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N749AA accident description

Florida map... Florida list
Crash location 26.744722°N, 81.935000°W
Nearest city North Fort Myers, FL
26.667293°N, 81.880086°W
6.3 miles away
Tail number N749AA
Accident date 26 Jun 2003
Aircraft type Cessna 414
Additional details: None

NTSB Factual Report

HISTORY OF FLIGHT

On June 26, 2003, about 1251 eastern daylight time, a Cessna 414, N749AA, registered to Osprey Air Services, Inc., experienced an in-flight loss of control and collided with trees then the ground near North Fort Myers, Florida. Visual meteorological conditions prevailed at the time and no flight plan was filed for the 14 CFR Part 91 personal flight from Palm Beach County Park Airport (KLNA), West Palm Beach, Florida, to Pine Shadows Airpark, Fort Myers, Florida. The airplane was substantially damaged and the commercial-rated pilot sustained serious injuries. A pilot-rated passenger seated in the copilot's seat and another passenger in the cabin were fatally injured. The remaining passenger sustained minor injuries. The flight originated about 1213, from Palm Beach County Park Airport.

According to an NTSB prepared transcription of communications from an uncertified copy of the voice tape from Fort Myers Air Traffic Control Tower, at an undetermined time, the pilot contacted the facility and was advised by the controller to remain clear of "Class Charlie Airspace." A position relief briefing was conducted and the controller established contact with the pilot who advised that the flight was over Lake Okeechobee inbound to " Pine Shadows Airpark", and requesting VFR flight following. The controller provided a discrete transponder code and altimeter setting. The pilot repeated the altimeter setting and advised the controller that he would report when the destination airport was in sight. The flight was radar identified, and the flight continued. At an undetermined time the pilot advised the controller that the destination airport was in sight; the controller advised the pilot that radar service was terminated and frequency change was approved. The pilot acknowledged that transmission. There were no further recorded transmissions from the pilot.

The pilot later stated in writing that he performed a "thorough" preflight inspection of the airplane using a checklist. He "examined the fuel and calculated that we would have at least 45 minutes of reserve fuel after we landed", and he checked both main fuel tanks. He reported twice checking the fuel level in both main fuel tanks and reported the level in both tanks was 2-3 inches from the top. He estimated the flight duration to be less than 1 hour, and he planned on fueling the airplane at the destination airport, so he did not fill the auxiliary or engine nacelle tanks. The passengers were boarded, and both engines were started; the right engine took a little more time to start than the left. He "checked that all the pressures and temperatures were within proper limits and the magnetos on each engine were operating properly."

The pilot stated that the flight departed to the east from KLNA, and after takeoff initially climbed to 2,500 feet mean sea level (msl), then climbed to between 4,500 and 6,500 feet msl. During cruise flight he leaned the fuel/air ratio for each engine and completed the cruise checklist items. The flight continued and he began to descend when the destination airport was in sight, which was when the flight was 12 miles away. When the flight was 3 miles from the destination airport he performed the pre landing checks and noticed, "the fuel gauges indicated 15 gallons/90 lbs. of fuel remaining in the left main tank and 18 gallons/108 lbs. in the right main fuel tank." Less than 2 minutes later he entered left downwind for landing to the east at the destination airport and went through the "pre landing GUMPS checks." He lowered the landing gear, turned on the fuel pumps for both engines, enrichened the fuel/air ratio, verified that the gear was down and locked, and that everyone had their seatbelts on. While flying at an airspeed 25 knots above the manufacturers recommended final approach speed and when abeam the touchdown point, he reduced power and lowered the flaps 10 degrees. He turned onto base leg, and while rolling out of the turn he stated, "the right engine suddenly came to a stop, and I banked to the left maintaining a zero sideslip configuration and directional control." He pushed the mixture, propeller, and throttle controls forward in that order, and identified that the right engine had failed. He pulled the right propeller control to the feather position, and while doing so the airplane, "began to yaw right and simultaneously bank right. I reached for the throttle on the left engine and pulled it [to] idle, attempted to maintain control of the aircraft and accomplish an emergency landing in the safest area I could find." He also stated that the right engine quit while flying at 600 feet and less than 6 seconds later, "we were on the ground."

A witnesses located approximately 3/4 nautical mile northeast of the crash site reported seeing the airplane banking to the left, which increased to an inverted position as well as being in a nose low attitude, nearly vertical. The airplane was then observed to roll to the right while remaining in the nose low attitude. The witness then lost sight of the airplane due to obstructions. Another witness located approximately .15 nautical mile southeast of the accident site reported seeing the airplane flying westbound with decreasing engine sound; no smoke or fire was observed trailing the airplane. The airplane was observed to spin to the right 4 times in a tight turn; the witness then lost sight due to obstructions.

