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C-GJOL accident description

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Crash location 33.833334°N, 116.500000°W
Nearest city Palm Springs, CA
33.830296°N, 116.545292°W
2.6 miles away
Tail number C-GJOL
Accident date 23 Nov 2014
Aircraft type Embraer EMB-505
Additional details: None

NTSB Factual Report

HISTORY OF FLIGHT

On November 23, 2014, about 1104 Pacific standard time, an Embraer EMB-505 airplane, C-GJOL, experienced an uncommanded severe yaw to the right immediately after takeoff from the Palm Springs International Airport (PSP), Palm Springs, California. Neither the airline transport pilot or the 4 passengers on board were injured. The airplane, which was owned by a private individual, was operated by Hawkeye Aviation Holdings Ltd, Kelowna, British Columbia. Visual meteorological conditions prevailed for the planned cross-country flight, which was being operated in accordance with 14 Code of Federal Regulations Part 91. The left wing received minor damage during the landing. An instrument flight rules flight plan was in effect at the time of the event, with Springbank, British Columbia, the reported destination.

In a statement provided to the National Transportation Safety Board investigator-in-charge, the pilot reported that prior to takeoff the preflight preparations were normal, including the removal of the control lock pin. The pilot stated that the initial taxi out was normal, although he "detected an abnormal 'feel' to the rudders." All turns to runway 13L were right turns, which the pilot described as "easily executed." The pilot opined that the initial takeoff acceleration was normal, but at some point he drifted slightly right of centerline. Upon rotation the pilot noticed a significant yaw tendency to the right, accompanied by a significant roll to the right. The pilot stated that both tendencies were easily counteracted by application of left aileron, after which he flew the departure procedure to the best of his ability. The pilot reported that due to the surrounding terrain, he elected to climb to a safe altitude in order to deal with the problem. At this time the airplane was uncoordinated, with the electronic slip indicator displaced significantly to the left. The pilot stated that he was continuously applying left rudder in an attempt to correct the yaw [to the right], ran the yaw trim to the left, but it did help in resolving the situation.

The pilot reported that he climbed to about 11,000 feet, and at some point received fuel imbalance warning due to the uncoordinated flight. After advising air traffic control that he had a control issue, he was cleared for a visual approach to runway 31L at PSP. The pilot subsequently asked the passenger who was occupying the right front pilot seat, a private pilot, to assume the pressure on the left rudder so he could rest his leg prior to the landing. The pilot stated during final approach, he took control of the rudder and performed the landing.

The pilot opined that the touchdown was normal; however, after touchdown the aircraft began to drift right of the center line, as there was a left to right crosswind at the time of the landing. The pilot stated that trying to correct the drift with rudder was to no avail, he used aileron and power to the best of his ability. In the process the right wing lifted and the left wing tip contacted the runway, which resulted in minor damage. The pilot added that he was able to bring the airplane under control, exited onto the taxiway, and taxied to the local fixed based operator and shut down.

An examination of the airplane shortly after the incident revealed that the airplane's gust lock actuator had failed in the locked position. Under the supervision of a Federal Aviation Administration aviation safety inspector, the component was removed from the airplane and taken into possession of the NTSB IIC.

PERSONNEL INFORMATION

The pilot, age 60, possessed a current Canadian issued airline transport pilot certificate, with airplane single-engine land, multiengine land, and instrument airplane ratings. The pilot also possessed a Canadian designated E55P type rating, which is the Canadian designator for the EMB-505 airplane. Additionally, the pilot's most recent flight review was completed on April 26, 2014, and his most recent first-class airman medical examination was performed on August 5, 2014.

The pilot reported a total flying time of 13,185 hours, with 4,178 hours in multiengine airplanes, and 368 hours in the EMB 505 make and model. The pilot also reported a total number of hours flown in the last 90 days and 30 days to be 147 and 35 hours respectively, with 21 hours in make and model.

AIRCRAFT INFORMATION

The airplane involved in the incident was an Embrarer EMB-505, Canadian registration C-GJOL, serial number 5050009, manufactured in 2013. The airplane is a twin-engine cantilever monoplane with a low-positioned, swept wing. It is equipped with two rear positioned Pratt and Whitney Canada 535E turbofan engines, one on each side of the fuselage. The airplane can accommodate 2 crewmembers and 7 passengers; if operated single-pilot, it can accommodate an additional passenger. The airplane is equipped with an airstair door on the left forward side of the fuselage, single-point refueling, and a private lavatory.

The EMB-505 was equipped with an Umbra Group gust lock actuator, serial number 00075. The actuator was designed specifically to prevent rudder surface movement due to ground gusts.

