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N72TZ accident description

Idaho map... Idaho list
Crash location 43.581389°N, 116.523056°W
Nearest city Nampa, ID
43.540717°N, 116.563462°W
3.5 miles away
Tail number N72TZ
Accident date 24 Sep 2009
Aircraft type Frazier Tangent
Additional details: None

NTSB Factual Report

HISTORY OF FLIGHT

On September 24, 2009, about 1030 mountain daylight time, a Frazier Tangent, N72TZ, experimental category airplane, collided with terrain during high speed taxi tests at Nampa Municipal Airport, Nampa, Idaho. The commercial pilot operated the airplane under the provisions of Title 14 Code of Federal Regulations, Part 91. The pilot was killed, and the airplane was substantially damaged. Visual meteorological conditions prevailed, and no flight plan had been filed. According to a colleague of the pilot, the pilot was performing high speed taxi tests and routinely raised the nose of the airplane up during the test runs. During the test run that precipitated the accident, the airplane became airborne and rose to about 75 feet above ground level (agl), started a right-hand turn, stalled, and impacted terrain in a flat attitude. Audible engine sounds could be heard from the airplane throughout the event.

PERSONNEL INFORMATION

The pilot, age 62, held a commercial pilot certificate with ratings for airplane multiengine land, and instrument airplane, with single-engine land private pilot privileges, issued on February 15, 1999. He held a third-class medical certificate issued in April 28, 2009, with the restriction that he possess glasses for near and intermediate vision. Examination of a copy of the pilot’s most recent logbook recorded a total flight time of 2,170 hours, with 994 hours of multiengine time. No flight time was recorded within the last 90 days. His most recent flight review was conducted on June 21, 2008.

AIRCRAFT INFORMATION

The single seat, twin engine, experimental category airplane, serial number (S/N) 001, was of the pilot's own design, with a conventional T-tail and a forward canard. It was powered by two Hirth F33V, 28-hp engines. The engines were mounted on the inboard trailing edge of each wing facing aft, in a pusher type configuration. The landing gear main mounts are forward of the engine nacelles. The main mounts were fixed and the nose gear was retractable. Each engine was equipped with a Powerfin E-48 fixed pitch composite propeller. A review of a copy of the airplane's maintenance logbook showed that the pilot/builder performed a 100-hour inspection on July 2, 2009, and a special airworthiness certificate was issued on the same date. The airplane had not accumulated any flight time at the time of the inspection.

A colleague of the pilot, who is a commercial pilot and airframe and power plant (A&P) mechanic, worked with the pilot on the airplane design, construction, and testing. He said that they were at the beginning of the ground handling and taxiing testing phase. During previous high speed taxiing tests (35-55 knots), pitch was nonresponsive; the nose would not lift to a positive angle of attack (AOA). They added ballast to move the center of gravity (CG) aft of 30 percent mean aerodynamic chord (MAC), and added a larger canard control surface (elevator), which provided the desired pitch control at 45-50 knots. Additionally, he stated that, "It is not uncommon for a pusher prop type aircraft to have a pitch up tendency with a reduction in power when the wheels are on the runway."

FLIGHT RECORDERS

The airplane was equipped with a Dynon Avionics Flight DEK-D180 electronic flight information system (EFIS) that recorded the following data in 1-second intervals: fuel level (each tank); exhaust gas temperature (EGT) for each engine; cylinder head temperature (CHT) for each engine; pitch; roll; heading; turn rate; airspeed; altitude; vertical speed; g’s; and outside air temperature (OAT). The data provided to the Safety Board investigator-in-charge (IIC) consisted of the taxi run before the accident and the accident taxi run. The data from the first taxi run revealed that the pitch varied between 0 and 9 degrees throughout the run, and a maximum airspeed of 67 knots was achieved. The data from the taxi run that precipitated the accident revealed that during the last 16 seconds of data, the pitch rose rapidly from 8 to almost 45 degrees then suddenly dropped to negative 18 degrees; the airspeed decayed from 55 to 22 knots as the pitch passed from positive to negative. The altitude data showed that just prior to the pitch excursion the airplane was at 2,384 feet (mean sea level), and the peak altitude recorded during the excursion was 2,506 feet before the altitude data decreased, which implied that the airplane climbed approximately 122 feet above the ground before it descended. The recorded airspeed during the last 3 seconds of data was zero.

WRECKAGE AND IMPACT INFORMATION

The wreckage was located in the dirt infield next to the runway. The airplane was upright with the nose pointed perpendicularly away from the runway edge. The airplane wreckage was completely intact; the landing gear had collapsed into the fuselage. A ground scar was present that extended about 20 feet behind the wreckage. A Federal Aviation Administration (FAA) inspector examined the airplane on scene, and reported that there was control continuity between ailerons, canard, rudder. The engine controls cables from the throttle quadrant in the cockpit were connected to both engines. Each of the three bladed propellers had two blades sheared off at the hub, and one blade still in its hub.

MEDICAL AND PATHOLOGICAL INFORMATION

An autopsy was performed on the pilot November 2, 2009, by the Canyon County Coroner, Caldwell, Idaho, Forensic Pathologist. The autopsy findings state that the cause of death was "Blunt force trauma due to an aircraft accident," and noted medical intervention to include an endotracheal tube, a neck brace, EKG pads, pacemaker pads over the torso and catheters in both tibias.

Forensic toxicology was performed on specimens from the pilot by the FAA Forensic Toxicology Research Team, CAMI, Oklahoma City, Oklahoma. The toxicological report stated that there was no carbon monoxide, cyanide, or ethanol detected. Atropine was detected in the liver and blood, and diphenhydramine was detected in the liver and blood.

The pilot’s most recent application for third-class airman medical certificate, dated April 28, 2009, did not note any medical conditions or the use of diphenhydramine. The pilot’s spouse noted that the pilot took Tylenol PM several times a week to help him sleep.

NTSB Probable Cause

The pilot's failure to maintain pitch control of the airplane.

© 2009-2020 Lee C. Baker / Crosswind Software, LLC. For informational purposes only.