Crash location | 29.173889°N, 82.224167°W |
Nearest city | Ocala, FL
29.187199°N, 82.140092°W 5.2 miles away |
Tail number | N96398 |
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Accident date | 09 Apr 2016 |
Aircraft type | Mooney M20K |
Additional details: | None |
HISTORY OF FLIGHT
On April 9, 2016, about 0850 eastern daylight time, a Mooney M20K, N96398, was substantially damaged during a forced landing following a total loss of engine power after takeoff from Ocala International Airport (OCF), Ocala, Florida. The commercial pilot was fatally injured, and the passenger was seriously injured. The personal flight was conducted under the provisions of 14 Code of Federal Regulations Part 91. Visual meteorological conditions prevailed, and no flight plan was filed for the flight, which had an intended destination of Lakeland Regional Airport, Lakeland, Florida.
Information from the OCF air traffic control tower revealed that the airplane was cleared for takeoff and began its takeoff roll from runway 36 with about 7,000 ft of runway available. About 1 minute after the airplane was cleared for takeoff, the pilot announced, "I'm losing my engine… I'm going down on [runway] 26." Runway 26 was located at the end of and perpendicular to the takeoff runway.
The OCF ground controller (GC) was receiving a clearance by telephone when he overheard the pilot's radio call. He estimated that the airplane was north of the tower about 200 to 300 ft above the runway before it turned west. According to the GC, "The wings rocked a little in the turn, but when he lined up with the runway [26] he looked clean. He still looked high, like he might touchdown past midfield and go off the departure end. He looked stable, but then he turned left. The more he turned the steeper the turn got, and then when the wingtip hit the ground the airplane was 90 degrees."
The passenger was interviewed the day after the accident. She stated that she was not a pilot but had flown in the airplane several times. After landing at OCF the day before the accident, the pilot requested a fuel service of 10 gallons per wing, and they then spent the night with family. On the morning of the accident, they boarded the airplane for a flight to the Sun-n-Fun fly-in event. According to the passenger, engine start, taxi, run-up, acceleration, takeoff, and initial climb from runway 36 were "normal."
The passenger said she heard a sudden noise "like a click," and the engine stopped producing power. The pilot announced the loss of power and his plan for the forced landing over the radio. The airplane was north of both runways, and the left turn westbound was "steady" until the airplane was about over runway 26. The wings began "rocking," and the turn continued to the left until the bank angle was 90° and the left wing struck the ground.
An airport employee said that his attention was drawn to the airplane by a "sputter-cough" sound. Demonstrating what he observed with a model of an airplane, he described a straight-ahead descent, followed by a left turn over runway 26, two "dips" that resembled a porpoising motion, and then a sharp, 90° left turn to ground contact.
PERSONNEL INFORMATION
The pilot held a commercial pilot certificate with ratings for airplane single-engine land, rotorcraft-helicopter, and instrument airplane. His most recent Federal Aviation Administration (FAA) third-class medical certificate was issued on February 7, 2014. He reported 1,670 total hours of flight experience on that date.
AIRCRAFT INFORMATION
According to FAA records, the airplane was manufactured in 1981. The maintenance records were not recovered, but a copy of the airplane's most recent annual inspection showed that it was performed on June 10, 2015, at 2,435.2 total aircraft hours.
METEOROLOGICAL INFORMATION
Weather reported at the time of the accident included wind from 010° at 9 knots, 10 statute miles visibility, clear skies, temperature 14°C, dew point 3°C, and an altimeter setting of 30.15 inches of mercury.
WRECKAGE AND IMPACT INFORMATION
The airplane came to rest on the flat, grass surface of the airport infield, and all major components were accounted for at the scene. The wreckage path was oriented 212° and was about 300 ft long. The airplane came to rest upright. The engine and its mount were separated from the airframe but remained attached by cables and wires. The propeller was separated and located 45 ft down the wreckage path from the first ground scar.
The firewall, instrument panel, and center console were crushed aft in compression and canted about 45° to the airplane's left. The windshield was destroyed, and the cabin roof was torn spanwise from the door opening to about mid-cabin. The inboard sections of both wings were intact and remained attached to the fuselage. The left wing outboard of the flap was separated by impact. The leading edge of the right wing was crushed aft in compression. Both wing fuel tanks contained fuel.
Control continuity could not be immediately established due to impact damage and the airplane's resting position. As the wreckage was sectioned for recovery, control continuity was established from the cockpit through impact breaks and saw cuts to the flight control surfaces.
The fuel selector handle was found between the "Left Tank" and the "Off" placard positions. Crushed airplane structure surrounded the selector handle and preserved its position at the time of impact.
