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N2283M accident description

North Carolina map... North Carolina list
Crash location 34.127500°N, 78.339722°W
Reported location is a long distance from the NTSB's reported nearest city. This often means that the location has a typo, or is incorrect.
Nearest city Brunswick, NC
34.286836°N, 78.701127°W
23.4 miles away
Tail number N2283M
Accident date 10 Jun 2016
Aircraft type Wsk Pzl Mielec M 18A
Additional details: None

NTSB Factual Report

HISTORY OF FLIGHT

On June 10, 2016, about 0900 eastern daylight time, an experimental WSK PZL MIELEC M-18A, N2283M, was destroyed following an inflight separation of the right wing while maneuvering near Brunswick, North Carolina. The commercial pilot was fatally injured. Visual meteorological conditions prevailed, and no flight plan was filed for the aerial application flight, which was operated by Canam Aviators Inc., under the provisions of Title 14 Code of Federal Regulations Part 137. The flight originated from Bear Pen Airstrip (NC43), Supply, North Carolina, around 0845.

According to ground personnel, the airplane departed with a full load of fertilizer and 45 minutes of fuel with 30 minutes of reserve fuel. After 1 hour passed and the airplane did not return to the airport, ground personnel called 911 to report the airplane missing. The airplane was subsequently located in a wooded area.

PERSONNEL INFORMATION

According to Federal Aviation Administration (FAA) records, the pilot held a commercial pilot certificate with ratings for airplane single-engine land, airplane multiengine land, instrument airplane, and rotorcraft-helicopter. He also held an FAA second-class medical certificate, which was issued on May 13, 2016. At the time of the medical examination, the pilot reported 30,576 total hours of flight experience. The pilot's logbook was not recovered.

AIRCRAFT INFORMATION

The airplane was manufactured in 1994 and imported to the US, where it was issued a special airworthiness certificate in the restricted category. The accident operator purchased the airplane in 2003.

The most recent annual inspection was performed on January 15, 2016, at 8,567.9 hours total time in service. All of the inspection and maintenance entries from October 17, 2012, to the time of the accident were performed by the same company and mechanic. There were four annual inspections completed in this timeframe, and all entries specified that the inspections were conducted in accordance with the M-18 Service Manual. There was no specific information to indicate which of the published inspections from the manual were performed.

The airplane wing is composed of three sections; the center section and the right and left outboard sections. The outboard wing sections are connected to the center wing at three points each: two on the forward spar and one on the aft spar. The center section contains clevis fittings at the forward spar upper and lower spar caps and a clevis fitting at the aft spar. Corresponding lug fittings on the outboard wing sections fit into the center wing clevis fittings. The forward spar connections use an expansion mandrel installed through the bores of the center wing clevis and wing lug fittings. The aft spar connection uses a bolt installed through the bores of the center wing clevis and wing lug fittings.

An FAA inspector estimated that the takeoff weight was about 11,787 lbs, using an airplane empty weight of 5,975 lbs, chemical weight of 4,940 lbs (800 gallons), a fuel weight of 692 lbs (1.5 hours), and a pilot weight of 180 lbs.

AIRPLANE MODIFICATION AND MAINTENANCE HISTORY

The type certificate for the PZL M-18A was approved by the FAA in September 1987. The maximum weight was 9,260 lbs with a maximum hopper weight of 3,300 lbs regardless of the hopper capacity.

The original engine was removed from the accident airplane in April 1996 and replaced with a Honeywell TPE 331 turbine engine driving a Hartzell 3-blade, constant speed, reversing and feathering propeller in accordance with STC SA09039SC. Geared servo tabs were installed on the ailerons, elevators, and rudder in accordance with STC SA09063SC as part of the engine conversion. At the time of the modification, the airplane had accrued 997.0 hours total time in service. The airplane was again modified in January 2005, in accordance with STC SA09039SC, to install a different Honeywell TPE331 turbine engine driving a Hartzell 5-blade constant-speed reversing and feathering propeller. The airplane had accrued 5,153.7 hours total time in service at the time of this modification. The maximum weight approved as part of the STC was 9,260 lbs with the spray bar installed and 8,800 lbs with the spreader installed. A modified hopper was also installed at this time, which increased the hopper capacity to 800 gallons.

A logbook entry at an airframe time of 6,389.0 hours on June 21, 2006, indicated that the service life of the airplane was increased to 10,000 hours by incorporation of a manufacturer service bulletin. An entry on October 9, 2009, adjusted the total time in service of the airframe from 7,630 hours to 6,147 hours. The explanation provided in the entry indicated that the hour meter installed was recording incorrectly. On February 20, 2014, at an airframe time of 8,042.0 hours, a logbook entry documented the replacement of both left lower wing attach fittings and expanding mandrel in accordance with SB E/02.170/2000. On July 2, 2015, a logbook entry documented the replacement of the wing center section with a used serviceable unit with an estimated total time of 7,460 hours; the airframe time was 8,562.9 hours.

