Crash location | 34.765000°N, 88.165278°W |
Nearest city | Iuka, MS
34.811757°N, 88.190042°W 3.5 miles away |
Tail number | N195AP |
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Accident date | 26 Jul 2015 |
Aircraft type | Cessna 195A |
Additional details: | None |
On July 26, 2015, at 1520 central daylight time, N195AP, a Cessna 195A, sustained substantial damage during a forced landing after a total loss of engine power on takeoff from the Iuka Airport (15M), Iuka, Mississippi. The airline transport pilot and the passenger sustained minor injuries. The airplane was registered to and operated by the pilot. A visual flight rules flight plan was field for the flight that was destined for Mesquite Metro Airport (HQZ), Mesquite, Texas. Visual meteorological conditions prevailed for the personal flight conducted under the provisions of 14 Code of Federal Regulations Part 91.
The pilot stated that he had landed at 15M and purchased 64 gallons of 100LL fuel. He then departed for Texas. The pilot said the takeoff was normal until he reached an altitude of about 600 to 800-ft above the ground. At that point, he looked down at his engine monitor and saw one of the EGT bars "drop." The pilot said the engine "felt a little rough" and he made an immediate turn back to the airport. Shortly after, the engine suddenly stopped producing power and the pilot made a forced landing to a narrow road adjacent to the airport. The airplane landed hard resulting in substantial damage to both wings, the firewall, and the right horizontal stabilizer. The landing gear and propeller were also damaged.
A postaccident examination of the airplane and engine revealed that the right-hand lower engine mount was broken in two places and the engine had pushed up and back causing the starter to be forced back thru the firewall. The fuel supply hose bushing that screwed into the inlet side of the engine driven fuel pump was also fractured at the back of the pump. The fuel pump was removed and the fuel pump drive was undamaged. Continuity was then established to the fuel drive by manual rotation of the propeller. An electric drill was then used to turn the engine driven fuel pump as fuel was poured into the pump. The pump forced fuel out of the pump as designed. The engine driven fuel pump was sent to the National Transportation Safety Board's Materials Lab and the fractured section of the supply hose bushing was examined. The examination revealed the brass bushing failed due to overload stresses and no pre-exisiting anomalies were noted.
The fuel servo was not damaged and a sample of fuel was taken from the main fuel supply. The sample was absent of water and debris. Continuity of the fuel selector valve was confirmed thru the left, right and off positions. The electric boost pump was tested and operated normally. The fuel line that would normally run to the inlet side of the engine driven fuel pump was then attached to the fuel servo and all but one of the fuel injector lines were disconnected. When the electric fuel boost pump was turned on, fuel spray was observed coming from each injector. The airframe fuel filter was removed and a small amount of water was observed in the bowl. A visual inspection of the spark plugs found no anomalies. The distributor was turned on and the engine was rotated with the starter and spark was observed on several leads. No mechanical discrepancies were observed that would have precluded normal operation of the engine.
The pilot held an airline transport pilot rating for airplane single and multi-engine land. He reported a total of 12,000 total flight hours, of which, 1,500 hours were in the accident airplane. The pilot's last Federal Aviation Administration second class medical was issued on July 14, 2014.
A total loss of engine power for reasons that could not be determined because a postaccident examination of the engine and fuel system found no mechanical anomalies that would have precluded normal operation.