Crash location | 33.896666°N, 117.574167°W |
Nearest city | Corona, CA
33.875293°N, 117.566438°W 1.5 miles away |
Tail number | N1133S |
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Accident date | 04 May 2003 |
Aircraft type | Cessna 411 |
Additional details: | None |
HISTORY OF FLIGHT
On May 4, 2003, at 1453 Pacific daylight time, the pilot of a Cessna 411 twin engine airplane, N1133S, lost control and collided with terrain approximately 2 miles east of the Corona Municipal Airport, Corona, California. The pilot/owner was operating the airplane under the provisions of 14 CFR Part 91. The commercial pilot, who was the sole occupant, received fatal injuries. The airplane was destroyed. Day visual meteorological conditions prevailed, and no flight plan had been filed. The flight originated from the Corona airport around 1430, and was en route to Santa Monica, California.
According to Air Traffic Control (ATC) communications, and family members, the purpose of the flight was to deliver the airplane to Santa Monica Propeller for maintenance on one of the airplane's propellers. The pilot checked in with Southern California Approach (SoCal Approach) and requested flight following to Santa Monica. Approximately 3 minutes after checking in with SoCal approach, the pilot reported having engine difficulties and was returning to Corona. SoCal approach assisted the pilot with vectors to Corona Airport. SoCal approach lost radar contact with the airplane approximately 3 miles to the east of Corona Airport. So Cal approach advised loss of radar contact then instructed the pilot to change to the airport advisory frequency, which the pilot acknowledged.
The airplane flew over several witnesses who were within 1/2 mile of the accident site. They reported to the National Transportation Safety Board investigator-in-charge (IIC) that they observed the airplane flying "very low," about 300 to 500 feet msl. The airplane was heading toward the Corona airport. The witnesses reported consistent observations of the airplane "wobbling," then going into a steep knife-edge left bank before it dove into the ground. The wreckage was immediately located by police and fire rescue crews who extinguished a fire on the right side of the airplane.
PERSONNEL INFORMATION
The pilot obtained his third-class medical certificate on March 25, 2002. His medical was valid with no limitations.
Examination of the pilot's logbook and Federal Aviation Administration (FAA) records revealed the pilot received his commercial pilot certificate, single engine land, and instrument ratings through military competency on May 4, 1960. He received his multiengine land rating on May 17, 1999. The pilot had accumulated about 4,899 total flight hours with approximately 412 hours in the Cessna 411.
In the Riverside Automated Flight Service Station re-recording of the pilot requesting a weather brief, the pilot can be heard to say in a side conversation while he was waiting for a briefer, "Thank you very much for coming and helping I,...its been four and a half months since I've been in an airplane, I can't even figure out how to put the radios back in."
AIRCRAFT INFORMATION
The twin engine, low wing airplane was powered by two Teledyne Continental GSTIO-520-C engines. The airplane's serial number was: 411-0202. The airplane and engines underwent their last annual inspection on March 19, 2003, at an aircraft total time of 4,915 hours, and 86.5 hours since the last inspection in 2002. The total time since the last engine overhaul was 503 hours on the right engine and 563 hours on the left engine.
An aircraft logbook entry dated March 19, 2003, indicated the aircraft annual inspection was completed; however, the left propeller did not comply with AD 95-24-05 RI: "The propeller must be inspected by a certified person. Completion of AD 95-24-05RI will make the aircraft airworthy."
The mechanic who performed the last annual inspection provided copies of his discrepancy notes pertaining to the accident airplane to the Safety Board IIC. In those documents it is noted that the left propeller was leaking red dye.
According to Corona Aircraft Sales, the airplane had been placed on their sales lot to be sold. The airplane had not been flown since the completion of the annual inspection.
AIR TRAFFIC CONTROL AND RADAR DATA
Review of the Air Traffic Control (ATC) communications re-recording and radar plot data revealed that the pilot had been in communications with Southern California Approach. Upon initial contact with SoCal approach the airplane was observed by the controller to be heading east, away from Santa Monica. When the controller queried the pilot, the pilot said his GPS indicated he was heading the correct direction. The controller informed the pilot that he was heading east when Santa Monica was to the west, and gave the pilot an appropriate heading towards his stated destination. Approximately 3 minutes 15 seconds after initial contact with SoCal approach, and at an altitude of 4,000 feet, the pilot reported an "engine cutting out" and intended to return to Corona airport. The SoCal approach controller observed the airplane descend in altitude, assisted the pilot with vectors to Corona Airport, and expressed concern about the airplane's ability to maintain altitude. The pilot reassured the controller that he could maintain altitude. Approximately 3 miles east of Corona airport the controller reported that radar contact was lost and to switch to the airport advisory frequency. The pilot acknowledged this last communication.
