Crash location | 37.341944°N, 93.466945°W |
Nearest city | Willard, MO
37.305047°N, 93.428527°W 3.3 miles away |
Tail number | N436KS |
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Accident date | 15 Sep 2012 |
Aircraft type | Cirrus Design Corp SR22 |
Additional details: | None |
HISTORY OF FLIGHT
On September 15, 2012, at 0021 central daylight time, a Cirrus Design SR22 airplane, N436KS, was substantially damaged when it impacted terrain near Willard, Missouri. The pilot and four passengers were fatally injured. The aircraft was registered to and operated by JL2, LLC under the provisions of 14 Code of Federal Regulations Part 91 as a personal flight. Instrument meteorological conditions prevailed for the flight, which was operated on an instrument flight rules (IFR) flight plan. The flight originated from Lee's Summit Municipal Airport (LXT) about 2330 on September 14, 2012. The intended destination was the Springfield-Branson National Airport (SGF), Springfield, Missouri.
At 2338, the pilot contacted the Kansas City Terminal Radar Approach Control (TRACON) facility and requested an IFR clearance to SGF. The pilot was subsequently issued an IFR clearance and the flight proceeded on course to SGF. A cruising altitude of 7,000 feet mean sea level (msl) was assigned.
About 0002, control of the flight was transferred to the Springfield TRACON. The flight was about 50 miles north of SGF at that time. At 0014, air traffic control instructed the pilot to cross the initial approach fix (BVRLY intersection) at or above 3,000 feet msl, and cleared the pilot for an Instrument Landing System (ILS) approach to runway 14 at SGF. The flight was about 18 miles north of SGF. The pilot was instructed to contact the control tower at that time.
At 0017, the pilot contacted the SGF air traffic control tower. At that time, the tower controller cleared the pilot to land at that time. At 0020:31 (hhmm:ss), the pilot requested radar vectors in order to execute a second approach. The controller instructed the pilot to maintain 3,000 feet msl and turn left to a heading of 360 degrees. The pilot subsequently acknowledged the clearance. At 0021:17, the pilot contacted the controller and the controller acknowledged. At 0021:21, the pilot transmitted, "I need some help." No further communications were received from the pilot.
Radar track data depicted the accident airplane approaching SGF from the north-northwest on an approximate magnetic course of 157 degrees. After an en route descent, the airplane leveled at an altitude of 2,900 feet msl about 16 miles north-northwest of SGF. About 0018:00, the airplane flight path crossed the ILS runway 14 localizer near the initial approach fix (BVRLY intersection). The airplane drifted about 0.25 miles southwest of the localizer before crossing the localizer again, and drifting about 0.25 miles northeast of the localizer. Beginning about 0019:44, he airplane flight path appeared to parallel the localizer, about 0.12 miles northeast, for about the next 40 seconds.
The track data indicated that, about 0020:09, the airplane entered a left turn to become established on an approximate 064-degree magnetic course. About 0020:38, the airplane entered a second left turn that continued until the final radar data point, which was recorded at 0021:28. The final radar data point was located about 420 feet west-northwest of the accident site. The data indicated that the accident airplane descended from 2,800 feet msl at 0021:18 to 1,800 feet msl at 0021:28; an average descent rate of 6,000 feet per minute.
A witness reported hearing a low flying airplane prior to the accident. She noted the engine surged with high power about four times, followed by what sounded like a high speed dive. She stated that she heard the initial impact followed by an explosion. She observed the glow of the postimpact fire from her bedroom window. Her husband notified local authorities and they both responded to the accident site.
The airplane impacted an open area of a lightly wooded pasture located about 6 miles north-northwest of SGF. The elevation of the accident site was about 1,120 feet.
PERSONNEL INFORMATION
The pilot held a private pilot certificate with single-engine land airplane and instrument airplane ratings. He was issued a third class airman medical certificate without limitations on October 7, 2011. On the application for that medical certificate, the pilot reported a total flight time of 731.9 hours, with 97.2 hours flown within the preceding 6 months. The pilot's logbook was not available to the NTSB for review.
According to the pilot's flight instructor, the accident pilot had completed a flight review on January 23, 2012. The flight instructor estimated the pilot's total flight time at 1,000 hours, with about 75 hours of actual instrument time and 650 hours in Cirrus airplanes.
AIRCRAFT INFORMATION
The accident airplane was a 2002 Cirrus Design SR22, serial number 0202. It was a low wing, four place, single engine airplane, with a fixed tricycle landing gear configuration. The airplane was powered by a 310-horsepower Continental Motors IO-550-N reciprocating engine, serial number 686271. The accident airplane was issued a normal category, standard airworthiness certificate in April 2002.
The aircraft maintenance logbooks were not available to the NTSB for review. Maintenance work orders provided by a mechanic indicated that an annual inspection was completed on September 1, 2011, at 2,001 hours total airframe time. An engine oil change was accomplished on April 10, 2012 at 2,070 hours total airframe time.
A logbook that appeared to contain flights in the airplane was recovered at the accident site. The most recent entry was dated September 9, 2012. The entry included an ending airframe service time of 2,172.8 hours. The preceding entry, dated September 8, 2012, included a notation for a dual VHF Omni Range (VOR) equipment check that appeared to have been signed by the pilot. The log contained entries totaling 14.5 hours within the preceding 30 days, and about 70.3 hours within the preceding 90 days.
