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N152BK accident description

Idaho map... Idaho list
Crash location Unknown
Nearest city Lewiston, ID
46.416551°N, 117.017657°W
Tail number N152BK
Accident date 11 Feb 2000
Aircraft type Mitsubishi MU-2B-60
Additional details: None

NTSB Factual Report

HISTORY OF FLIGHT

On February 11, 2000, at 0815 pacific standard time, a Mitsubishi MU-2B-60, N152BK, operated by American Check Transport, was destroyed when it impacted terrain approximately 1.5 nautical miles east of the Lewiston Nez-Perce County Airport (LWS), Lewiston, Idaho. The 14 CFR Part 135 non-scheduled domestic cargo flight had departed Boise Air Terminal Airport (BOI), Boise, Idaho, at 0723 and was en route to the Lewiston airport. The airplane was cleared for the ILS Rwy 26 approach to the airport. The Lewiston Air Traffic Control (ATC) tower controller reported the airplane in sight approximately four miles from the airport. The pilot was given the option of landing on runway 26 or runway 29, and he chose to land on runway 29. At 0815, the winds were 300 degrees at 13 knots, gusting to 21 knots. At approximately two miles east of the airport, the pilot reported a dual engine flameout. The airplane impacted the ground near the top of a ridgeline. The airline transport pilot was fatally injured. Visual meteorological conditions prevailed and an IFR flight plan had been filed.

The flight was one leg of a regularly scheduled cargo flight that originated in Salt Lake City, Utah, where the airplane was based. The routine flight plan, which the pilot had regularly flown during the past 12 months, was to fly in the morning from Salt Lake City to Boise, Idaho; then to Lewiston, Idaho; and then to Coeur d'Alene, Idaho. At approximately 1800, the pilot would return to Salt Lake City via Lewiston and Boise. The flight logbook maintained by the pilot indicated that the entire flight required about 5.2 hours of flight time. The logbook indicated the flight schedule provided the pilot 9 hours of rest.

On February 11, 2000, N152BK had departed Salt Lake City and arrived in Boise without incident. Fuel logs maintained at the Boise Executive Terminal, Inc., showed that N152BK was fueled with 100 gallons of jet fuel.

N152BK departed Boise at approximately 0723 en route to Lewiston. The Lewiston ATC Tower manager reported that N152BK was in contact with Seattle Center prior to being "handed off" to Lewiston Tower. N152BK was required to hold prior to executing the ILS Runway 26 approach to Lewiston Airport since it could not commence an instrument approach until another airplane, a Cessna Caravan operated by Federal Express, had landed at Lewiston. After the Caravan landed, N152BK was cleared for the ILS Rwy 26 approach.

Radar data indicated that N152BK's en route altitude from BOI to LEW was 16,000 feet mean sea level (msl). At approximately 0756, N152BK started a descent to 6,000 feet msl. The last radar contact at 0809:01 indicated N152BK was at 6,000 feet msl and 7.75 nautical miles on a 081 degree bearing from the Perce VOR.

The LEW ATC Tower manager reported the normal lowest holding altitude for airplanes waiting to make an approach into LEW is 6,000 to 7,000 feet msl. The approach plate for the LEW ILS RWY 26 approach indicates the minimum altitude for the Procedure Turn is 5,300 feet msl. The ILS glide slope intercept altitude is 4,700 feet msl. The distance from the outer marker to the runway is 5.9 nautical miles, and the inbound course is 259 degrees magnetic. The airport elevation is 1,438 feet msl.

At 0810:37, N152BK reported to Lewiston Tower that it was inbound on the ILS approach.

The ATC Tower controller reported that he saw N152BK come out of the clouds approximately four miles from the airport. The tower controller reported he gave N152BK the option of landing on runway 29.

At 0815:25, N152BK reported, "Let's see, I'll take 29."

The tower controller reported observing N152BK turn left and then turn back to the right to line up on runway 29 centerline.

At 0815:25, N152BK reported, "I just had two flameouts. I'm goin in."

