Crash location | 27.649722°N, 80.439166°W |
Nearest city | Vero Beach, FL
27.638643°N, 80.397274°W 2.7 miles away |
Tail number | N262MM |
---|---|
Accident date | 09 Apr 2001 |
Aircraft type | Piper PA-46-500TP |
Additional details: | None |
**This report was modified on September 30, 2009**
HISTORY OF THE FLIGHT
On April 9, 2001, about 1208 eastern daylight time, a Piper PA-46-500TP, N262MM, registered to LK Aero Corporation, collided with trees shortly after takeoff from Vero Beach Municipal Airport, Vero Beach, Florida, while on a Title 14 CFR Part 91 personal flight to Daytona Beach, Florida. Visual meteorological conditions prevailed at the time and no flight plan was filed. The airplane was destroyed and the commercial-rated pilot and private-rated passenger were fatally injured. The flight was originating at the time of the accident.
Transcripts of recorded communications from the FAA, Vero Beach Air Traffic Control Tower, show that at 1200:12, N262MM was cleared by the ground controller to taxi to runway 29 left. At 1204:54, the passenger transmitted to the local controller that the flight was ready for takeoff. The local controller instructed the flight to hold short of the runway. At 1205:40, the local controller instructed the flight to taxi into position and hold on runway 29 left. At 1206:43, N262MM was cleared for takeoff and a north bound departure was approved. At 1208:03, the passenger transmitted "we need to land we have to turn around". The local controller cleared the flight to return to the airport when able. At 1208:20, the passenger transmitted "two mike mike we're going down we're going down", followed by "over the golf (unintelligible)". The local controller responded "copy over the golf course". No further transmissions were received from the flight. (See transcript of communications).
Witnesses stated they observed N262MM taxi to runway 29 left and the pilot perform what appeared to be a normal engine runup. The airplane then taxied onto runway 29 left for takeoff. The wind was from the east, making the takeoff with a tail wind. During the takeoff, the engine seemed to operate at a steady level, but appeared to be low on power. The flight lifted off about halfway down the runway and the landing gear was retracted. The airplane climbed slowly and turned slowly to the left. The airplane then entered a 60-80 degree left bank followed by the airplane rolling level and the wings rocking back and forth. The airplane was now on a southerly heading and the nose dropped. The airplane then collided with trees about 15-20 feet above the ground, fell to the ground, and burst into flames. Witnesses stated they saw no smoke or flames coming from the airplane prior to impact with the trees. At the time of the accident the landing gear was retracted and the engine was running. (See witness statements).
PERSONNEL INFORMATION
The pilot, age 43, held a FAA commercial pilot certificate, with airplane single engine land, private privileges airplane multiengine land, and instrument airplane ratings, last issued on December 4, 1998, when the commercial pilot certificate was issued with a single engine land rating. The pilot held a FAA class 3 medical certificate, last issued on January 6, 2000, with a limitation that the pilot wear corrective lenses while exercising the privileges of the certificate. The pilot's logbook reflected that the pilot received a biennial flight review as required by 14 CFR Part 61, on January 4, 2000. Pilot logbook records show the pilot had accumulated about 1,514 total flight hours, and about 33 flight hours in the Piper PA-46-500TP. The pilot also had 608 flight hours in the Piper PA-46-350P, and 119 flight hours in a Piper PA-46 JetProp conversion. The pilot attended Attitudes International, Inc., Vero Beach, Florida, in January 1998, for Piper PA-46-350P initial pilot training, and in January 1999, for Piper PA-46-350P recurrent training. On March 8, 2001, the pilot received 5 flight hours of training in the Piper PA-46-500TP, from a flight instructor. (See pilot records.)
The passenger, age 44, held a FAA private pilot certificate, with a airplane single engine land rating, last issued on March 25, 1988. The passenger held a FAA class 3 medical , with no restrictions, last issued on January 11, 2001. At the time of the medical examination, the pilot reported he had accumulated 378 total flight hours and that he had flown 60 flight hours in the previous 6 months.
AIRPLANE INFORMATION
The airplane was a 2001 model year Piper PA-46-500TP, registration N262MM, manufactured in February 2001, and certificated on March 5, 2001. The airplane was equipped with a Pratt and Whitney PT6A-42A, 500 shaft horsepower engine. At the time of the accident the airplane had accumulated 45 total flight hours. At the time the pilot took possession of the airplane, it had about 12 total flight hours.