According to documentation provided by the manufacturer, Umbra Cusinetti, the actuator, S/N 00075, was delivered by Umbra to Embraer on February 28, 2011. It subsequently failed during tests on aircraft S/N 00052, at the Embraer assembly line on May 19, 2011. The non-conformity report by Embraer stated, "Rudder gust lock actuator inoperative". The actuator was then returned to Umbra by Embraer on July 15, 2011. Umbra replaced both microswitches and returned the actuator to Embraer on November 28, 2011. Embraer then installed the actuator on the incident airplane, C-GJOL.

Rudder Gust Lock Actuator

General Description

The EMB-505 flight controls have a control lock system installed which is designed to prevent damage to the control column and flight control systems caused by wind gusts. There are two parts of the control lock system, namely the elevator and aileron control lock and the rudder control lock.

The aileron, rudder and elevator control systems are locked by means of the installation of the gust lock safety pin in the pilot control yoke assembly. The rudder gust lock actuator is installed in the aircraft's rear fuselage, at frame 46. The function of the rudder gust lock is to prevent rudder surface movement due to ground gusts by locking the rudder control system at the rear fuselage torque tube.

In order to preclude in-flight uncommanded locking, the system has the following interlocks:

• TLA (Thrust Lever Angle)

• WOW (Weight-on-Wheels)

No maintenance is required over the rudder gust lock actuators life.

Components

The gust lock system comprises the following elements:

• Aileron/rudder/elevator gust lock cockpit assembly

• Gust lock safety pin

• Rudder gust lock mechanism

• Gust lock quadrant

The rudder gust lock mechanism has the following elements:

• Gust lock actuator

• Command spring

• Bellcrank

• Control box with connector

The bellcrank, pivoted by the action of the actuator, locks one of the grooves on the gust lock quadrant, which is connected to the rudder rear torque tube, thereby preventing the movement of the rudder surface in case of wind gust.

Operation

The aileron control system and the elevator control system are mechanically locked by means of the installation of the gust lock pin in the pilot's control yoke assembly. The rudder control system gust lock mechanism is actuated through an electromechanical actuator.

When the gust lock safety pin is inserted into the pilot's control wheel to lock the aileron and elevator control system, two switches are activated, providing automatic engagement of the rudder gust lock system.

When the aileron and elevator control systems are unlocked by the removal of the gust pin, the rudder gust lock system is designed to be automatically disengaged. As designed, the rudder gust lock system in a locked position is evident to the pilots because of the following conditions:

• Gust lock pin is inserted in its hole.

• Both pedals are locked in a deflected position.

• Aircraft cannot taxi with rudder surface locked.

METEOROLOGICAL INFORMATION

At 1052, the PSP automated weather reporting facility indicated wind calm, visibility 45 miles, sky clear, temperature 19°C, dew point 10°C, and an altimeter setting of 30.08 inches of mercury.

WRECKAGE AND IMPACT INFORMATION

The only reported damage to the airplane, which occurred during the landing rollout, was a minor scrape on the underside of the left wingtip, and some damage to the associated strobe light.

TESTS AND RESEARCH

Computed Tomography (CT Scanning)

Under the supervision of a lead aerospace engineer assigned to the NTSB's Aviation Engineering Division, located at NTSB Headquarters, Washington, D.C., the rudder gust lock actuator was subjected to x-ray computed tomography (CT) scanning to document its internal condition. The scanning was conducted from December 24, 2014 to March 23, 2015. The scans were performed by Varian Medical Systems, Inc. (formerly Bio-Imaging Research, Inc. (BIR) using a combination of the Varian Actis 500/225 microfocus CT system and the Actis 500/450 standard focus CT system.

For the CT scans, the component was loaded into the imaging unit and placed on a turntable. It was then rotated in front of the x-ray source, and the x-rays were captured by a detector after they went through the part. The x-ray source produced a fan beam of x-rays, and the portion of the part imaged was adjusted slightly after each scan was completed until the entire assembly was scanned. The x-ray energy levels captured by the detector were recorded at several thousand different points during each rotation. This information was then converted into slice images using a reconstruction algorithm.

The actuator was scanned using a total of 6,421 slices. The total size of the combined data sets was 50.26 Gb. The actuator was scanned multiple times with different scanning protocols using both the microfocus imaging system and the standard focus imaging systems. The microfocus scans provided the best possible spatial resolution, but this type of imaging was constrained to a lower power level that resulted in streaking artifacts within the images. The standard focus scans used a higher power level (with a lower spatial resolution), but these higher power levels eliminated the streak artifacts, and had an inherently higher contrast resolution. Target CT imaging using the microfocus system was used for selected areas to get the highest possible resolution. In addition, the entire part scans and the limit switch scans were re-reconstructed using different reconstruction parameters in an effort to highlight the low density components within the scans.

