Crash location | Unknown |
Nearest city | Glenn, CA
39.521828°N, 122.013865°W |
Tail number | N6258Z |
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Accident date | 21 Feb 1999 |
Aircraft type | Bell UH-1H |
Additional details: | None |
HISTORY OF FLIGHT
On February 21, 1999, at 1510 hours Pacific standard time, a Bell UH-1H helicopter, N6258Z, collided with the ground following a pilot report of an in-flight control system failure while conducting an aerial spraying operation near Glenn, California. The airline transport pilot was seriously injured during the accident sequence, and died in the hospital during a surgical procedure on February 23, 1999. The helicopter, owned and operated by Avag, Inc., was destroyed during the crash sequence. The aircraft was operating under 14 CFR Part 137 of the Federal Aviation Regulations when the accident occurred. The helicopter had departed a dirt-landing zone after being serviced with spraying chemicals moments before the crash. Visual meteorological conditions prevailed at the time and a flight plan was not filed for the flight.
The pilot told his son, who visited him in the hospital, that the helicopter kept banking in one direction and there was nothing he could do to stop it. He reported that his father said he lost control of the "systems" on the helicopter, that it was a mechanical failure of some sort, and that all of a sudden, the helicopter started veering to the right and as he tried to manipulate the controls, he was unable to change the direction of the helicopter's movement.
In his written report, the owner of the company reported that the pilot was just finishing a spray run on an almond orchard when the helicopter impacted the ground in a nose low attitude. He stated that there was a powerline approximately 5 to 8 tree rows (approximately 100 feet) in the orchard perpendicular to the path of flight. He stated that he thought the pilot flew up and over the powerline, and while descending back to the almond orchard the tail of the helicopter hit the powerline causing a tail high or nose low attitude. The pilot reportedly told him that after he went over the powerline, he heard a noise and lost control.
PERSONNEL INFORMATION
According to all sources of information, the pilot had accrued a total flight time in excess of 32,600 hours, with over 29,900 hours in various helicopters. A review of Federal Aviation Administration (FAA) airman records disclosed that he held an airline transport pilot certificate with a rotorcraft helicopter rating, and commercial pilot privileges in single engine land airplanes. The pilot held type ratings in the following helicopters: Sikorsky S-58, Sikorsky S-61, Sikorsky S-62, and the Boeing Vertol BV-44.
The owner of the company said that the pilot had not complained of any medical problems. He said that the pilot jogged regularly and was very health conscious. The owner said that he arrived at the crash site shortly after the crash and that the pilot was conscious and talking, complaining that his legs hurt.
WRECKAGE AND IMPACT
On February 24, 1999, at the request of Safety Board investigators, a technical representative from the Flight Safety Department of Bell Helicopter Textron, (BHT) traveled to Richvale, California, to examine the helicopter wreckage under the supervision of two inspectors from the FAA's Sacramento Flight Standards District Office. According to the BHT report, examination of the wreckage revealed that the main fuselage and tailboom were intact. Upward crushing and deformation were seen on the belly of the cabin, which was more severe on the right-hand side of the helicopter. Deformation was also present in the floor structure below the right front (pilot's) seat. The occupant restraints were intact and the right front seat did not exhibit evidence of deformation. The landing skids were separated from the fuselage, with overload fractures seen at the left rear, right rear, and left front crosstube/skid tube attachment fittings. The right side of the forward crosstube was fractured in overload outboard of the belly attachment fitting.
The tailboom was still attached to the fuselage and was relatively undamaged. A hole was observed in the left side of the tail rotor driveshaft cover on the fin, matching the dimensional geometry of the tailrotor blade. Examination of the tail stinger revealed a series of dark colored parallel lines, which were located on the left-hand underside of the stinger. According to BHT, these markings were present from several inches aft of the stinger's exit from the tailboom fairing all the way back to the aft end. The marks were described as approximately 1/2 inch in length and 1/8 inch apart.
The main transmission separated from the fuselage with overload fracture of the lower mounting flange of the transmission main case. The K-Flex main driveshaft was separated from the engine and transmission from overload fracturing of the load beams. The tail rotor driveshaft was intact and all the couplings and hanger bearings appeared to be in good condition. The tail rotor 42- and 90-degree gearboxes were intact and operable.