At 0815:30, N152BK reported, "I'm gonna pick out ah, ah...."

At 0815:32, N152BK reported, "Pickin out, ah, I'll go as far as I...." No further transmissions were made by N152BK.

At 0815:39, an unintelligible sound was made.

At 0815:48, the sound of an Emergency Locator Transmitter (ELT) was heard.

The tower controller reported that N152BK's location, when the pilot reported the dual flameout, was over a residential subdivision located about 2 miles east of the airport. He reported that N152BK's altitude was approximately 400 feet above ground level (agl). He reported observing N152BK descend in altitude until it was blocked from his sight by the rolling terrain.

Two witnesses observed N152BK as it over flew the residential area. One witness reported hearing, "... two noises (one followed by another)... " that sounded like, "... skidding in slush." He reported seeing two vapor trails from the airplane. He reported the airplane increased its descent after it crossed 10th street. He did not hear or see the impact.

Another witness reported seeing the airplane flying west in front of her house. She reported hearing a whining type of noise. She reported the airplane was, "... just barely over the power lines." She reported seeing white smoke coming from the left engine. She lost sight of the airplane as it flew down the canyon. She did not see the impact.

N152BK impacted the terrain about 20 feet from the top of a ridgeline. N152BK came to rest on top of the ridgeline in a plowed field located approximately 1.5 miles east of the airport. The accident site could not be observed from the airport tower due to hilly terrain. Rescue personnel arrived at the accident site at approximately 0826.

PERSONNEL INFORMATION

The pilot was an airline transport pilot with single engine and multi-engine land ratings. He held a Second Class medical certificate. He was a Certified Flight Instructor in single engine land airplanes and instruments. He had retired from a major airline where he had obtained airplane type ratings in the following airplanes: B-337, B-727, B-737, B-747, B-747-4, BA-111, DC-9, and L-188's. He had a total of about 21,100 hours of flight time. 19,700 flight hours were in multi-engine airplanes. In the last 13 months, the pilot had flown approximately 1,100 hours in the make and model of the accident airplane.

The pilot was employed by the aircraft operator in November 1998. The pilot was qualified to fly in the company's Mitsubishi MU-2's and Piper PA-31's. The pilot had completed an annual check ride in the MU-2 on November 26, 1999. In the last 90 days, the pilot had logged about 321 hours of flight time.

AIRCRAFT INFORMATION

The airplane was a twin engine Mitsubishi MU-2B-60, serial number 1537SA. The airplane was configured for cargo operations and seated two. Its maximum gross weight was 11,575 pounds. The engines were Garrett TPE-331-10 engines flat rated to 715 shaft horsepower. The last 100 hour continuous airworthiness inspection was conducted on February 10, 2000. The airplane had flown approximately 2 hours since the last inspection and had a total time of 5,460 hours.

METEOROLOGICAL CONDITIONS

The observed weather at LWS at 0716 was: winds 290 degrees at 8 knots; visibility 10 miles; ceiling 3,400 feet overcast; temperature 1 degree C; dew point 0 degree C; altimeter setting 29.76 inches of Hg.; unknown precipitation (UP) ended 0713; 0.00 inch (trace) precipitation from 0656.

The observed weather at LWS at 0756 was: winds 300 degrees at 14 knots gusts to 19 knots; visibility 10 miles; ceiling 3,600 feet overcast; temperature 2 degrees C; dew point -1 degree C; altimeter setting 29.78 inches of Hg.; UP ended 0713; 0.00 inch (trace) precipitation from 0656.

The observed weather at LWS at 0815 was: winds 300 degrees at 13 knots, gusting to 21 knots; sky condition 3,200 feet broken, 4,000 feet overcast; visibility 10 miles; temperature 2 degrees C; dew point -1 degrees C; altimeter 29.80.

Pilot Weather Reports (PIREPs) for the BOI and LWS areas indicated light to moderate mixed and rime icing was present.

