Crash location | 33.351111°N, 84.563889°W |
Nearest city | Peachtree City, GA
33.396783°N, 84.595763°W 3.7 miles away |
Tail number | N559LJ |
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Accident date | 01 Jan 2003 |
Aircraft type | Lonnie Johnson RV6A |
Additional details: | None |
HISTORY OF FLIGHT
On January 1, 2003, about 1655 eastern standard time, a homebuilt RV6A, N559LJ, registered to a private individual, crashed approximately 715 feet south-southeast of the approach end of runway 31 at the Peachtree City Airport-Falcon Field, Peachtree City, Georgia. Visual meteorological conditions prevailed at the time and no flight plan was filed for the 14 CFR Part 91 personal flight from the Waycross-Ware County Airport, Waycross, Georgia, to the Peachtree City Airport-Falcon Field, Peachtree City, Georgia. The airplane was substantially damaged and the private-rated pilot, the sole occupant, sustained minor injuries. The flight originated about 1540 from the Waycross-Ware County Airport.
The pilot stated the fuel tanks were filled before departure; no fuel contamination was noted during the preflight. The flight departed and approximately 45 minutes into the flight, he repositioned the fuel selector to the right tank. The flight continued and approximately 15 minutes later, he noticed a slight rpm drop. He applied throttle input to compensate for the rpm decrease and switched to the UNICOM frequency. He elected to perform a practice localizer approach to runway 31 and after crossing the localizer, he turned on the auxiliary fuel pump, applied carburetor heat, then reduced power. At that time, the engine quit completely like a normal shutdown using the mixture control. He repositioned the fuel selector to the left tank which was unsuccessful in restoring engine power. He also turned off the auxiliary fuel pump, and turned it back on after engine power was not restored. Additionally, he removed and reapplied carburetor heat which was also unsuccessful in restoring engine power. Thereafter the propeller stopped and he established best glide airspeed of 75-80 miles-per-hour. After clearing a railroad embankment he turned left to avoid approach lights, and recognizing that he was unable to land on the runway, he lowered full flaps, and slowed to just above stall speed. The wheel pants of both main landing gears made contact with an elevated concrete sewer access, followed by ground contact approximately 20 feet later. The airplane came to rest inverted; the pilot evacuated the airplane by cutting a portion of the canopy with a survival tool.
A witness reported hearing the engine running rough and observed black smoke trailing the airplane. The same witness reported that the engine stopped, ran for 5 seconds, then quit again. A second witness also heard the engine running rough, it then ran fine for a while, before it finally quit.
AIRCRAFT INFORMATION
The airplane was equipped with a Lycoming O-320-E2D engine, and a fixed pitch propeller. The airplane was not equipped with a primer, nor was it equipped with a carburetor temperature probe and/or gauge. The installed carburetor heat system consists of an approximate 5-inches long by two-inches diameter pipe listed in the Van's 2003 Accessory Catalog as "Carb Heat Muff" P/N "EA Carb Heat Muff", which is secured to the exhaust crossover pipe, a "Carb Heat Connector" P/N "Vent DL-07" which is attached forward of the air filter on the filtered air box, and a scat hose that connects the two. A control in the cockpit activates an alternate air door located on the filtered air box forward of the Carb Heat Muff inlet. With carburetor heat applied, air flows through the Carb Heat Muff into the filtered air box, through the air filter, then into the venturi of the carburetor.
METEOROLOGICAL INFORMATION
The temperature and dew point at 2,420 feet mean sea level for the Peachtree City Airport-Falcon Field area taken approximately 2 hours after the accident were each recorded to be 7 degrees Celsius, which equates to 44.6 degrees Fahrenheit.
Review of an icing probability chart revealed that at the above listed temperature and dew point, the conditions were favorable for serious icing at any power setting.
WRECKAGE AND IMPACT INFORMATION
Examination of the airplane by the FAA inspector revealed damage to the vertical and left horizontal stabilizer, rudder, nose gear, and bottom portion of the firewall. The fuel tank vent lines were checked and found to be clear of obstructions. Fuel was found in both wings; fuel was leaking from the right wing. Fuel samples taken from the right wing and the gascolator showed no contaminants. The fuel boost pump operated postaccident. The spark plugs and inside ends of both exhaust pipes were found sooted. The carburetor heat system was found operable post accident. The engine was started and operated only to idle power setting; vibration prevented operation at a higher power setting. The carburetor was removed for further examination.
TESTS AND RESEARCH
Bench testing of the carburetor at the manufacturer's facility with FAA oversight revealed the fuel flow rate at idle was .6 pounds-per-hour (pph) less than the specified amount, and at the four remaining test points, was flowing greater than the rich limit at all points. At the last test point which equates to full throttle, the carburetor was flowing 18.5 pph above the rich service limit. Disassembly of the carburetor revealed a curved sliver of material adhering to the exterior surface of the fuel inlet screen. Additionally, the main metering nozzle was flow tested and found to be approximately 7 percent above the rich limit.
The pilot reported verbally that approximately 50 flight hours earlier, when he was taxiing to takeoff, the engine quit just like it did during the accident flight. The carburetor and engine driven fuel pump were replaced. The engine quit again in a similar fashion, and the auxiliary fuel pump and all fuel lines were replaced. Additionally, the fuel selector valve was disassembled and rebuilt.
Review of the engine logbook revealed that on September 8, 2002, an overhauled carburetor and a new engine driven fuel pump were installed. The engine had accumulated 54.5 hours since then at the time of the accident.
According to the General Manager of Van's Aircraft, Inc., "I checked with our engineering staff and we have never done any heat rise testing through any of the various [carburetor] heat systems that can be installed on an RV." He additionally stated "We currently offer an 8" sealed heat exchanger that can be used to supply heated intake air to the [carburetor]. We also offer a shorter [carburetor] heat exchanger that mounts on the crossover pipe directly above the alternate air door...It is about 5" in length."
Review of Section 11 of the builders manual titled, "Engine and Propeller Selection and Installation" revealed a subsection titled, "[Carburetor] and Cabin Heat Muffs." Review of that subsection revealed that each builder will have to evaluate his/her own installation based on the likelihood of carburetor ice in his/her intended operating environment.
Flight testing was performed with a RV6A airplane equipped with the same type of carburetor heat system as the accident airplane (approximate 5-inches long by 2-inches diameter pipe attached to the exhaust crossover pipe), same model carburetor as the accident airplane but with an installed temperature probe, and same model engine with slightly higher horsepower as the accident airplane. The testing revealed that at the flight test altitude of 5,500 feet with the engine operating at an estimated 75 percent power and carburetor heat applied, the temperature rose 1/2 degree Fahrenheit above the temperature with carburetor heat off.
ADDITIONAL INFORMATION
The airplane minus the retained carburetor was released to the airplane owner on November 13, 2003. The retained carburetor was released to the airplane owner on February 23, 2004.
The failure of the pilot to activate carburetor heat control during cruise flight after experiencing a loss of engine rpm, inadequate carburetor heat system by the builder, and the unsuitable terrain encountered by the pilot-in-command during the forced landing following the total loss of engine power. A factor in the accident was the weather conditions ( temperature and dew point) which were susceptible to carburetor icing during cruise flight and descent.