The airframe manufacturer stated that the accident airplane was equipped with four seats and four corresponding restraints (seatbelts/shoulder harnesses) at the time of manufacture. The manufacturer was not aware of any available modifications to increase the seating capacity of the airplane. The Federal Aviation Administration (FAA) Type Certificate Data Sheet applicable to the accident airplane noted a seating capacity of four. Aircraft records on file with the FAA did not include any modifications to the seating arrangement or occupant restraint systems.
METEOROLOGICAL CONDITIONS
Weather conditions recorded by the SGF Automated Surface Observing System, at 0020, were: wind from 070 degrees at 6 knots, 8 miles visibility, overcast clouds at 700 feet above ground level (agl), temperature 16 degrees Celsius, dew point 14 degrees Celsius, dew point 30.27 inches of mercury.
The area forecast current at the time of the accident noted overcast ceilings at 3,000 feet with cloud tops to 15,000 feet, and visibilities of 3 to 5 mile in light rain and mist. The terminal forecast for SGF current at the time of the accident noted overcast clouds at 300 feet agl with 6 miles visibility in mist and rain showers in the vicinity of the airport. An airman's meteorological information (AIRMET) advisory noted that IFR conditions were expected over southwestern Missouri, which included the accident site, with ceilings below 1,000 feet agl and visibility below 3 miles. There were no significant meteorological information (SIGMET), convective SIGMET, or weather watches in effect for Missouri at the time of the accident.
Civil twilight ended at 1948, with the moon setting at 1818. The moon was more than 15 degrees below the horizon at the time of the accident. The subsequent moonrise occurred at 0627, with the beginning of civil twilight at 0630.
There was no record of the pilot obtaining an official weather briefing from a flight service briefer; nor was there any record of weather information being accessed via the Direct User Access Terminal Service (DUATS). However, two IFR flight plans were filed through DUATS. An IFR flight plan from SGF to LXT was filed at 1604, and an IFR flight plan for the return flight from LXT to SGF was filed at 2257.
AIRPORT INFORMATION
The Springfield-Branson National Airport (SGF) was served by two paved runways. Runway 14 was 8,000 feet by 150 feet and constructed of grooved concrete. Approach and landing guidance to runway 14 consisted of an ILS approach procedure, a 4-light precision approach path indicator (PAPI), a medium intensity approach lighting system with runway alignment indicator lights (MALSR), and high intensity runway edge lights.
The ILS runway 14 approach procedure specified a minimum initial (glide slope intercept) altitude of 2,900 feet msl, with a 3.00-degree glide slope. The published decision height for a straight-in approach was 1,462 feet msl, with one-half mile visibility required for landing.
WRECKAGE AND IMPACT INFORMATION
The accident site was located in an open area of a lightly wooded pasture about 6 miles north-northwest of SGF. Linear ground impact marks consistent with being formed by the wing leading edges emanated from the main impact crater. Based on the ground impact markings, the airplane was oriented on an approximate heading of 340 degrees at the time of impact. The debris field extended to approximately 110 feet east, 140 feet northeast, and 70 feet north of the main impact crater. Significant portions of the airframe were consumed or damaged by a postimpact fire. Isolated areas of the surrounding vegetation were also affected by the postimpact fire.
The entire airframe was fragmented. The main impact crater contained the propeller, engine, instrument panel, and portions of the fuselage. The airplane flight control surfaces and wing flaps were located within the debris field. The ailerons and flaps had separated from the wings and were deformed consistent with impact forces. The aileron control cables were frayed and separated consistent with impact forces.
The empennage was separated from the airframe. It came to rest inverted about 10 feet east of the main impact crater. The elevator remained attached to the stabilizer and both appeared to be otherwise intact. The left horizontal and vertical stabilizers, left elevator, and rudder were consumed by the postimpact fire. A portion of the rudder remained attached to the lower rudder hinge. Elevator and rudder control continuity was confirmed between the empennage and the cockpit area.
The engine was located in the impact crater. It remained partially attached to the engine mount and airframe firewall. Portions of the firewall were deformed into/around the engine accessory section. The crankcase, cylinders, induction system, and exhaust system exhibited damage consistent with impact forces. All of the cylinders remained attached to the crankcase. The magnetos had separated from the engine and the ignition harness was damaged.
The three-bladed propeller assembly, with the propeller flange attached, separated from the engine. The engine crankshaft was fractured aft of the propeller flange. The appearance of the fracture surface was consistent with an overstress failure. One propeller blade had separated at the hub and was recovered from the impact crater. The remaining two propeller blades remained attached to the hub. The propeller blades exhibited S-bending and chordwise scratches.
The Cirrus Airframe Parachute System (CAPS) components remained attached to the airframe. The activation cable was continuous from the cockpit activation handle to the igniter assembly. The safety pin was not located with the activation handle consistent with it being removed prior to flight. The packed parachute assembly was located about 40 feet from the main impact crater. The parachute risers and suspension lines extended from the main impact crater to the parachute assembly and were oriented approximately perpendicular to the linear impact marks emanating from the main impact crater.
The postaccident examination of the airframe and engine did not reveal any anomalies consistent with a preimpact failure or malfunction.
MEDICAL AND PATHOLOGICAL INFORMATION
An autopsy of the pilot was conducted at the Boone/Callaway County Medical Examiner's Office, on September 17, 2012. The pilot's death was attributed to blunt trauma injuries sustained in the accident.
The FAA Civil Aerospace Medical Institute toxicology report was negative for all drugs in the screening profile. The report stated that 10 (mg/dL, mg/hg) ethanol was detected in blood samples. The report also noted that the ethanol was likely due to sources other than ingestion.
The pilot's loss of airplane control as a result of spatial disorientation experienced in night instrument meteorological conditions.