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N86235 accident description

Colorado map... Colorado list
Crash location 40.015556°N, 105.049444°W
Nearest city Erie, CO
40.050262°N, 105.049982°W
2.4 miles away
Tail number N86235
Accident date 26 Jan 2015
Aircraft type Enstrom 280FX
Additional details: None

NTSB Factual Report

HISTORY OF FLIGHT

On January 26, 2015, about 1202 mountain standard time (MST), an Enstrom 280FX, N86235, was destroyed when it impacted terrain during final approach for landing at Erie Municipal Airport (EIK), Erie, Colorado. Both the instructor pilot and student pilot were fatally injured. The helicopter was registered to New Course Aviation Company and operated by Mountain One Helicopters as a 14 Code of Federal Regulations Part 91 instructional flight. Visual meteorological conditions prevailed for the local flight, which operated without a flight plan.

According to a witness interview, the helicopter was on final approach to land on the runway at what seemed like a steep angle of descent. As the helicopter descended, she heard a loud "pop." After the pop, the helicopter began to rotate and then the main rotor (MR) blades separated from the top of the helicopter. The remainder of the helicopter descended to ground impact and then "exploded."

All three MR blades were found during the on-scene investigation and were identified as blades #1 through #3. The #2 MR blade was found separated from the MR head, which still contained MR blades #1 and #3. Post accident examination revealed that the #2 MR blade had separated due to a fractured spindle.

PERSONNEL INFORMATION

AIRCRAFT INFORMATION

The helicopter, an Enstrom 280FX, was a three-seat, single-engine helicopter (serial number 2002) manufactured in 1985. The three-bladed MR system was powered by a turbo-charged Lycoming HIO-360-F1AD engine rated at 225 horsepower at 3050 rpm.

The inboard end of each main rotor blade is attached to its respective grip and drag link. Each rotor blade is attached to the outboard side of its respective grip via a retention bolt. At the inboard side of each grip, a pitch arm and drag link are attached to the leading and trailing sides, respectively, of the grip. Two feather bearings, which accommodate rotor blade pitch change motion, a bearing spacer, and a spindle are installed within the grip. A Lamiflex bearing, a spindle retention nut, and a cover are installed at the threaded outboard end of the spindle. Two flanges at the inboard end of the spindle attach to a universal block, the latter of which is attached to the main rotor hub, that accommodate rotor blade flapping and lead-lag motions. See figure 1.

According to the maintenance records, the most recent 100-hour inspection was completed on March 17, 2014, at an airframe total time of 9,167 hours. During this annual inspection, all three Lamiflex bearings were replaced. Additionally, all three MR grip assemblies were removed to "purge and clean" the flapping hinge bearings, then were reassembled and preloaded per the Enstrom Maintenance Manual. Lastly, the leading-edge tape was replaced on one of the MR blades; the helicopter was then flight tested and subsequently adjusted for proper track and balance. No other maintenance to the MR grips or blades was performed during this inspection or at any other time between the inspection and the accident.

According to the maintenance records, the #2 spindle, part number (P/N) 28-14282-13, serial number (S/N) 03-014-84N, had not been replaced since the helicopter's manufacture. At the time of the accident, the spindles were not life limited, and there were no recurrent inspections specified for the spindle threads. According to the Enstrom Maintenance Manual, the Lamiflex bearings required replacement every 5 years.

When the MR is assembled, the spindle threads reside under the retention nut retaining the Lamiflex bearing. The retention nut must be removed in order to examine the entire threaded region of the spindle for damage. It is unknown whether a thread crack, once grown to a sufficient depth, would produce an out-of-track MR blade. Examination of the maintenance records for the accident helicopter revealed at least 9 instances, from the time the helicopter was manufactured, of Lamiflex bearing replacement for the #2 spindle. (The Enstrom Maintenance Manual the Enstrom Maintenance manual requires the lamiflex bearing to be replaced every 5 years.) However, there was no pattern in the Lamiflex bearing replacement intervals or interrelated note of the helicopter's MR track and balance or the helicopter's flying characteristics.

During manufacture, the cotter pin hole in the spindle is match-drilled with the spindle retention nut installed. There is no specific requirement on the dimension for the cotter pin hole in the engineering drawing to break the sharp edges or chamfer the edges at the cotter pin hole after it is match-drilled. Breaking or chamfering the sharp edges is typically used to reduce stress concentrations that may arise from the matched-drill process.

METEOROLOGICAL INFORMATION

The 1155 weather observation at EIK reported no wind, visibility 10 miles, clear skies, temperature 09ºCelsius (C), dew point 11ºC; barometric altimeter setting 30.18 inches of mercury.

