Crash location | 40.570834°N, 90.080278°W |
Nearest city | Canton, IL
40.581705°N, 90.046506°W 1.9 miles away |
Tail number | N2968C |
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Accident date | 21 Jul 2003 |
Aircraft type | Navion L-17A |
Additional details: | None |
On July 21, 2003, at 2039 central daylight time, a Navion L-17A, N2968C, owned and piloted by an airline transport pilot, was substantially damaged during a forced landing following a loss of engine power about one-quarter mile east of the Ingersoll Airport (CTK), Canton, Illinois. The airplane was on final approach to runway 27 (3,295 feet by 60 feet, asphalt) at CTK. The personal flight was operating under 14 CFR Part 91 and was not on a flight plan. Visual meteorological conditions prevailed at the time of the accident. The pilot reported minor injuries. The flight departed the Delaware Municipal Airport, Delaware, Ohio, at 1715 central daylight time. The final destination was Manhattan Regional Airport, Manhattan, Kansas, with a planned fuel stop at CTK.
The pilot reported the engine lost power completely as the electric fuel boost pump was turned on in preparation for landing. He stated: "As flight neared final for [runway] 27 at CTK, aircraft was slowed to gear/flap speed (100 mph, [indicated airspeed]), gear lowered and (full) flaps deployed. Boost pump was turned on; engine immediately hesitated for 1-2 seconds and then failed (to windmill state)." He noted the aircraft was at 800 feet above ground level when the engine failed. With the landing gear and flaps extended, and the propeller windmilling, the descent rate was "high, approximately 1,000 [feet per minute]," according to the pilot.
The pilot's attempts to restart the engine were not successful. Unable to make the runway, the pilot decided to executed a forced landing straight ahead; approximately one-quarter mile from the airport. The aircraft impacted a bean field and struck a berm, shearing off the landing gear.
According to the pilot, approximately ten miles from CTK, he switched from the main fuel tanks to the auxiliary fuel tank. He reported the "switch over was made using boost pump for approximately 30 seconds. Engine operation after switch over was smooth." He noted the elasped flight time at the time the tanks were changed was about 3 hours. The aircraft's main fuel tank capacity was 39-1/2 gallons and fuel burn rate was about 12 gallons per hour.
A post-accident examination was conducted. The landing gear had collapsed and the aircraft was resting upright on the ground. The fuselage skin was wrinkled on both sides immediately aft of the cabin area/wing root fairing. The engine and cowling remained intact. The propeller was oriented horizontally at the accident site. The right side (descending) blade was bent aft about 45 degrees at a point approximately 1/3 of the span from the spinner. No other damage to either propeller blade was observed.
A total of four gallons of fuel was recovered from the main fuel tanks. The auxiliary fuel tank was about 1/2 full. The fuel selector was set to the aux tank. A fuel smell was present in the engine compartment. The auxilary fuel tank was located under the rear passenger seat and had an approximate capacity of 20 gallons. The outlet was located at the aft center portion, on the bottom of the tank. The fuel outlet fed into a small header tank.
Engine continuity was verified through crankshaft rotation. Compression was present at all cylinders. The magnetos and spark plugs operated properly when tested. The fuel selector functioned properly, however, the selector leaked air under suction. No sign of leakage was detected when pressure was applied. Fuel flow was observed through the electric fuel boost pump when power was applied to the pump. However, fuel was observed leaking from the carburetor when the pump was activated. The carburetor was removed for further inspection.
The carburetor was returned to the manufacturer for examination under supervision of the NTSB. An external inspection observed no damage to the carburetor. The throttle control rotated smoothly. All fittings and levers were present and in good condition. Movement of the mixture control, however, was "sluggish."
A bench flow test of the carburetor was conducted. Of the ten data points measured, flow rates at two were determined to be out of acceptable standards. Specifically, test point 4 measured 34.0 pounds per hour (pph), where the acceptable range was 34.85 - 36.95 pph. Test point 5 measured 46.5 pph, where the acceptable range was 46.7 - 49.5 pph. All other test points measured within acceptable limits. No external leakage was noted during the bench test.
Upon teardown, the mixture control needle and spring were found to be covered with grease. The fuel inlet screen was clean; all passages, bleeds and jets were unobstructed; and the gaskets and diaphrams appeared undamaged.
According to the Federal Aviation Administration Type Certificate Data Sheet for the L-17A, all auxiliary fuel tank installations are required to have a placard in clear view of the pilot restricting use of the aux tank to level flight only. A placard was not present in the aircraft when inspected after the accident.
A complete loss of engine power during landing approach for undetermined reasons, as well as the unsuitable terrain for a forced landing encountered by the pilot. Contributing factors were the berm and the crops.