Each data set of slice images was evaluated using the VGStudioMax software package to create orthogonal slice images and a three-dimensional reconstructed image of the component. As part of the evaluation, some sections of the components were digitally removed or rendered transparent to allow closer observation of interior parts. In the images, the high density areas were shown as brighter shades of gray and lower density areas were shown as darker shades of gray. The pointers shown in some of the images denote specific areas of interest within that image. The images of the actuator were examined for any signs of missing or damaged parts, contamination, obstructed passages or any other anomalies.

Computed Tomography results revealed the following:

• The extend limit switch contacts appeared to be closed during the standard focus scans, and open during the microfocus scans. Whether this difference was due to an actual position change of the contacts or due to the resolution differences of the two scanning methods, could not be determined.

• The extend and retract limit switch plungers were extended different lengths (0.87 mm and 1.26 mm respectively).

• High and medium density particles were found in various locations throughout the actuator.

• A low density indication within one of the extend limit switch screws was only visible in the standard focus scans and not the microfocus scans – this indication is consistent with the apparent low density area being a scanning artifact.

• Indications of a crack in the ball screw that were noted in the standard focus scans were more completely resolved in the microfocus scans as the balls and groove located on the ball screw. However, there was an indication of a discontinuity within one of the balls shown on the microfocus images.

• There were indications of two areas with distorted windings within the solenoid. Neither of these areas appeared to contain breaks in the windings, nor did either area contact the solenoid plunger

• Review of the solenoid images using enhanced contrast methods indicated that there was material containing voids within the passages of the solenoid.

• A high density particle was noted within the solenoid within the area of the piston to housing gap.

(Refer to the Computed Tomography Specialist's Factual Report, which is appended to the docket for this report.)

Rudder gust lock actuator examination by Umbra Cusinetti

The rudder gust lock actuator was examined by the manufacturer, Umbra Cusinetti, in the presence of an Italian ASNV representative on June 16, 2015.

According to the Umbra Failure Analysis Report, dated November 11, 2015, the results of the examination revealed the following:

Initial Visual Inspection

• It was observed during the visual inspection that the actuator was locked in a position close to the extended one.

Disassembly and Reported Observations

• when the actuator was placed on a test rig, it did not move when maximum current at rated voltage was supplied.

• when the actuator cover was removed the solenoid/locking system was exposed.

• the electrical board was moved to the side but remained connected.

• the cam that operates the microswitch was observed closed to the microswitch actuating lever, but did not operate it.

• the solenoid was not disassembled.

• the solenoid/locking system was observed locked in the extended position.

• the Pin position was observed close to the full extended position. Measurement of the exact position was prevented by Pin misalignment due to the distortion of the solenoid plastic reel.

• functionality of the microswitch was checked, with positive results.

• when the cap was removed it was observed that the ballscrew moved freely. The cap did not show any signs of interference with closed items.

• resistance of the three windings were acceptable.

• the motor brushes were not checked.

• the rotor OD showed signs of possible interference with the stator.

• the bearings were found operative with no axial play.

Conclusion of the Umbra Cusinetti Examination

The solenoid/locking system was found seized at approximately the full extended position

Rudder Gust Lock Circuit Board Examination

The electronic circuit board within the actuator was examined by the manufacturer, Umbra Cusinetti, on October 14, 2015, in the presence of an Italian ASNV representative. According to the Umbra Failure Analysis Report, dated November 11, 2015, the results of the examination revealed that no evidence of a mechanical failure on components and PCB. Surface coatings have been found damaged.

According to the NTSB Systems Group Chairman's Factual Report, Embraer provided the following comments relative to the Umbra Cusinetti examination:

Rudder Gust Lock Actuator Position Determination

Embraer determined that the rudder gust lock actuator dimensional information gathered during the Umbra Cusinetti examination revealed that with the screwshaft in the "as found" position, the bellcrank would be in contact with the rudder quadrant. It could also engage in the slots on the rudder quadrant.

Rudder Gust Lock Actuator Irreversibility, Spring Forces, and Component Replacement - Embraer Evaluation

Additionally, Embraer commented that the irreversibility of the gust

NTSB Probable Cause

The failure of the gust lock actuator solenoid for reasons that could not be determined because postaccident examination of the rudder gust lock system revealed no mechanical malfunctions or failures that would have precluded normal operation.

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