At 0644, a PIREP indicated moderate mixed icing between 10,000 to 12,000 feet mean sea level (msl) over the Perce VOR (MQG) located about 3 nautical miles east of LWS.

At 0730, a PIREP indicated moderate rime icing at 13,000 feet msl, 40 nautical miles southeast of BOI.

At 0849, a PIREP indicated light mixed icing at 7,000 feet msl, 20 nautical miles north-northeast of LWS.

At 0905, a PIREP indicated light rime icing at 11,500 to 13,700 feet msl, at 20 nautical miles east of BOI.

At 0916, a PIREP indicated light to moderate rime icing 10,000 to 15,000 feet msl, 25 nautical miles northwest of BOI.

The Upper Air Data for Spokane, Washington, located 82 nautical miles north-northwest of LEW, indicated that at 0400 on February 11, 2000, the temperature at 3,000 feet msl was -2.17 degrees C. At 1600, the temperature at 3,000 feet msl was -0.85 degrees C.

The National Weather Service issued the AIRMET Zulu Update 2 for Ice (SLCZ WA 111445) on February 11, 2000 at 0645, and it was valid until February 11, 2000 at 1300. The forecast was for occasional moderate rime/mixed icing in clouds and in precipitation below 15,000 feet. The area covered by this AIRMET included the route from BOI to LWS.

The National Weather Service issued the AIRMET Sierra Update 5 for IFR (SLCS WA 111605 AMD) on February 11, 2000 at 0805, and it was valid until February 11, 2000 at 1300. The forecast was for occasional ceilings below 1,000 feet/visibility below 3 miles in clouds/precipitation/mist. The northeastern extent of this AIRMET area was just south of LWS. (See NTSB Meteorological Factual Report)

WRECKAGE AND IMPACT INFORMATION

The airplane impacted the slope of a ridgeline and the wreckage path was oriented on a heading of 240 degrees. The main wreckage came to rest about 64 feet from the initial impact mark and was on top of the ridgeline in a muddy plowed field. The nose and longitudinal axis of the airplane was on a heading of 165 degrees.

Numerous aircraft parts from the left side of the airplane were found in the wreckage path from the initial impact mark to the main wreckage. The parts included the left landing gear, left forward gear door, left forward main door, a blade from the left propeller, the left elevator counterweight, and a section from the left elevator.

The left propeller was located on top of the ridgeline and about 20 feet from the main wreckage. One of the four propeller blades had separated from the hub.

The left tip tank was found 162 feet from the initial impact mark. The tip tank exhibited crushing along the lower surface of the tank. The front tip of the fuel tank did not exhibit any crushing.

The radome separated from the fuselage and was found 1.5 feet from the right wing tip tank.

The lower surface of the fuselage exhibited crushing from the forward pressure bulkhead, Fuselage Station (FS) 1275, to the aft side of the main cabin door, FS 7250. The roof of the fuselage cabin was crushed from approximately FS 4025 to FS 5890 where the high wing crushed down into the cabin area. The nose landing gear had separated from the fuselage and the nose gear trunion was found against the left side of the fuselage. The right main landing gear remained attached to the fuselage fitting; the drag strut was broken.

The two upper fuselage-to-empennage attach fittings failed at FS 8995, resulting in the separation of the empennage from the fuselage. The vertical tail, right horizontal tail, and right elevator exhibited minor damage and no crushing. The left horizontal tail was bent upward about 10 degrees at approximately Horizontal Station 1790. The fuselage strakes were deformed.

The left wing remained attached to the fuselage. The left engine remained attached to the left wing. The left wing was broken and separated outboard of the engine at approximately Wing Station (WS) 2550. The left outer wing was broken upward about 10 degrees at approximately WS 3800. The left wing flaps, ailerons, and trim ailerons remained attached to their respective wing sections.