Control continuity was established from the cyclic, collective, and pedal controls in the cockpit to the hydraulic servos. The main rotor and tail rotor hydraulic servo actuators manually operated smoothly. The cyclic and collective boost tube extensions at the top of the servo actuators were fractured in overload at the riveted joints. The fluid lines from the pump to the servos, regulator, and filter modules were intact. The hydraulic reservoir had been broken loose from its mounting and a large hole had been punched in its left side.
The main rotor hub and control system was observed to be still attached to the mast, with the swashplate and sleeve assembly intact and operable. One of the scissors to equalizer link control tubes was fractured and the other was intact. Both swashplate drive links were separated from the swashplate due to fractures of the trunnion housings in the swashplate outer ring casting. The trunnions were still attached to the lower ends of the drive links. The scissors were intact and operable. The main rotor hub assembly was intact and the feathering and flapping axes moved freely. Additionally, it was noted that the stabilizer bar assembly was intact and operable.
TESTS AND RESEARCH
The hydraulic pump was removed from the transmission by the FAA inspectors and was sent to the Safety Board's South Central Regional Office. On April 29, 1999, the pump was taken to BHT by a Safety Board investigator for testing. The hydraulic pump was set up on a bench test cell and run according to BHT standards. The pump operated at the following specifications: at 4,170 rpm and 900 psig (+100, -0) the flow standard was 6 gpm (+0, -1). The pump flow while running on the test stand was 5.75 gpm.
The outlet pressure standard was 1,000 psig (+ -25). The pressure was recorded at 1,050 psig. Additionally, a cavitation test was performed. No surging noise was heard and no air bubbles were observed in the flowrator. BHT concluded that the pump operated normally and no deviations from the acceptance criteria for new and overhauled pumps were observed which could have affected the pump's performance in the helicopter.
The three UH-1H hydraulic servo actuators were examined and bench tested at BHT under the supervision of a Safety Board investigator. Following an external examination, the actuators were installed in a flow bench and tested in accordance with Bell laboratory test procedure FW 211 Rev. R. The purpose of the test was to verify general functionality of the actuators. Installation of the units in the test bench required the installation of irreversible valves on the units. The bench test results presented in Table 1 of the attached BHT servo actuator report notes that each servo actuator operated smoothly in both the extend and retract direction. BHT concluded that the movement rates appeared normal. They did note, however, that the minimum operating pressure was exceeded and was likely due to the servo actuators being tested with the irreversible valves installed.
The tail boom stinger and an exemplar sample of the 14-inch copper powerline from the orchard were taken to Materials Analysis, Inc., in Dallas, Texas for examination and EDS analysis by Safety Board personnel. On the bottom right side of the stinger there were about 40 1/2-inch black, paralleling marks separated by an equal distance of about 1/4-inch. Two of the marks were examined under the scanning electron microscope (SEM) to see if the marks contained copper or copper oxide. There was no copper. The stinger was examined under a microscope and it was determined that there was no evidence of any copper wire transfer to the stinger.
MEDICAL AND PATHOLOGICAL INFORMATION
An autopsy on the pilot was performed by the County of Santa Clara Office of the Medical Examiner-Coroner's office, with tissue and fluid samples retained for toxicological examination. The samples were submitted to the FAA Civil Aeromedical Institute (CAMI) in Oklahoma City, Oklahoma.
According to the Manager, Toxicology and Accident Research in Oklahoma City, the samples from the pilot were positive for the following substances:
0.3 (ug/ml, ug/g) Lidocaine detected in Blood Atropine detected in Liver Fluid Lidocaine detected in Liver Fluid Procainamide detected in Liver Fluid N-Acetylprocainamide detected in Liver Fluid Atropine detected in Kidney Fluid Lidocaine detected in Kidney Fluid Procainamide detected in Kidney Fluid N-Acetylprocainamide detected in Kidney Fluid Ephedrine detected in Liver Fluid Ephedrine detected in Kidney Fluid.
A thorough review of the medications discovered on the toxicology evaluation revealed that they were consistent with emergency treatments provided during resuscitation efforts at the hospital.
According to the Assistant Medical Examiner-Coroner, the cause of death was Cardio-Respiratory Failure with adult respiratory distress syndrome, with a contributory factor of the compressed fracture, Lumbar Spine.
The pilot's hospital records, autopsy report, and a certified copy of his FAA medical records were obtained and reviewed by the Safety Board's medical officer. The medical records did not indicate any significant pre-existing condition.
ADDITIONAL INFORMATION
The wreckage was released to the registered owner at the conclusion of the tests and research on January 5, 2000.
An inflight loss of control for undetermined reasons.