The engine was rotated by hand through the vacuum pump drive pad. Continuity was established from the accessory section to the valvetrain and powertrain. Compression was confirmed using the thumb method. The turbocharger impeller moved freely when rotated.
MEDICAL AND PATHOLOGICAL INFORMATION
The Medical Examiner for District 5, Leesburg, Florida, performed the autopsy on the pilot and determined the cause of death was blunt chest trauma. The FAA Bioaeronautical Research Sciences Laboratory, Oklahoma City, Oklahoma, performed toxicology testing on specimens from the pilot; the testing was negative for alcohol and drugs.
TESTS AND RESEARCH
Engine-Monitoring Instrument Data Download
The airplane was equipped with an Electronics International CGR-30P, panel-mounted instrument that monitored and recorded up to 66 parameters related to engine operations. The device was downloaded in the NTSB Recorders Laboratory.
The data began at 0741:04, at a point consistent with the engine at idle at device power-up, and the parameters continued through what was consistent with taxi, run-up, and eventually takeoff power application at 0751:04. At 0751:28, there was a rapid decrease in fuel flow, and, at 0751:42, there was a decrease in engine rpm and manifold pressure. Subsequently, manifold pressure and rpm stabilized around 14 inches and 1,300, respectively, and remained at these values until the end of the recording.
Engine Examination/Test Run
The engine was examined and test run in Mobile, Alabama, between May 31 and June 2, 2016. During examination and preparation, the crankshaft was sleeved, and the fractured propeller flange was welded back onto the crankshaft. The aft left oil cooler mount/mount leg and the magneto ignition harnesses were replaced due to impact damage. The magnetos remained secured in their mounts, and timing was confirmed at 20° before top dead center.
The engine starter, Nos. 3 and 5 cylinder intake tubes, and the entire exhaust system were replaced due to impact damage and for compatibility with the engine test cell equipment. The engine's turbocharger and waste gate were intact and installed for the engine test run without modification.
The engine started immediately, accelerated smoothly, and ran continuously without interruption. The engine was run through the manufacturer's entire test run protocol with no anomalies noted. After completion of the test protocols, the engine was accelerated and decelerated rapidly several times between idle and full power. During the accelerations and decelerations, the engine ran smoothly and without interruption.
Fuel Selector Valve Tests
The 3-position fuel selector valve had detents corresponding to "Right Tank," "Left Tank," and "Off." When viewed relative to a clock face, the detents for "Right Tank," "Left Tank," and "Off" were positioned at 2 o'clock, 10 o'clock, and 8 o'clock, respectively.
As previously mentioned, the fuel selector valve handle was found in an intermediate position between the "Off" and "Left Tank" placard positions. Computerized axial tomography scan imagery revealed that the valve handle was positioned between the "Left Tank" and "Right Tank" detent positions and that all three valve ports were open to each other. The difference between the handle's position according to the placard and its actual position was consistent with the valve placard having been displaced relative to the handle.
The valve was placed on a flow bench in its as-found condition. When fuel was drawn through the selector valve at the engine port, fuel was drawn from both the left and the right tank ports simultaneously.
An exemplar Continental TSIO-360GB engine was placed in a test cell, and the engine fuel system was set up and adjusted to factory specifications of unmetered fuel pressure of 45 to 49.5 pounds per square inch (psi). The engine was then stopped, and the test stand fuel system was disconnected.
Fuel was then provided to the engine from an external fuel tank and a fuel system mockup (left tank, right tank, left and right vapor return, engine supply and return lines) through the accident fuel selector valve. The accident fuel selector valve was tested in the as-found position between the left tank and the right tank detent positions.
The engine was primed using the test cell's fuel system, but it was started and run on an external fuel tank that was positioned about wing level. The engine started immediately and ran continuously without interruption to full power of 2,700 rpm and 40 inches of manifold pressure. During the full-power portion of the run, which was between 8 and 10 minutes, the unmetered fuel pressure maintained 49 psi. Engine power was reduced to idle and the engine continued to run normally.
ADDITIONAL INFORMATION
Step two in the Before Takeoff checklist found in the manufacturer's Pilot's Operating Handbook was: "Fuel Selector … FULLEST TANK."
The pilot's failure to maintain sufficient airspeed following a loss of engine power, which resulted in the airplane exceeding its critical angle of attack and an aerodynamic stall. Contributing to the accident was the pilot's inadvertent placement of the fuel selector in the "Off" position before takeoff, which resulted in fuel starvation and a total loss of engine power.