The right wing-to-fuselage fittings were broken and the wing separated from the fuselage. The right engine and propeller remained attached to the right wing. The right wing was broken inboard of the right engine at approximately WS 1950. The right outer wing panel was bent up about 5 degrees at approximately WS 3800. The right tip tank wing-to-tip tank fittings were deformed, but the tip tank remained attached to the right wing. The right inboard flap was separated from the wing and was found 34 feet in back of the right wing. The right outboard flap and trim aileron remained attached to the wing.

Control cable continuity for the elevator, rudder, and trim tabs was established from the aft pressure bulkhead to the elevator and rudder bellcrank and trim actuators.

Fuel tanks and fuel lines were ruptured and no fuel was found in the tanks. Fuel was leaking from the lines when the wreckage was removed from the site. Rescue personnel reported that they smelled fuel when the arrived at the accident scene. The main fuel gauge read approximately 1040 pounds.

The on-site examination of the cockpit switches revealed the switches were found in the following positions:

Main Fuel Valves OPEN

L & R Pitot Heat ON

L & R Engine Inlet Heat OFF

Propeller Anti-Ice Left OFF, Right ON

Oil Cooler Inlet Anti-ice Left ON, Right OFF

L & R Continuous Ignition OFF

Examination of the pilot's seat belt and shoulder harness revealed that the seat belt buckle was still engaged and the seat belt was fastened around the pilot. But the two shoulder harness straps were hanging loose and not attached to the seat belt buckle. Fire department personnel reported they had found the seat belt engaged and the shoulder harness not in use when they arrived at the accident site.

A MU-2B-60 Airplane Flight Manual was recovered from the airplane wreckage. The manual was current with the latest revisions incorporated.

MEDICAL AND PATHOLOGICAL INFORMATION

The autopsy on the pilot was performed at the Pathologists' Regional Laboratory in Lewiston, Idaho.

A Forensic Toxicology Fatal Accident Report was prepared by the FAA Civil Aeromedical Institute. The report indicated the following results:

No Carbon Monoxide detected in blood.

No Cyanide detected in blood.

No Ethanol detected in urine.

0.054 (ug/ml, ug/g) Hydrocodone detected in blood.

Hydrocodone present in urine.

2.665 (ug/mL, ug/g) Dihydrocodeine detected in blood.

Dihydrocodeine present in urine.

0.806 (ug/ml, ug/g) Diphenhydramine detected in blood.

Diphenhydramine present in urine.

Dihydrocodeine is a prescription narcotic painkiller used for the control of moderate to severe pain. Hydrocodone is a prescription narcotic painkiller that can also be produced by the metabolism of dihydrocodeine. Diphenhydramine is an over-the-counter sedating antihistamine.

Clark's Isolation and Identification of Drugs, Senior consulting editor A.C. Moffat, second edition, London, The Pharmaceutical Press, 1986, contained the following information concerning the therapeutic concentrations of dihydrocodeine:

"Following single doses of 30 mg and 60 mg to 7 subjects, mean peak plasma concentrations of 0.072 to 0.146 ug/ml were attained in 1.7 hours; the corresponding peak plasma concentrations of acidic metabolites were 0.56 and 1.48 ug/ml."

The therapeutic concentrations for diphenhydramine were described as follows:

"In plasma, usually in the range of 0.1 to 1.0 ug/ml."

The pilot's medical records indicated that in December 1994 the pilot had become a habitual user of dihydrocodeine, and had self disclosed this fact to the medical personnel at the major airline where he was employed. The toxicologist for the laboratory that performed the drug screen for the airline reported that the laboratory's routine drug screen would not have detected nor reported dihydrocodeine. The laboratory performed testing under DOT guidelines that required the identification of opiates only for the presence of codeine and morphine. On August 22, 1995, the pilot was found eligible for and received a special issuance of a second-class medical certifi

NTSB Probable Cause

the pilot failed to follow the flight manual procedures and did not engage the Continuous Ignition system resulting in both engines flaming out when the air induction system was blocked with ice. Additional factors to the accident included the hilly terrain, the icing conditions, and the operator not complying with a Service Bulletin for the installation of an auto-ignition system.

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