Crash location | 45.888055°N, 84.747222°W |
Nearest city | St. Ignace, MI
45.903170°N, 84.720568°W 1.7 miles away |
Tail number | N3081N |
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Accident date | 13 Jul 2010 |
Aircraft type | Beech 58 |
Additional details: | None |
HISTORY OF FLIGHT
On July 13, 2010, at 1700 eastern daylight time, a Beech 58 twin-engine airplane, N3081N, sustained substantial damage when it impacted terrain shortly after takeoff from the Mackinac County Airport (83D), St. Ignace, Michigan. The private pilot and three passengers were fatally injured and one passenger was seriously injured. The airplane was registered to Tri United, Inc., Skokie, Illinois, and operated by the pilot. Visual meteorological conditions prevailed, and an instrument rules flight (IFR) plan was filed for the 14 Code of Federal Regulations Part 91 personal flight. The flight was departing at the time of the accident.
According to information provided by air traffic control, local authorities, and witnesses, the airplane departed Chicago Executive Airport (PWK), Wheeling, Illinois, at 1210, and arrived at 83D at 1354. According to a 83D fixed based operator (FBO) representative, the pilot came into the lobby and asked if he was at Mackinac Island. The representative explained to him that 83D was not on the island and she then pointed the island out through a window to the pilot. Mackinac Island is located approximately 5 miles east of 83D. The airplane then departed 83D and arrived at Mackinac Island Airport (MCD) a few minutes later.
Approximately 1630, the airplane returned to 83D from MCD and obtained 60 gallons of fuel. At 1644, the pilot contacted air traffic control services via his airplane radio to amend his IFR clearance.
Witnesses, who were mechanics at a local maintenance facility, observed the airplane attempt to takeoff on runway 25 three different times. During the first attempt, the airplane traveled approximately half way down the runway and then the takeoff was aborted. The pilot taxied the airplane back to runway 25 and attempted a second takeoff without an engine run-up. During the second takeoff attempt, the airplane traveled approximately three-quarters of the way down the runway and the takeoff was aborted. One witness stated that during the second takeoff roll, it sounded as if the engines were not throttled up to full power, and it appeared that the pilot had problems maintaining directional control of the airplane.
The pilot taxied the airplane back to runway 25 and attempted a third takeoff without an engine run-up. One of the mechanic witnesses stated that during the third takeoff attempt, "It appeared and sounded as if the right engine was running properly and the left engine was not at the same RPM. The pilot was having difficulty maintaining directional control...with the left engine sputtering and misfiring and traces of black smoke coming from the left engine exhaust." Witnesses observed the airplane become airborne near the departure end of the runway with the wings rocking back and forth, and the left wing impacted the northbound lanes of Interstate 75, which is located approximately 1,000 feet from the departure end of runway 25. The airplane continued through the highway median, traveled across the southbound lanes of the interstate and came to rest inverted in a grassy area adjacent to the interstate. A post crash fire ensued and consumed a majority of the airplane.
The seriously injured passenger, who was seated in the rear seat, exited the airplane after it came to rest. According to the passenger, he was sleeping at the time of the accident and had no recollection of the accident sequence.
PERSONNEL INFORMATION
The pilot, age 73, held a private pilot certificate with airplane single and multi-engine land and instrument ratings. His most recent Federal Aviation Administration (FAA) third-class medical examination was conducted on December 30, 2008. After review, the FAA issued the pilot a Class 3 Special Issuance Medical Certificate that was not valid for any class after December 31, 2010. In addition, the certificate noted a restriction for corrective lenses for near and distant vision.
The pilot's flight time logbook was destroyed during the accident. On his most recent medical application, the pilot reported 2,211 total flight hours and 67 in the previous six months.
A review of the pilot's FAA airman records showed that the pilot was issued his single engine land airplane rating on May 22, 1989, his instrument rating on May 27, 1990, and his multi-engine land airplane rating on August 29, 1991.
On December 7, 2006, the pilot was reexamined by the FAA in the accident airplane as the result of an undisclosed violation. The reexamination was disapproved by the FAA inspector for undisclosed reasons. On January 9, 2007, the pilot was reexamined by the FAA in the accident airplane. The reexamination was disapproved by the FAA inspector for undisclosed reasons. On that date, the pilot voluntarily surrendered his multi-engine land and instrument ratings.
On July 9, 2009, the pilot received his multi-engine land rating. On the rating application, the pilot reported 2,985 total flight hours and 2,097 hours in the accident airplane make and model.
On December 7, 2009, the pilot received his instrument rating for single engine land airplanes. On the rating application, the pilot reported 3,147 total flight hours.
On December 29, 2009, the pilot received his instrument rating for multi-engine land airplanes. On the application, the pilot reported a total of 3,166 total flight hours and 2,238 hours in the accident airplane make and model.
AIRCRAFT INFORMATION
The airplane was a 1987 Beech 58 (Baron), serial number TH-1526. It was a six-place, twin-engine airplane, with a retractable tricycle landing gear configuration. The airplane was powered by two 300-horsepower Teledyne Continental Motors IO-550-C engines. The left and right engine serial numbers were 271844-R and 271853-R, respectively. The engines were equipped with 3-blade, constant speed McCauley propellers.
