Crash location | 42.397777°N, 70.866389°W |
Nearest city | Nahant, MA
42.425097°N, 70.916159°W 3.2 miles away |
Tail number | N3558G |
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Accident date | 06 May 2001 |
Aircraft type | Piper PA 31-350 |
Additional details: | None |
On May 6, 2001, about 2015 eastern daylight time, a Piper PA 31-350, N3558G, experienced a loss of engine power on both engines, and ditched in Massachusetts Bay, 3 miles southeast of Nahant, Massachusetts. The pilot and eight passengers sustained minor injuries. Visual meteorological conditions prevailed and an instrument flight rules flight plan was filed for the flight that departed Nantucket Memorial Airport (ACK), about 1945, destined for the Beverly Municipal Airport (BVY). The personal flight was conducted under 14 CFR Part 91.
The airplane was owned by the pilot and based at BVY. Earlier in the day, the pilot and the eight passengers departed BVY, and flew to ACK for dinner.
During a telephone interview, the pilot stated he departed BVY with 24 gallons of fuel in the outboard tanks, and 80 gallons of fuel in the main tanks. He used the main tanks for takeoff and landing, and conducted the majority of the flight utilizing the outboard fuel tanks. Additionally, he described the flight as "normal and uneventful."
After landing at ACK, the airplane was refueled with 24 gallons of 100 low-lead (100LL) aviation gasoline; 12 gallons in each main fuel tank. Before departing ACK, the pilot performed a preflight inspection of the airplane, which included a walk around inspection and a check of the control surfaces, engine cowlings, tires, and the underside of the airplane. He did not visually check or sump the airplane's fuel tanks.
The pilot described the takeoff from ACK as normal; however, he experienced a "small surge in both engines," while climbing through 1,150 and 3,300 feet, respectively. He further described the surges as "minor but still noticeable." About 30 minutes later, when the airplane had descended, and was leveling at 1,500 feet, the pilot experienced an intermittent illumination of the "right aux fuel pump light," which was followed by a total loss of power on the right engine. The pilot turned the electric fuel pump on, switched to the outboard tank, and pushed the throttle, propeller and mixture levers to the full forward position, with no response from the engine. He then elected to feather the right engine propeller. The airplane was not able to maintain altitude on one engine and began a slow descent.
Shortly thereafter, the left engine began "surging." The left engine manifold pressure was at 32 inches, when it began to drop and return. The surging continued regardless of the position of the throttle and caused the airplane to yaw and porpoise. He did not recall the engine's fuel flow, fuel pressure or rpm. The pilot said the left engine was producing "some power." The airplane continued to descend, yaw and porpoise, and after about "three or four minutes, at most," he feathered the left engine propeller.
The pilot stated he thought carefully about not stalling the airplane during the ditching and he maintained an airspeed of about 85 knots. He stated that it was "dark"; however, he was able to see the water due to the moonlight. After touchdown, he exited the airplane via the pilot's seat window exit, and inflated a raft. The passengers then exited the airplane and the airplane sank within "40 to 45 seconds."
The airplane was located on May 9, 2001, by Massachusetts State Police divers and the Army Corp. of Engineers. The airplane came to rest inverted, at a depth of about 100 feet. The airplane was recovered on June 7, 2001, and was examined by a Federal Aviation Administration (FAA) inspector, with representatives of Textron Lycoming, and The New Piper Aircraft Company.
The landing gear and flaps were found in the retracted position. Flight control continuity was verified to all control surfaces. The fuel selectors were positioned to the outboard fuel tanks, and the throttle, propeller and mixture levers were full forward. The airplane's fuel tanks remained intact, and all fuel caps were in-place. Samples from the airplane's fuel tanks taken just after the airplane was recovered revealed fluid consistent with seawater with "some odor of fuel;" however, no visible evidence of fuel was observed. All fuel valves were tested and found to be operational. Additionally, the supply lines between the fuel valves and fuel pumps were removed and found to be unobstructed. Both engine fuel filters were corroded, consistent with saltwater corrosion.
Both propellers were observed in the feathered positions. The dual magneto cases were destroyed by corrosion and could not be examined. Both engine crankshafts rotated freely, and compression and valve train continuity was attained for all cylinders. Both oil filters were filled with a mixture of oil and seawater, however, internal examination of the filter elements did not reveal any contamination.
Examination of the airframe and engine did not reveal evidence of any pre-impact mechanical malfunctions.
According to the airplane information (AIM) manual, the airplane was equipped with four flexible fuel cells, with two fuel cells located in each wing panel. The outboard fuel cells held 40 gallons each, and the inboard fuel cells held 56 gallons each, for a total of 192 gallons, of which 182 gallons was "usable."
The ACK airport manager reported that several other airplanes were refueled from the same fuel supply, which was added to the accident airplane. Additionally, a sample of the fuel was tested and found to meet or exceed the specifications for 100LL aviation gasoline.
The pilot reported he had purchased the airplane and attended 5-day type specific training course in March 2001. He reported about 1,050 hours of total fight experience, which included 800 hours in multi-engine airplanes, of which 65 hours was in the make and model of the accident airplane.
Additionally, the pilot reported he had been flying the airplane often during the past few weeks, and had not experienced any prior mechanical problems. He believed he had flown the airplane the day prior to the accident as well. The last documented refueling of the airplane prior to the date of the accident occurred on May 3, 2001, when the airplane was refueled with 128 gallons of aviation gasoline. The last flight documented in the pilot's logbook was on May 4, 2001, when the pilot logged 1.9 hours in the accident airplane. The pilot said he normally flew a 65 percent power, a "a little rich," and experienced a fuel burn of about 20 to 21 gallons per hour, for each engine.
According to maintenance records, the airplane's most recent annual inspection was performed on February 7, 2001. At that time, the airplane had been operated for about 2,920 total hours, and both engines had been operated for about 1,300 hours since major overhaul.
The weather reported at an airport about 7 miles west of the accident site, at 2054, was: wind from 090 degrees at 6 knots; visibility 10 statue miles; clear skies; temperature 7 degrees C; dew point 2 degrees C; altimeter 30.58 in/hg.
A loss of engine power due to fuel exhaustion for undetermined reasons. A factor in this accident was the pilot's failure to visual check the airplane's fuel quantity prior to takeoff.