AIRPORT INFORMATION

EIK is a publicly-owned airport without an air traffic control tower. The airport was equipped with one runway designated as runway 15/33. Runway 15/33 was a 4,700-ft-long by 60-ft-wide runway and was reported as "in good condition." The elevation of the threshold of runway 15 was about 5,076 ft above mean sea level.

WRECKAGE AND IMPACT INFORMATION

The helicopter came to rest upright with the right skid low off the east side of the runway. The main wreckage contained the main fuselage (flight deck, skids, tail boom) and engine. The aircraft wreckage displayed severe damage from a high energy vertical impact and post impact fire.

The MR head (with the #1 and #3 MR blades still attached) and MR gearbox were located about 299 ft from the main wreckage at a heading of 350º. The threaded portion of the spindle and associated retention nut on the #2 blade was missing; however, the inboard portion of the spindle was still attached. The #2 MR blade assembly, including the blade, the grip, the threaded portion of the spindle, the retention nut, and the drag link, was located about 657 ft from the main wreckage at a heading of 263º. The #2 blade did not exhibit any damage or indications of contact with any part of the aircraft. An approximate 18-inch section of the leading edge spar and balance weight for the #1 rotor blade was located about 493 ft from the main wreckage at a heading of approximately 248º. The tail rotor blades were found about 290 ft and 666 ft from the main wreckage, at headings of 276º and 325º, respectively. Several other pieces of wreckage were scattered around the approach end of runway 15. The tail rotor gearbox was not located.

Flight control continuity was established in the cabin area from the controls up to the MR gearbox and MR hub. The Hobbs meter located in the center pedestal indicated 9,332.7 hours.

The tailboom exhibited a MR blade strike. Examination of the MR gearbox mounts indicated that the gearbox mounts were intact and separation from the airframe occurred at the pylon. The overrunning clutch operated normally.

During the wreckage examination at the recovery facility, the #2 MR blade assembly (S/N 3469) was disassembled by removing the blade from the grip and removing the Lamiflex cover. The retention nut was found behind the cover with the fractured threaded end of the spindle still attached to the nut, and the cotter pin installed. Additionally, the Lamiflex bearing and shims were located behind the cover. The Lamiflex bearing (S/N 9383) had a manufacturing date of February 7, 2013.

TEST AND RESEARCH

Materials Laboratory Part Examination

The three sets of spindles, nuts, shims, grips, and Lamiflex bearings from the helicopter's rotor arm assemblies were sent to the NTSB Materials Laboratory in Washington, DC for detailed examination.

#2 Spindle

The threaded end of the #2 spindle had separated in-flight and was submitted still assembled inside the mating #2 retention nut. With exception of a small region on the #2 spindle threaded end fracture surface, most of the fracture surface of the #2 spindle was covered in a black-colored substance consistent with degraded grease. Dirt and debris coated the surface of the remaining inboard portion of the #2 spindle.

The threaded end of the #2 spindle was disassembled from the mating #2 nut, cleaned, and examined in more detail. About 92% of the fracture surface on the separated #2 spindle was flat, and had beach marks consistent with fatigue cracking. (Beach marks are macroscopic progression marks on the fracture surface of a fatigue crack that indicate successive positions of the advancing crack front.) The separation occurred through the root of the end thread (thread closest inboard), and the fatigue crack emanated from the trailing edge (TE) side of the spindle. Corrosion was visible on the fracture surface of the #2 spindle in the fatigue crack initiation area.

The remaining 8% of the fracture surface on the separated #2 spindle was rough and had a shear lip, which was consistent with overload. The shear lip was on the leading-edge side of the spindle, opposite the fatigue crack initiation area on the TE side. This was the same area on the fracture surface that was not covered with black grease. The fracture surface in the area of the shear lip on the #2 spindle fracture surface had features showing microvoid coalescence, which were consistent with overstress. On various portions across the entire fracture surface, shiny areas consistent with mechanical damage were observed.

The average root radius measurement for the #2 spindle was smaller than what was defined in the thread form profile specified by the Enstrom spindle drawing. The remainder of the thread features conformed to the required thread form profile. For additional details of the thread form profile, see the Materials Lab Factual Report in the docket for this investigation.

A cross-section was prepared through the separated #2 spindle threaded end. The hardness of the #2 spindle was within the range specified on the Enstrom spindle drawing. The threads of the #2 spindle were examined in the prepared cross-section. Corners with tight radii were observed in the flat-bottomed thread roots. The threads looked to be cut, rather than rolled, and no decarburization (a process used to reduce the carbon content in metal) or abusive machining was detected. The microstructure of the #2 spindle was tempered martensite and consistent with alloy steel.

