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N2626N accident description

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Crash location 27.780556°N, 82.431389°W
Nearest city Apollo Beach, FL
27.773084°N, 82.407594°W
1.5 miles away
Tail number N2626N
Accident date 30 Nov 2012
Aircraft type Robinson Helicopter R22 Beta Ii
Additional details: None

NTSB Factual Report

HISTORY OF FLIGHT

On November 30, 2012, about 1512 eastern standard time, a Robinson R22 BETA II, N2626N, operated by Fly N Choppers, was substantially damaged when it impacted water, following a main rotor blade separation in flight near Apollo Beach, Florida. The airline transport pilot was fatally injured. The personal flight was conducted under the provisions of 14 Code of Federal Regulations Part 91. Visual meteorological conditions prevailed and no flight plan was filed for the local flight that departed Peter O Knight Airport (TPF), Tampa, Florida, about 1502.

According to radar data provided by the Federal Aviation Administration (FAA), the helicopter departed its home base at Clearwater Airpark (CLW), Clearwater, Florida, about 1405. It flew over the local area and landed briefly at TPF, before performing another local flight. Witnesses reported that the helicopter was flying along the beach, from north to south, about 500 feet above ground level. The witnesses heard a bang, followed by a main rotor blade separation. The helicopter then immediately rolled right and descended nose down in to a bay, about 200 yards from shore. The last radar target was recorded at 1511:51, indicating an altitude of 200 feet, about 400 yards from shore. Review of the previous five radar targets revealed that the helicopter had climbed from approximately 500 feet, to 800 feet, before descending into the water.

PILOT INFORMATION

The pilot, age 60, held an airline transport pilot certificate with ratings for airplane single-engine land, airplane single-engine sea, airplane multiengine land, airplane multiengine sea, and rotorcraft helicopter. His most recent FAA first-class medical certificate was issued on September 26, 2012. At that time, he reported a total flight experience of 31,500 hours. Review of the pilot's logbook revealed that he had accumulated about 290 hours of helicopter experience; of which, 10 hours were flown during the 90-day period preceding the accident. All 10 hours were flown in the accident helicopter.

AIRCRAFT INFORMATION

The two-seat helicopter, serial number 3644, was manufactured in 2004. It was equipped with a Lycoming O-360, 180-horsepower engine. The helicopter's most recent 100-hour inspection was completed on November 12, 2012. At that time, the helicopter had accumulated 3412.8 hours of operation. The helicopter had flown approximately 55.2 hours from the time of the last inspection, until the accident flight.

A mechanic reported that during the most recent inspection, he had found one main rotor blade exhibiting delamination. He then replaced both main rotor blades with used blades; however, the used blades had 142.4 hours remaining on their 2,200-hour life limit and were inspected before being installed on the accident helicopter.

METEOROLOGICAL INFORMATION

MacDill Air Force Base (MCF), Tampa, Florida, was located about 8 miles northwest of the accident site. The recorded weather at MCF, at 1455, was: wind 070 degrees at 8 knots; visibility 10 miles; few clouds at 8,000 feet; temperature 26 degrees C; dew point 13 degrees C; altimeter 30.17 inches Hg.

WRECKAGE INFORMATION

The helicopter was recovered from the bay 2 days later. The engine and rotor mast remained attached to the airframe. The rotor hub remained attached to the rotor mast and the elastic teeter stops exhibited impact damage. Both spindle assemblies and their respective rotor blades had separated from the hub; one main rotor blade (with spindle assembly) was recovered from the water about 1 month after the accident and the other main rotor blade was not located. The tailboom separated about 6 feet from the transmission and the tailrotor remained with the tailboom. Both tailrotor blades exhibited impact damage. The horizontal stabilizer separated from the tailboom and the vertical stabilizer remained attached to the horizontal. The tailboom exhibited impact damage on the upper left side. The right skid remained attached and the left skid separated. The toe from the left skid was separated and not recovered.

The cockpit was crushed and the windscreen was not recovered. Localized impact damage was observed on the left lower side of the cockpit. Both collectives and the cyclic T-bar remained attached. The antitorque pedals on both sides of the cockpit remained attached. Continuity was established from the tailrotor through the tailrotor drive shaft, to the break in the tailboom, and in to the transmission. Continuity was also confirmed from the main rotor, through the transmission, to the tailrotor drive shaft. The cyclic remained connected via push-pull tubes to the mixer, where push-pull tubes were separated about 1 inch vertically of the mixer consistent with overstress. The push-pull tubes then continued to the swashplate. The antitorque pedals remained connected to push-pull tubes to the lower bellcrank. A push-pull tube had separated about 18 inches vertically of the lower bellcrank, consistent with overstress. Beyond the separation, the upper bellcrank was fractured and there was also a separation of a push-pull tube in the tailboom.

The carburetor heat was in the off position. The mixture control was in the full rich position. The magnetos were selected to both. The fuel selector was not recovered.

The valve covers and top spark plugs were removed from the engine and oil was noted throughout the engine. The spark plug electrodes were intact and light gray in color. The caps were also removed from the magnetos. The crankshaft was rotated by hand via the fan wheel. Camshaft, crankshaft, and valve train continuity was confirmed to the rear accessory section and thumb compression was attained on all cylinders. Both magneto gears rotated when the crankshaft rotated. The carburetor remained attached to the engine and was undamaged.

The rotor hub and the recovered main rotor blade with spindle assembly were forwarded to the NTSB Materials Laboratory, Washington, D.C., for further examination. Metallurgical examination of the components revealed features consistent with overstress and no preexisting cracking or fatigue was noted. Additionally, damage to the teetering stops was consistent with a mast bump (for more information, see Materials Laboratory Factual Reports in the NTSB Public Docket.)

MEDICAL AND PATHOLOGICAL INFORMATION

An Autopsy was performed on the pilot on December 2, 2012, by the State of Florida District 13 Medical Examiner's Office, Tampa, Florida. The cause of death was noted as due to blunt impact to the head and torso. Toxicological testing was performed on the pilot by the FAA Bioaeronautical Science Research Laboratory, Oklahoma City, Oklahoma. Review of the toxicological report revealed:

"Rizatriptan detected in Urine

Zolpidem detected in Liver

Zolpidem detected in Urine"

Review of the pilot's applications for FAA medical certificates revealed that he was first medically certified in 1973 and routinely medically recertified thereafter. The pilot did not report any medications, medical conditions, or physician visits until 2010, when he reported having had hernia surgery.

For many years, the pilot's aviation medical examiner was his personal physician. This physician had prescribed zolpidem (a sleep aid marketed under the trade name Ambien) for many years with the caution "do not fly an aircraft for 24 hours after taking this med." According to pharmacy records, during the last few months before the accident, the pilot had refilled this prescription monthly for 30 tablets each time. In addition, the physician had referred the pilot to a neurologist for evaluation and treatment of migraine headaches and was aware that the pilot had been prescribed rizatriptan (a vasoactive medication used to treat migraines, marketed under the trade name Maxalt) for these headaches. According to pharmacy records, the pilot routinely refilled his prescription for 9 tablets/month. According to the treating neurologist, the migraines were successfully aborted by this medication.

ADDITIONAL INFORMATION

According to the FAA-H-8083-21A, Helicopter Flying Handbook, "…mast bumping is the result of excessive rotor flapping. Each rotor system design has a maximum flapping angle. If flapping exceeds the design value, the static stop will contact the mast. It is the violent contact between the static stop and the mast during flight that causes mast damage or separation."

NTSB Probable Cause

Mast bumping for reasons that could not be determined because one main rotor blade was not recovered.

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