Crash location | 30.285555°N, 92.941111°W |
Nearest city | Fenton, LA
30.367148°N, 92.918204°W 5.8 miles away |
Tail number | N63E |
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Accident date | 01 May 2005 |
Aircraft type | Grumman-Schweizer G-164B |
Additional details: | None |
On May 1, 2005, approximately 0730 central daylight time, a tail-wheel equipped Grumman-Schweizer G-164B agricultural turbine powered single-engine airplane, N63E, was substantially damaged during a forced landing following a reported loss of engine power during an aerial application flight near Fenton, Louisiana. The airplane was registered to and operated by Kinder Ag Service, Inc., of Natchitoches, Louisiana. The commercial pilot, sole occupant of the airplane, was not injured. Visual meteorological conditions prevailed, and a flight plan was not filed for the 14 Code of Federal Regulations Part 137 aerial application flight. The local flight originated from a private airstrip near Kinder, Louisiana, at an unknown time.
In a written statement to the NTSB investigator-in-charge, the 2,800-hour pilot reported that he had just finished a turn to reverse direction and was in the process of positioning the airplane for the next pass when "the engine lost power." The pilot added that he attempted to land on an adjacent field road; however, the airplane landed short of the road, struck a drainage canal, bounced, and came to rest in an upright position in a rice field. There was no fire.
The pilot added that as the airplane came to a stop, the engine was still running. After shutting the engine down, the pilot evacuated the airplane.
Examination of the airplane by an Federal Aviation Administration (FAA) inspector, who responded to the accident site, revealed that the left and right main landing gear were folded outboard, and the main support beam for the landing gear was cracked. Fuel was observed in the left wing fuel tank.
Examination of the Walter M601 turbine engine by a representative from Walter America Inc., of West Helena, Arkansas, revealed that the firewall fuel filter was blocked by an unknown foreign contaminant. Remaining fuel drained from the fuel control unit and the engine fuel pump was found to be consistent with diesel fuel.
A completed Pilot/Operator Aircraft Accident Report (NTSB Form 6120.1/2) was not received from the pilot or the operator.
The loss of engine power due to fuel starvation as a result of blockage of the firewall fuel filter with an unknown contaminant. A contributing factor was the lack of suitable terrain for the forced landing.