The passenger who sustained minor injuries reported to sheriff's office personnel that prior to the accident, the landing gear was extended and he heard a buzzing sound immediately before the airplane entered a spin. He was not sure how many times the airplane spun.

PERSONNEL INFORMATION

The pilot (left seat occupant) is the holder of a commercial pilot certificate with ratings airplane single engine land, airplane multi-engine land, and instrument airplane. He was also the holder of a certified flight instructor certificate with airplane single engine, and instrument airplane ratings. The instrument rating was added on May 30, 2003, which was the date of his last flight review or equivalent required by 14 CFR Part 61.56. He was issued a first class medical certificate on December 6, 2002, with no limitations.

A review of the pilot prepared NTSB "Pilot/Operator Aircraft Accident Report" form revealed he listed a total time of 972 hours, with 0 hours in make and model and 38 hours total multi-engine time. In the last 90 days he listed a total time of 266 hours, with 3 hours in multi-engine airplanes and the remainder in single engine airplanes. During the last 30 days, he listed a total time of 90 hours, and during the last 24 hours he listed a total time of 6 hours, with 3 of the 6 hours in multi-engine airplanes.

A review of the pilots' pilot logbook revealed he was signed off by a certified flight instructor to operate a pressurized airplane capable of operating at high altitudes in accordance with 14 CFR Part 61.31(g), on May 31, 2003. The flight was conducted in a Beech 200 airplane; the flight duration was recorded to be 1.3 hours.

According to FAA records, the right seat occupant was the holder of a private pilot certificate with airplane single engine land rating. He was issued a third class medical certificate on March 13, 2003, with the limitation that he wear corrective lenses and possess glasses for near/intermediate vision. He listed a total time of 400 hours on the application for the last medical certificate.

AIRCRAFT INFORMATION

The airplane was manufactured by Cessna Aircraft Company in 1970, as model 414, and designated serial number 414-0049. It was type certificated in the normal category in accordance with Civil Aeronautics Regulation (CAR) 3, and equipped with two Teledyne Continental Motors TSIO-520-J engines rated at 310 horsepower. The airplane was also equipped with two McCauley, constant speed, manual feathering, 3AF32C93-R/82NC-5.5 propellers.

Review of the airplane maintenance records revealed the airplane was last inspected in accordance with a 100-Hour/Annual inspection that was signed off as being completed on February 11, 2003. The airplane total time at that time was recorded to be 1,710.1 hours.

METEOROLOGICAL INFORMATION

A METAR weather observation taken at 1253, or approximately 2 minutes after the accident at the Page Field Airport, Fort Myers, Florida, indicates clear skies existed, and the wind was 070 degrees at 7 knots, variable from 030 to 110 degrees. The visibility was 10 statute miles, the temperature and dew point were 30 and 22 degrees Celsius, respectively, and the altimeter setting was 30.05 inHg.

COMMUNICATIONS

The pilot was last in contact with Fort Myers Approach Control. There were no reported communication difficulties.

WRECKAGE AND IMPACT INFORMATION

Examination of the accident site revealed the airplane came to rest behind a mobile home located in a residential area; no postcrash fire was noted. The crash site was located at 26 degrees 44.689 minutes North latitude and 081 degrees 56.092 minutes West longitude, or approximately 294 degrees and 2.14 nautical miles from the destination airport. The airplane was resting against a tree. Several pine trees were in close proximity to the wreckage. Examination of several of the trees revealed evidence of multiple contacts approximately 46 feet above ground level. Two slashes associated with the right propeller were noted in one of the tree trunks. The nose section of the airplane forward of the front pressure bulkhead had a section of tree embedded in it. A section of tree trunk was embedded into the co-pilots seat area. Upon NTSB arrival, six seats and the seatback of the pilot's seat were located outside of the airplane. The seats were retained for further examination.

Examination of the wreckage revealed the airplane was upright on a magnetic heading of 218 degrees. All components necessary to sustain flight remained attached to the airplane or were in close proximity to the main wreckage. The empennage was separated at the aft pressure bulkhead but remained connected by flight control cables. Both wings remained secured to the fuselage, but approximately 6 feet of the right wing was separated by impact forces. The separated section of the right wing was found in close proximity to the main wreckage. The vertical stabilizer remained attached to the empennage and the rudder remained attached to the vertical stabilizer. The left horizontal stabilizer remained secured to the empennage and the left elevator remained secured to the left horizontal stabilizer. The right horizontal stabilizer remained secured to the empennage and a 3 foot 6 inch length of right elevator remained attached to the right horizontal stabilizer. The separated section of the right elevator was found in close proximity to the main wreckage.