Radar and radio communication re-recordings and data files were obtained from Southern California TRACON and a plot was generated by a private vendor for the Cessna Aircraft Company. A copy of the plot and communication transcripts is attached to this report. It shows the aircraft departing Corona airport, climbing to 4,000 feet, turning back towards Corona, and continuously descending until radar contact is lost at about 700 feet agl and 85 knots ground speed.
WRECKAGE AND IMPACT INFORMATION
The airplane wreckage was located in a construction site on a small plateau approximately 30 feet above River Road to the east. The dirt plateau falls away into a drainage culvert approximately 75 feet below to the north. The construction site was barren of all trees and brush. The plateau had an approximate 20-degree slope downwards to River Road. The wreckage location was recorded with a global positioning system as latitude north 33 degrees 53.794 minutes, longitude west 117 degrees 34.275 minutes at an elevation of 590 feet.
All major components of the airplane were present at the accident site. The airplane was oriented on a bearing of 310 degrees magnetic. The airplane was laying upright with the landing gear collapsed underneath the fuselage. The nose, flight deck, and instrument panel of the airplane were completely destroyed. The engine control quadrant; throttle, propeller, and mixture control levers were all found parallel, in the full forward position. The circuit breaker panels had pulled apart. Most circuit breakers were popped or broken, posts sheared, and extended out of position.
The right wing exhibited fire damage outboard of the right engine. The entire right engine was twisted 90 degrees along its longitudinal axis so that the engine cylinders were directed vertically. The crankshaft propeller flange exhibited torsional shearing and the propeller was not attached to the engine. The right wing leading edge and fuel tip tank were crushed aft to the wing spar and thermally damaged. The right aileron was consumed by fire but the aileron spar was attached to its respective hinge points. The right aileron flight control cables were present and attached to the aileron bellcrank and push rod, which connect to the aileron.
The right side of the fuselage was split along an upper longitudinal rivet line and laying open from aft of the upper corner of the emergency exit to the leading edge of the horizontal stabilizer.
The last outboard quarter of the right horizontal stabilizer had a 20-degree bend upward. The rudder had skin wrinkles along the rivet line that extends horizontally from the upper hinge. The left horizontal stabilizer and elevator displayed no apparent damage.
The left side of the fuselage was split aft horizontally along a lower rivet line from the bottom corner of the main cabin door. The top half of the split cabin door was jarred open. The bottom half of the cabin door was detached, and found laying on the ground 3 feet in front of the doorframe location, but remained attached to the airplane by its chain handrail.
The left wing was attached to the fuselage. The engine had detached from the firewall and was laying on top of the wing with a pivot point at the outboard intersection of the nacelle and wing leading edge. The propeller remained attached to the engine. The section of the wing outboard of the nacelle exhibited leading edge crushing and deformation. This section was also twisted about the wing spar upward approximately 110 degrees and passed through the vertical plane. The wing tip fuel tank was detached and located 30 feet from the wing tip. The wing tip tank had a softball sized hole in the forward section. Dirt beneath the tip tank hole had a slight gasoline odor. Neither the wing tip tank nor the interior baffle of the tank exhibited any evidence of hydraulic deformation.
The left propeller blades exhibited aft bending and slight chordwise scratches. The spinner was crushed aft without torsional twisting and with folds that paralleled the aft face of the spinner.
The right propeller was located approximately 7 feet from the right wing tip in line with the lateral axis of the airplane. The spinner, hub, and blades were buried about 12 inches into the ground, which formed a cratered area 4 feet across. The blades exhibited chordwise scratching and trailing edge buckling, forming a sinusoidal type bend.
Witnesses reported seeing the airplane flying very low, approximately 500 feet agl, towards Corona airport
MEDICAL AND PATHOLOGICAL INFORMATION
The Riverside County Sheriff-Coroner conducted an autopsy on the pilot. According to the coroner's report, the pilot died of multiple blunt force traumatic injuries and no preaccident anomalies were noted.
A toxicology test for ethanol and drugs were negative.
TESTS AND RESEARCH
Airframe:
The flap drive gears attached to the flap motor were observed at the aft sprocket with flap drive chain running to the left wing showing 2-3 chain links extended on top. The forward sprocket with the flap drive chain running to the right wing showed 2 chain links extended from the bottom. The Cessna 411 service manual states that this corresponded to the flaps retracted position.
Control cables were traced from the elevator, rudder, and aileron control surfaces to the cockpit control column and rudder pedals. The control cables were found attached to their respective control arms and control surfaces. The elevator trim actuator was measured extended 1.25 inches.
