division for data extraction. The data revealed that the unit recorded 31 hours of data over 36 separate cycles, with two recorded on the day of the accident. The last recording documented the accident flight, and lasted 4 minutes and 36 seconds.

For the first 3 1/2 minutes of the last recording, the engine manifold pressure, engine rpm, oil pressure, cylinder head temperatures (CHT), and exhaust gas temperatures (EGT) exhibited variations consistent with initial engine start, ground run-up, and taxi. For the 50 seconds prior to the last recorded data point, all of these values remained relatively constant. The engine speed remained around 2,630 rpm, with an associated manifold pressure of 23.2 inches of mercury. The EGT and CHT remained consistent across all cylinders at 1,200 and 300 degrees, respectively. Fuel flow remained at 16 gallons per hour (GPH), and the oil pressure and temperature was at 78 pounds per square inch and 160 degrees F, respectively. The engine was producing 72.5% of its potential power output, as calculated by the EDM-930. Additionally, the fuel tank readings indicated that each tank contained 30 gallons of fuel.

The data from the prior flight revealed that about 4.5 hours prior to the accident, while departing from San Bernardino Airport, the engine produced 87% of its potential power output. San Bernardino Airport was at an elevation of 1,159 feet, and the calculated density altitude about the time of departure was 1,980 feet. During the subsequent landing approach into St Johns Airport, the engine intermittently produced comparable power outputs to the accident flight at similar rpm and manifold pressure settings.

Performance

According to the airplane owner's flight manual, the engine will develop 66% brake horsepower (BHP) when cruising at an altitude of 10,000 feet in standard conditions, with an engine speed of 2,500 rpm. At that power setting, the engine will consume 9.5 GPH. At 2,500 feet and 2500 rpm, the engine will produce 79% BHP, and consume 11.5 GPH.

Takeoff and climb rate data garnered from the manual, indicated that based on maximum gross weight with the accident weather conditions, zero flaps, and at 5,000 feet mean sea level, the ground roll would have been 1,217 feet. The distance required to clear a 50-foot obstacle would have been 2,307 feet, with a climb rate of about 574 feet per minute.

The 'Take-Off' section of the manual states the following under the 'Power Check' subsection:

"Prior to take-off from short fields above 3,000 feet elevation, the mixture should be leaned in accordance with the maximum power fuel flow placard located on the instrument control pedestal"

The maximum power fuel flow placard reported fuel flow for maximum engine power at various altitudes. Neither the manual, nor the placard provided specific instructions for leaning procedures for before takeoff. The pilot reported that he leaned the engine fuel mixture during taxi, but could not recall the setting for takeoff.

ADDITIONAL INFORMATION

Multiple plastic fascia items were replaced during the avionics system upgrade, and as such, some of the original placards, including the maximum power fuel flow, cowl flap, trim, and fuel selector positions, could not be located in the cabin.

The gascolator was disassembled, and about 2 ounces of fuel was recovered. The fuel sample was tested for the presence of water utilizing SAR-GEL water detecting paste. No water was present. According to airport fueling records, a Cessna 182 was serviced with fuel from the same pump as the accident airplane about 10 minutes prior. The Cessna 182 subsequently departed uneventfully.

NTSB Probable Cause

The pilot did not attain and maintain an adequate airspeed during the takeoff initial climb, which resulted in an aerodynamic stall.

© 2009-2020 Lee C. Baker / Crosswind Software, LLC. For informational purposes only.