No browning of grass due to fuel leakage was noted beneath either wing. The left main and left auxiliary fuel tanks were breached. The left main fuel tank bulkhead baffle exhibited a slight forward bulge. The right main fuel tank was separated. No fuel was found in either the breached left main fuel tank or in the separated right main fuel tank. Approximately 4.0 gallons and 1.5 gallons of 100 low-lead (100 LL) fuel were drained from the left auxiliary and right auxiliary fuel tanks, respectively. The left locker tank was drained and found to contain approximately 2 ounces of water admixed with fuel, no fuel was found in the right locker tank. No fuel staining was noted on the wings aft of any of the six fuel tank filler openings. Both engines remained attached, and the left propeller remained attached to the engine. The right propeller was separated from the engine but found in close proximity to the engine.

Further examination of the wreckage revealed rudder, elevator, and left aileron flight control continuity was confirmed. The right aileron control cable was fractured in the co-pilots seat area. No evidence of preimpact damage was noted to the fractured right aileron control cable. The flaps were extended approximately 10 degrees, and the aileron trim tab actuator was positioned greater than maximum limits. The rudder trim tab actuator was positioned to approximately 7 degrees trailing edge tab left, while the elevator trim tab actuator was positioned approximately 6 degrees trailing edge down. The landing gear was extended based on examination of the landing gear actuator.

Examination of the cockpit revealed both control yokes were in position. The readings from the dual tachometer were left (2,500 rpm) and right (800 rpm). Both fuel flow readings, both oil temperature readings, both exhaust gas temperature readings, the left cylinder head temperature reading, the right fuel quantity, and right oil pressure readings were off scale low. The right cylinder head temperature reading was 200 degrees Fahrenheit. The left fuel quantity indicated 70 pounds. The left oil pressure reading was at the lower red line. The throttle quadrant was displaced to the left. The left and right throttle controls were full forward and midrange, respectively. The left and right propeller controls were also full forward and midrange, respectively. The left and right mixture controls were found 1/2 inch and 1.5 inches aft of full forward, respectively. The throttle friction was loose. The aileron and rudder trim indicators were found positioned near full right and neutral, respectively. The alternate engine air controls were each found in the off position. The left fuel selector was found positioned to the right main position, while the right fuel selector position was not determined. Impact damage to the left fuel transfer switch precluded determination of position, while the right fuel transfer switch was in the off position. The master switch, and left and right alternator switches were found in the off position. The left and right magneto switches of both engines were each in the on position, while both auxiliary fuel pump switches were in the low position. Fuel quantity indicating system components were retained for further examination.

Further examination of the cockpit revealed the pilots seat base remained in the airplane. The floor adjacent to the pilots seat was crushed up. The pilot's shoulder harness remained secured to the lapbelt which was not buckled. The co-pilots seat was detached, and the seat pedestal was destroyed. The copilot's shoulder harness was cut. The forward portion of the cabin roof was crushed down most prominently in the copilots seat area. Blood was noted on the interior fabric in the cabin between the two seats in the second row. The annunciator panel, left and right auxiliary tank indicator light bulbs, and the Shadin Digiflo instrument were retained for further examination.

Examination of the fuel system components of the airplane revealed the left and right fuel selector valves located near each engine were each in the "off" position. Approximately 2 ounces of 100LL fuel were drained from the left fuel strainer; the screen was clean. The right fuel strainer screen exhibited very slight contamination; no fuel was noted at the strainer inlet fitting. Residual fuel was noted in the in-line fuel pump outlet for the left auxiliary fuel tank. No fuel was noted at the outlet of the in-line fuel pump outlet for the right auxiliary fuel tank, while residual fuel was noted at the inlet of the in-line fuel pump for the right auxiliary fuel tank. No fuel was noted at the inlet or outlet of the left auxiliary fuel pump. A drop of fuel was noted at the inlet and outlet fittings of the right auxiliary fuel pump. Residual fuel was noted in the crossfeed line at the left wing root, while no fuel was noted in the crossfeed line at the right wing root.

The left engine was examined following recovery of the airplane to determine fuel remaining in the flexible fuel lines in the engine compartment. Examination of the flexible fuel lines revealed approximately 1/2 ounce of fuel was drained from the fuel line from the mechanical fuel pump to the fuel metering unit. Only 2 drops of fuel were found in the fuel line from the fuel metering unit to th

NTSB Probable Cause

The failure of the pilot to maintain airspeed (Vs) following a total loss of engine power from the right engine due to fuel starvation, resulting in an inadvertent stall, uncontrolled descent, and in-flight collision with trees and terrain. Factors in the accident was the failure pilot to feather the right propeller following the total loss of engine power, and his lack of total experience in the accident make/model of aircraft.

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