Maintenance records show the airplane was taken by the pilot to Sun Aviation, Inc., Vero Beach, Florida, on April 2, 2001, for installation of weather avoidance and collision avoidance systems. The pilot had also complained about intermittent alternator output problems and about the pilot's microphone and headset being intermittent. During this shop visit, the voltage regulator was changed to correct the alternator problem, but the microphone and headset problem could not be duplicated. The airplane was picked up by the pilot on April 6, 2001, and the airplane total time at this work was 43.7 hours. On April 9, 2001, the day of the accident, the pilot took the airplane to the New Piper Aircraft, Inc., Vero Beach, Florida, for repair of the intermittent pilot's microphone and headset and a high alternator load. The plug for the headset was reconnected securely behind the lower pilot's side panel and the alternator voltage regulator was adjusted. The airplane total time during this work was 44.8 hours. (See witness statements and airplane records.)
WEIGHT AND BALANCE INFORMATION
Calculations show that at the time of the accident the airplane weighed about 4,686 pounds and the center of gravity was located at 139.76 inches aft of the datum. The maximum takeoff weight for the airplane is 4,850 pounds and the center of gravity limits at the maximum takeoff weight is 139.3 inches aft of the datum forward limit and 147.10 inches aft of the datum aft limit. (See weight and balance information).
METEOROLOGICAL INFORMATION
Visual meteorological conditions prevailed at the time of the accident. The Vero Beach Municipal Airport, 1150 surface weather observation was winds from 070 degrees at 5 knots, visibility 12 statute miles, few clouds at 3,000 feet, few clouds at 20,000 feet, temperature 82 degrees F, dew point temperature 67 degrees F, altimeter setting 30.10 inches Hg.
COMMUNICATIONS
At the time of the accident the occupants of N262MM were in radio communications with controllers at the FAA, Vero Beach Municipal Airport, Control Tower. The pilot's sister stated that the voice on the recording was not her brother. A person who knew both the pilot and passenger stated the transmissions from N262MM to the local controller were made by the passenger. (See witness statements).
AIRPORT INFORMATION
The Vero Beach Municipal Airport runway 29 left is 7,296 feet long and 100 feet wide.
WRECKAGE AND IMPACT INFORMATION
The airplane crashed in a wooded area between the 17th tee of the Dodger Pines Golf Course and a residence located at 2761 51st Avenue, Vero Beach, Florida. The main wreckage coordinates were 27 degrees, 38 minutes, 59.0 seconds, north latitude, and 080 degrees, 26 minutes, 21.1 seconds, west longitude.
Examination of the crash site showed the airplane passed over the 17th tee of the golf course while on a southerly heading. The left wing struck a 75-foot-tall tree at about the 25-foot level, causing separation of the outboard left wing area. About 20 feet to the south, the left and right wings collide with trees at the 25-foot level, causing separation of the outboard right wing area and additional portions of the left wing outboard area. The airplane continued to the south about 55 feet, striking several other trees prior to the nose of the airplane striking a large tree at the 18-foot level. The remainder of the right wing separated and was located forward of the main wreckage. The airplane came to rest upright adjacent to the large tree. The propeller separated from the engine during impact with the large tree and the propeller dome and portions of the weather radar system were found up to 120 feet to the south of the airplanes main wreckage. A post crash fire erupted, burning the airplane wreckage and an estimated 100-feet by 100-feet portion of the wooded area around the crash site.
Examination of the airplane wreckage showed that all components of the airplane, which are necessary for flight, were located on or around the main wreckage of the airplane. Examination of the flight control system showed that all separation points within the flight control system was consistent with overstress separation due to impact forces and damage from the postcrash fire. The elevator trim system and rudder trim system were found in the neutral position. The airplane was equipped with a ground adjustable tab on the right aileron for the aileron trim. The landing gear and wing flaps were found in the retracted position. The main cabin door was destroyed by the post crash fire. The locking pins for the door were found in the locked position. The autopilot pitch, roll, yaw, and pitch trim servos were found in the disengaged position and the cables from the actuators were attached to the respective cables to the flight control and trim tab surfaces.
Examination of the engine controls in the airplanes cockpit and at the engine showed they had received impact and fire damage. The condition lever was found in the run position. The power lever was found in the midrange position. The manual over ride lever was found in the midrange position. (See The New Piper Aircraft, Inc. Report).
Examination of the engine was performed under NTSB supervision at Pratt and Whitney Canada, Montreal, Canada. The engine sustained severe fire and impact damage , including complete fire consumption of the accessory gearbox. Strong circumferential rubbing and machining were displayed by the compressor impeller, the impeller shroud, the compressor turbine vane ring, the compressor turbine, the first stage power turbine vane ring, the first stage power turbine, the second stage power turbine vane ring, and the second stage power turbine due to their making axial contact with their adjacent components under impact loads and external housing deformation. The compressor first, second, and third stage shrouds, the compressor turbine shroud, the first stage power turbine shroud, and second stage power turbine shroud displayed strong circumferential rubbing and scoring due to their making radial contact with their adjacent blade tips. There were no indications of any operational dysfunction to any of the engine components, controls, or accessories examined. The engine displayed contact signatures to its internal components characteristic of the engine developing significant power at the time of impact. The engine displayed no indications of any preimpact anomalies or distress that would have precluded normal engine operation prior to impact. (See Pratt and Whitney Report).