Maintenance records showed the most recent annual inspection was completed on November 18, 2009, at a total airframe time of 3,902.6 hours. The left and right engines' most recent 100-hour inspections were completed on November 18, 2009, at a total time since major overhaul of 378.9 hours.
The airplane's weight and balance documentation was not located. Based on the weight of the occupants, estimated fuel load, and estimated baggage, the airplane was within the gross weight limitations at the time of the accident.
METEOROLOGICAL INFORMATION
Weather conditions reported at the time of the accident were clear sky, calm winds, and a temperature of approximately 80 degrees Fahrenheit. The calculated density altitude was approximately 2,300 feet.
AIRPORT INFORMATION
The Mackinac County Airport is a public, non-towered airport located 2 miles northwest of St. Ignace, Michigan, at a surveyed elevation of 624 feet. The airport features one runway, Runway 7/25, which has a concrete surface, and is 3,800 feet long by 75 feet wide.
Fuel records from the 83D airport FBO showed the airplane received 60.33 gallons of fuel prior to the planned departure. Three other airplanes obtained fuel from the FBO prior to the accident airplane. Fuel test results showed no anomalies with the fuel provided by the FBO.
WRECKAGE AND IMPACT INFORMATION
Initial ground impact was on the northbound lanes of Interstate 75 about 1,000 feet west of runway 25. The debris path was oriented on an approximate 230-degree magnetic heading. The main wreckage, which consisted of the fuselage, empennage, both wings, and right engine, came to rest inverted about 150 feet from the initial impact point. Grass scorched by the postimpact fire extended to the north and around the main wreckage.
The fuselage was consumed by fire. The cockpit and instrument panel were destroyed and consumed by fire. The cockpit and cabin seat frames were found separated from their attach fittings. The nose landing gear remained attached and the retract/extend arm was in the retracted position. The empennage was partially consumed by fire. The empennage flight control surfaces remained attached to their respective fittings.
The right wing was partially consumed by fire. The aileron and flap were consumed by fire. The flap actuator was consumed by fire and a flap position could not be determined. The landing gear remained attached and was found in the retracted position. The engine remained attached to the firewall and was damaged by fire. The right propeller remained attached to the engine crankshaft. The propeller blades contained leading edge gouging, s-type bending, and chordwise scratching.
The left wing was bent aft, twisted upright, and consumed by fire. The aileron was separated and partially consumed by fire. The flap was consumed by fire. The flap actuator was consumed by fire and a flap position could not be determined. The landing gear remained attached and found in the retracted position. The left engine was separated and came to rest in the debris path. The left propeller remained attached to the engine crankshaft. The propeller blades contained leading edge gouging, s-type bending, and chordwise scratching.
Flight control continuity was confirmed to all flight control surfaces. No anomalies consistent with a preimpact failure or malfunction of the airframe were observed.
PATHOLOGICAL INFORMATION
An autopsy was not performed on the pilot. The FAA's Civil Aeromedical Institute (CAMI) performed toxicology testing on the pilot's blood specimen. The tests for carbon monoxide, cyanide, and ethanol were negative. The following drugs were detected in the specimen: unspecified level of Amlodipine, unspecified level of Atenolol, and 5.6 percent Hemoglobin A1C. Amlodipine is a prescription medication that is a long-acting calcium channel blocker that is used to control high blood pressure and treat chronic angina. Atenolol is a beta blocker medication used to control high blood pressure or control heart rate. The use of Atenolol was not reported on his most recent medical certificate application.
The NTSB Medical Officer reviewed the medical records maintained by the FAA Aerospace Medical Certification Division, as well as records kept by the pilot's physicians. The following information was extracted from those records. The pilot had recurrent coronary artery disease with angioplasty procedures in 1999, 2000, 2003, and 2008. In January 2010, cardiovascular testing was normal with no evidence of disease progression since the angioplasty and stenting in 2008. The pilot had been diagnosed with obstructive sleep apnea and treatment with continuous positive airway pressure (CPAP) had been recommended. The diagnosis was not reported to the FAA. The pilot reported he stopped using the CPAP device. The pilot was a type-2 diabetic who controlled his condition with oral medication.
Air traffic control communications were reviewed to determine if there were any relevant speech patterns that were consistent with a medical issue.
TESTS AND RESEARCH
The engines were examined at Teledyne Continental Motors, Mobile, Alabama, under the supervision of the NTSB investigator-in-charge. Postaccident examination of the engines revealed the engines could not be test run due to impact and fire damage, and a teardown inspection was completed. The teardown inspection showed no anomalies that would have prevented normal engine operation.
The left engine throttle and fuel control unit were bench tested, and the unit functioned with no anomalies. The left engine fuel pump could not be bench tested due to damage. The pump was disassembled and no anomalies were noted. The left engine fuel manifold valve was bench tested and no anomalies were noted.
The right engine throttle and fuel control unit was damaged due to impact and fire. The unit could not be bench tested due to damage. The right engine fuel pump could not be bench tested due to damage. The pump was disassembled and no anomalies were noted. The right engine fuel manifold valve was damaged by fire. The valve could not be bench tested. The valve was disassembled and no anomalies were noted.
The propellers were examined at McCauley, Wichita, Kansas, under the supervision of the NTSB investigator-in-charge. Examination of the propellers revealed the blade angles at the time of impact were in the low pitch operating range position. No anomalies were noted with the propellers.
The pilot's failure to maintain aircraft control during takeoff for undetermined reasons.