Crash location | 37.763611°N, 120.926945°W |
Nearest city | Escalon, CA
37.797427°N, 120.996603°W 4.5 miles away |
Tail number | N9286U |
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Accident date | 02 Feb 2010 |
Aircraft type | Arrow Falcon Exporters Inc OH-58A |
Additional details: | None |
HISTORY OF FLIGHT
On February 2, 2010, about 1400 Pacific standard time, an Arrow Falcon Exporters, OH-58A helicopter, N9286U, landed hard in an orchard shortly after takeoff near Escalon, California. Cavanagh Flying Service was operating the helicopter under the provisions of Title 14 Code of Federal Regulations Part 91 as a positioning flight. The commercial pilot sustained serious injuries; the helicopter sustained substantial damage. The local flight departed from an orchard near Escalon. Visual meteorological conditions prevailed, and no flight plan had been filed.
The pilot left two voicemail messages for his mechanic about 30 minutes prior to the accident. In the messages he relayed that the helicopter was vibrating heavily, "did not have a whole lot of power," and that the dc generator caution light was illuminated. He further stated that he was experiencing, "big maintenance problems." He went on to comment that his work load was heavy, and he would attempt to fly the helicopter home.
According to a family member of the pilot, while fueling the helicopter prior to the accident flight, the pilot reported that the helicopter was vibrating. The pilot then proceeded to takeoff in the helicopter, and a short time later reported over the radio that the generator light was illuminated. Shortly thereafter, the pilot relayed the message, "I'm going down."
In a written statement, the pilot reported that shortly after departure, at an altitude of about 200 feet above ground level, the engine lost power. He performed a forced landing and the helicopter landed hard, sustaining substantial damage to the entire fuselage structure.
HELICOPTER INFORMATION
The helicopter, serial number 69-16198, was equipped with a Rolls-Royce/Allison T63-A-720 gas turbine engine, serial number 405588. In February 1997 it received a restricted class airworthiness certificate under the agricultural and pest control category.
A review of the helicopter's logbooks revealed that during the last annual inspection dated December 7, 2009, the helicopter amassed a total airframe time of 7,549.3 flight hours, with a corresponding Hobbs hour meter time of 3,602.7. The corresponding entry for the annual inspection in the engine logbook indicated, "Eng TT 1,776.3."
An entry in the engine logbook revealed that the fuel control unit was replaced on December 27, 2009, at a Hobbs hour meter time of 3,610.4.
The most recent logbook entry was for a 25-hour inspection, dated January 31, 2010, at a Hobbs hour meter time of 3,633.6. The Hobbs hour meter at the accident site indicated 3,636.6 hours.
TESTS AND RESEARCH
External Engine Exam
The engine was removed from the helicopter in the presence of the NTSB investigator-in-charge, and representatives from Rolls-Royce and Bell Helicopters. The engine compartment was largely intact and the engine appeared to have sustained minimal impact damage. Inward facing indentations were observed on the outer combustion case adjacent to the fuel igniter; additionally, the fuel nozzle/igniter boss appeared canted approximately 10 degrees from its normal plane.
Rotation of the N1 rotor by hand revealed it to be free and continuous from the compressor through to the starter generator. Additionally, rotation of the N2 rotor revealed it to be continuous from the 4th stage turbine through to the freewheeling unit output shaft. No indication of foreign object damage was noted at the compressor inlet and first stage wheel.
Examination of the engine fuel control unit (FCU) revealed that the pneumatic control line, part number 6870035, which connects the power turbine governor to the FCU, had fractured at the FCU connector. The line was noted displaced about 1/4-inch laterally from its fitting.
Pneumatic Control and Oil Sump Accessory Lines
Examination of the pneumatic control line revealed that it had fractured 0.42 inches from the end of the tube, adjacent to the end of the ferrule. A rub mark measuring about 0.125 inches in diameter was noted on the line adjacent to an oil sump accessory housing line, part number 6853464AL. The oil line displayed a corresponding rub mark. The pneumatic line was visually compared to an exemplar tube and appeared to be bent outwards in two planes.
Both lines were further examined by the Rolls-Royce metallurgical department. The examination revealed that the outer surfaces of the pneumatic line displayed several circumferential score marks adjacent to the fracture surface at the shoulder of the ferrule. The fracture face was examined utilizing a scanning electron microscope (SEM). Crack signatures were observed to progress radially at the tube wall in the area of the scoring, and progress circumferentially around the tube. Rolls-Royce stated that the fracture features were indicative of high cycle fatigue. A cross-section of the flared tube end revealed the existence of two additional cracks originating on the outer wall, which had not propagated through to the inner surface of the tube. According to Rolls-Royce, the pneumatic line was of an appropriate stainless steel type, and met the wall thickness and diameter dimensions specified in the engineering drawings.
Rolls-Royce produced an examination report, which was reviewed by the Safety Board Office of Research and Engineering, Materials Laboratory Division. The report is included in the public docket for this accident.
Engine Test
The engine was relocated to a Rolls-Royce service facility for further examination.
The damaged pneumatic and oil scavenge lines, and the impact damaged outer combustion case, were replaced with slave units in preparation for an engine test run. During their replacement it was noted that the fuel nozzle/igniter had sustained fretting damage in the area adjacent to the combustion liner. Additionally, a 2-inch-long section of the double lip flange at the base of the combustion liner was missing. The missing section was not located within the engine.
The engine was then installed in a Rolls-Royce engine test cell. The engine was started, and checked throughout its power range for about 1 hour; no anomalies were noted.
DC Starter-Generator
The starter-generator was removed from the engine for examination. A data plate on the side of the unit indicated that it was manufactured by Lear Siegler, Inc., model number of 23032-022, with a manufacture date of June 6, 1980.
Visual examination of the starter-generator revealed that the main bearing shield had become separated from the bearing, exposing the inner bearing race at the splined shaft. The shield was free on the shaft and appeared distorted. Both the race and shield exhibited a blue tint. Rotation of the starter-generator by hand resulted in a grinding sound emanating from within the unit. Additionally, about 1 millimeter of lateral play was noted in the splined shaft at the area of the main bearing.
ADDITIONAL INFORMATION
Rolls-Royce released a Customer Service Letter A-1166, MAINTENANCE WARNING – EXTERNAL LINES dated November 15, 1990, and revised February 5, 2007. The letter reiterated the need to adherence to operation and maintenance manual procedures regarding proper alignment, clamping, and torquing of engine tubing during installation. In part, the letter stated that failures in external tube lines can be caused by, "Bent tubes which induce misalignment at the flare and result in cracked flares or fretting of the tube at the end of the ferrule...Tube to fitting misalignment caused by poorly aligned fittings, which result in cracked flares or fretting of the tube at the end of the ferrule."
The Rolls-Royce Operation and Maintenance Manual 73-20-02 applicable to the accident engine described the fuel control removal and installation procedures in the section – Bendix Gas Producer Fuel Control – Maintenance Practices. The section states:
"WARNING: FAILURE TO PROPERLY INSTALL, ALIGN AND TIGHTEN FUEL, OIL, AND AIR FITTINGS AND TUBES COULD RESULT IN AN ENGINE FAILURE."
According to the Rolls-Royce representative, a leak in the pneumatic control line could result in a reduction in engine power, with a complete failure of the line likely causing an engine power loss to sub-idle conditions.
A loss of engine power during cruise flight due to the fatigue failure of the pneumatic fuel-to-governor control line. Also causal was the inadequate installation of the pneumatic line by maintenance personnel, and the pilot’s decision to continue flight with a known discrepancy.