Examination of the propeller was performed under NTSB supervision at Hartzell Propeller, Inc., Piqua, Ohio. The propeller separated from the engine during tree impact when a portion of the engine propeller flange separated from the engine and remained bolted to the propeller with two bolts and the remaining propeller mounting bolts either broke, pulled out the inserts in the propeller hub, or stripped the threads of the inserts. The propeller spinner was crushed and had an impact mark from the counter weight of the number three blade consistent with the blade being in the normal operating range at impact. The cylinder and piston had separated from the propeller hub. Each of the propeller blades had bending damage and no significant leading edge damage or rotational scoring. The examination concluded that the propeller was rotating and not in the feathered position at the time of impact. The amount of engine power applied at the time of impact could not be determined. There were no propeller discrepancies noted that could have precluded normal operation of the propeller. All damage was consistent with impact damage. (See Hartzell Propeller, Inc. Report).
NTSB was informed that the Meggitt Avionics, Inc., data acquisition unit, on board the airplane, contained stored information about any limits in engine operation that are exceeded. The unit received impact and fire damage. The unit was taken by NTSB to Meggitt Avionics, Inc., for possible extraction of any stored data. The circuit boards were fire damaged and the memory chip containing the stored data was fire damaged. Meggitt Avionics, Inc. was unable to retrieve data from the chip. The circuit board containing the memory chip was then taken by FAA to Atmel, Inc., the memory chip manufacturer. Atmel, Inc. was unable to retrieve data from the damaged memory chip. (See Atmel, Inc. Report).
MEDICAL AND PATHOLOGICAL INFORMATION
Postmortem examination of the pilot and pilot-rated passenger was performed by Charles A. Diggs, M.D., Associate Medical Examiner, Fort Pierce, Florida. The cause of death for each was attributed to blunt trauma of the head. No findings which could be considered causal to the accident were reported.
Postmortem toxicology tests were performed on specimens obtained from the pilot by the FAA Toxicology Laboratory, Oklahoma City, Oklahoma, and by Wuesthoff Reference Laboratory, Melbourne, Florida. The tests were positive for 2.4 percent carbon monoxide and negative for cyanide, ethanol, and drugs.
Postmortem toxicology tests were performed on specimens obtained from the pilot-rated passenger by the FAA Toxicology Laboratory, Oklahoma City, Oklahoma, and by Wuesthoff Reference Laboratory, Melbourne, Florida. The tests were positive for 6.2 percent carbon monoxide and negative for cyanide, ethanol, and drugs. (See toxicology reports.)
TESTS AND RESEARCH
Analysis of background noises recorded by the FAA, Vero Beach Municipal Airport, Control Tower, during transmissions from N262MM, and from transmissions recorded from a test Piper PA-46-500TP at known power settings, was performed by the NTSB Vehicle Recorders Division, Washington, D.C. The analysis showed that noise signatures from the propeller of N262MM and from the test airplane were present on the recordings. At the time the passenger on N262MM transmitted to controllers that they were ready for takeoff and when he acknowledged the takeoff clearance, the propeller was rotating at 1,261 rpm and 1,255 rpm respectively. When the passenger transmitted to controllers after takeoff, that they needed to land, the propeller was rotating at 1,980 rpm. When the passenger transmitted we have to turn around, shortly after the above transmission, the propeller was rotating at 2,017 rpm. When the passenger made his last transmission stating they were going down, the propeller rpm was 1,965. The propeller speed at takeoff is 2,000 rpm. (See NTSB Specialists Factual Report, Air Traffic Control Recording).
Metallurgical examination of components from the engine and debris found in the compressor of the engine was performed by the NTSB Materials Laboratory, Washington, D.C. All fractures were consistent with overload separation. The debris found in the compressor of the engine was made of aluminum and magnesium with traces of carbon, oxygen, and zinc, materials found in the melted accessory gearbox.
After the investigation was concluded, additional evidence was found indicating electrical arcing and progressive fatigue cracking in the engine’s P3 line. The P3 line is a component of the compressor air lines group and functions as a pneumatic control line that regulates fuel flow to the engine; a hole in the P3 line could result in a rapid rollback of engine power. Based on this information, a series of tests were conducted in a Meridian simulator to determine how quickly a power rollback would occur and to compare this data with sound spectrum evidence. The simulator was configured with the engine at full takeoff power (2,000 propeller rpm) and a P3 line failur
The pilot's excessive bank angle and his failure to maintain airspeed while returning to the airport after takeoff due to an unspecified problem resulting in the airplane stalling and colliding with trees during the resultant uncontrolled descent.