#1 and #3 Spindles

The #1 and #3 spindles were completely covered in red/brown grease; the grease was removed and the threaded ends were further cleaned for detailed examination. The average root radius measurements for the #1 and #3 spindles were smaller than what was defined in the thread form profile specified on the Enstrom spindle drawing. The remainder of the thread form features conformed to the required thread form profile. The threads on the #1 spindle were flat-bottomed and had tight radii in the corners, similar to the threads on the #2 spindle. The threads on the #3 spindle were not flat-bottomed, but the radii were smaller than specified.

The threaded ends of the #1 and #3 spindles were examined using magnetic particle inspection (MPI). Multiple MPI indications were observed in the thread roots of both spindles. There was one very bright linear crack indication in the root of the end thread on the trailing edge (TE) side of the #3 spindle, which was the same location from which the fatigue cracking on the #2 thread initiated.

A bright linear crack indication was also observed in the root of one of the threads on the #1 spindle on the TE side. However, this indication was observed in the root between two threads about mid-length down the threaded end and in a thread root adjacent to the cotter pin hole. A portion of the crack indication was visible on the inner diameter of the cotter pin hole. The crack indication extended out of the cotter pin hole towards the top side of the #1 spindle. Additional MPI indications also were observed running parallel along portions of multiple thread roots. The parallel indications were in similar locations to where the spindle #2 had tight radii in the thread corners.

The fracture surfaces of the cracks in the threads of the #1 and #3 spindles were flat with features consistent with fatigue cracking. Dark areas were observed on the fracture surface of the #3 spindle, consistent with corrosion products.

No metallurgical issues were observed with the remaining components of the rotor arm assemblies.

Finite Element (FE) Modeling

As a result of the fatigue cracking and fracturing found on the helicopter's spindles, FE modeling was performed to examine local stresses on the spindle. Modeling revealed that there was a possibility that, in addition to a longitudinal centrifugal force, the loading on the threaded portion of the spindle may include lateral forces and bending moments. Two regions of interest were studied: the threaded portion of the spindle where the #2 spindle separated due to a fatigue crack that propagated and the cotter pin hole region where cracks were found in the #1 spindle. In November 2015, Enstrom instrumented the MR spindles of an exemplar helicopter with strain gauges to determine whether there was existence of bending loads at spindle threads. These tests revealed that a bending moment existed that increased the stresses in the threaded area of the spindle with a bending moment that was not previously accounted for during the spindle design.

Spindle 2-D Model

The measured #2 spindle profile was used to construct the FE model of the accident spindle. The corner radii were chosen to be 0.003 inch for all thread roots. A model of a spindle with specified larger 0.009" thread profile was also constructed for comparison purpose. The 2-D models with these two profiles will be referred to as the "measured" model and the "nominal" model. The geometry of the nut was approximated from design drawings.

The only external load considered for the 2-D model was the axial centrifugal force due to blade rotation. According to Enstrom, during the design of the spindle it was assumed that this was the most significant load acting on the threaded portion of the spindle. The magnitude of the force was chosen to be 21,460 lbs, which, according to design calculations, corresponded to the maximum force allowed at a rotation speed of 385 rpm. This force was applied as a pressure to the nut surface contacting the Lamiflex bearing (which was not included in this model). This surface was constrained to remain horizontal during the simulation, which is an assumption that was intended to account for the stiffness of the Lamiflex bearing. The Lamiflex bearing is stiff, it is not rigid as discussed later in this report. This assumption resulted in a nonuniform pressure distribution on the loading surface.

The longitudinal normal stress was the dominating stress component of the analyses and was the primary quantity of interest. With the measured thread profile, the peak stress occurred in the root region of the first tooth from the bottom, which coincided with the location of the crack that caused the failure of the #2 spindle. With the specified thread profile, stress values were the highest in two regions: the first tooth root and the stress relief feature beneath the threads. The peak stress magnitudes were 149 ksi and 84 ksi for the measured and nominal thread profiles, respectively.

Retention Assembly 3-D Model

During the investigation, it was determined that there was a possibility that in addition to the longitudinal centrifugal force, the loading on the threaded portion of the spindle may include lateral forces and bending moments. A 3-D model of the entire retention assembly was built to compute the loads to be applied to the detailed local 3-D FE models of the threaded portion of the spindle. The global 3-D FE model consisted of the flapping pin, the blade grip, the spindle, the two bearings inside the grip, the Lamiflex bearing, and the nut.

The forces and moments obtained from the global analysis were applied to the local model as external loadings. The loadings were applied in two steps. In the first step, only the axial

NTSB Probable Cause

An in-flight failure of the helicopter's #2 main rotor spindle due to undetected fatigue cracking, which resulted in an in-flight breakup. Contributing to failure were the nonconforming thread root radius of the spindle and the manufacturer's failure to include a bending moment within the spindle threads when performing the fatigue analysis during initial design of the spindle.

© 2009-2020 Lee C. Baker / Crosswind Software, LLC. For informational purposes only.