The two fuel selector valves for the left and right main fuel tanks corresponded to the cockpit fuel selector positions, which were set at the left and right main fuel tank positions. Approximately 4 ounces of fuel was collected from the left fuel selector valve. One bead of water was present. Approximately 2 ounces of fuel was collected from the right fuel selector valve with no water evident. Approximately 1/8 ounce of fuel was observed in the left engine fuel manifold valve. No fuel was found in the right engine fuel manifold valve. All fuel filler cap rubber o-rings were present and displayed a degree of flexibility with no apparent cracks.
Both fuel pumps, the auxiliary fuel pump, and fuel transfer pump from each main tank were removed and examined. The right wing fuel pumps were thermally damaged by fire and not functional but electrical connections were observed intact on both units. The left wing fuel pumps appeared to be in good condition with intact electrical connections and were tested for operation. The left auxiliary pump and fuel transfer pumps were wired with an external power source and tested using water as a working fluid. The purpose of the test was to determine if the fuel pumps were capable of operating. The left auxiliary pump operated and produced approximately a flow rate of 2.4 gallons per minute. The left fuel transfer pump operated and produced a flow rate of approximately 0.3 gallons per minute.
A Cessna service letter dating June 27, 1967, directed the installation of wing tip tank fuel pumps intended to maintain a constant fuel supply at the wing tank fuel outlet at all times. This letter alerted the owners of possible fuel starvation during steep descents. The Cessna 411 service manual states that the purpose of these fuel transfer pumps "is to transfer fuel from the forward end of the main tanks to the center baffle area where it is picked up and routed to the engine by either the engine-driven pump or the auxiliary fuel pump." These pumps are powered from the landing light circuits. The mechanic who performed the aircraft's required annual maintenance mentioned that in order to keep the fuel transfer pumps from running continuously when power was on the airplane the mechanics would pull the landing light circuit breakers while performing maintenance.
The landing gear actuator upper bellcrank was aligned with the lateral axis. Per the Cessna 411 service manual, this position corresponds to the landing gear down position.
Engine control cables remained attached to their respective control arms, and the cables were traced to the appropriate engine component attach points.
Engines:
Both the left and right engines were sent to Teledyne Continental Motors, Mobile, Alabama, for teardown and evaluation under the supervision of the Safety Board IIC. According to Teledyne Continental technicians, both engines exhibited normal operating signatures. All spark plugs were clean with no mechanical deformation. The spark plug electrodes were gray in color, which corresponded to normal operation according to the Champion Aviation Check-A-Plug AV-27 Chart. The magnetos were bench tested and produced sparks on all leads in firing order. Investigators manually rotated the engines. The engines rotated freely and the valves moved approximately the same amount of lift in firing order. Investigators obtained thumb compression on all cylinders in firing order. The fuel pump rotors turned freely, were unfractured with inner diaphragms, and rubber seals unbroken. The plunger in the fuel distribution valve moved freely, the rubber diaphragm was unbroken, and investigators did not observe any contamination. The oil sump screens were clean and open. The engines oil filters were examined and contained no metal debris. The governor screens were clean. The oil screen filters were clean. The fuel nozzles were open and the screens were clean.
Propellers:
Both propellers were sent to McCauley Propeller Systems, the manufacturer, for examination under supervision of investigators from the Safety Board. McCauley engineers concluded the following:
1. All propeller damage was the type associated with impact forces.
2. Feather stop mechanisms of each propeller we undamaged indicating mechanisms were not engaged at impact.
3. Counterweight impact marks found on the hub sockets of both propellers indicate that both propellers were operating near the low pitch range at impact.
4. Damage to the right propeller was extensive and included the break-up of the crankshaft flange indicating power at impact.
5. Left propeller overall damage was significantly less than that of the right propeller indicating lower energy (power) at impact.
ADDITIONAL INFORMATION
Fueling Information:
No fueling records were found at the Corona airport. The last location of the airplane prior to its arrival at Corona was Bermuda Dunes, California. Bermuda Dunes records show the airplane as fueled on October 31, 2002, taking on 56.2 gallons. Witnesses reported that the airplane did not take on any fuel immediately prior to the flight on May 4th..
Single Engine Flight Operations:
The "Airplane Flying Handbook" (FAA-H-8083-3) discusses the identification and the effects caused by a failure of the critical engine in a multiengine airplane.
"In m
The failure of the pilot to properly configure the airplane for a one engine inoperative condition (including his failure to feather the propeller of the affected engine, retract the landing gear, and maintain minimum single engine speed). Factors related to the accident were fuel starvation of the left engine, due to an inadequate fuel supply in the left tanks, inoperative fuel transfer pumps, and the pilot's decision to takeoff with out fueling.