WRECKAGE INFORMATION

Examination of the wreckage by an FAA inspector revealed that the debris path was oriented from south to north. The wreckage area was compact except for the right wing and one propeller blade, which were located about 125 ft east of the main wreckage. The airplane impacted in a nose-down attitude of about 60°. The left wing was located on top of the engine and separated from the fuselage. The fuselage, cockpit, and hopper were found 10 ft north of the initial impact point. The remainder of the empennage was found 20 ft north of the cockpit. Small pieces of debris were found within a 50-ft radius of the initial impact point.

Further examination of the airplane by an NTSB investigator revealed that the right outboard wing forward spar lower fitting was fractured. Additionally, the right outboard aileron attach bracket was fractured, and visible cracks were evident on the right center and inboard aileron attach brackets. The fractured wing fitting, a fractured wing fitting attach bolt, and all three aileron attach brackets were sent to the NTSB Materials Laboratory Division in Washington, D.C. for analysis.

ADDITIONAL INFORMATION

Metallurgical Examination

The right outboard wing forward spar lower fitting fractured through the upper and lower arms in the areas indicated by arrows in figure 1. Each arm contained six vertical bolt holes used to attach the fitting to the outboard wing forward spar. The fracture in the upper arm intersected the inboard vertical bolt hole, and the fracture in the lower arm intersected the second vertical bolt hole from the inboard end. Bench binocular microscope of the fractured arms revealed all the fracture faces contained fatigue cracks that emanated from the bore of the holes on diametrically opposite sides of each hole, in the areas indicated by brackets "O" in figure 1.

Figure 2 shows a photograph of the lower arm fracture faces. The fatigue cracks in the lower arms initiated from multiple origins along the entire length of the bolt hole, in the areas indicated by brackets "O" in figure 2. Most of the fatigue crack origins were associated with corrosion pitting in the bore. Fatigue propagation on each side of the hole was through a 90% of the thickness and terminated in the areas indicated by dashed lines in figure 2.

Figure 3 shows a photograph of the upper arm fracture faces. The upper arm fractures contained similar fatigue cracks with the exception that the fatigue cracks initiated from multiple origins near the lower portion of the bolt hole. Most of the fatigue crack origins were associated with corrosion pitting in the bore. The fatigue cracks in the upper arms exhibited better defined fatigue fracture features than those on the lower arms.

The fractured bolt examined was installed through the third vertical bolt hole in the right outboard wing forward spar lower fitting. The fracture intersected the root thread portion of the bolt. The fracture face of the bolt contained fatigue cracks that emanated from multiple origins all around the root portion. Fatigue propagation was toward the center of the bolt and extended through about 95% of the bolt cross section.

Figure 4 shows a photograph of the right outboard aileron attach bracket, which contained a circumferential fracture in the main tube portion, near the location where the two upper arms were welded to the main tube. The fracture intersected the aft edges of the welds at the base of the two arms, indicated by arrows "X" in figures 4. Bench binocular microscope examination of the forward face of the main tube fracture revealed multiple fatigue cracks that emanated from the outer surface of the main tube at the aft edges of the welds. Fatigue propagation was through about 50% of the thickness and extended around about 30% of the tube circumference. Corrosion was noted on the outboard tube surface.

The right center and inboard aileron attach brackets were intact, but both brackets contained visible cracks in the white paint layer where the two upper arms were welded to the main tube. The paint was removed with a commercial paint stripper from the weld areas of the intact brackets. Bench binocular microscope examination of both intact brackets after paint stripping revealed the presence of corrosion and intermittent cracks on the outer surface of the welds in the same respective location as the fracture on the outboard bracket. The cracks were not opened, but examination of the inner face of the main tube portion for both intact brackets revealed the intermittent cracks did not extend through the thickness.

Manufacturer Information

The PZL M18 Description and Service Manual provides procedures for maintaining and inspecting the airplane, including procedures for corrosion prevention and control; particular emphasis was placed on the cleaning of the airplane, with the statement that "regular and thorough cleaning of both the interior and exterior of the aircraft is a major part of corrosion control." The instructions for cleaning included the statement, "particular attention should be given to wing fittings." In addition, the manual provides instructions for non-destructive inspection of airframe structural fittings, with specific details for the wing fittings and anti-corrosion protection of the wing fittings. The manual also includes a maintenance schedule that contains procedures for verifying inspections every 3,000 flight hours, and periodic inspections at 50, 100 and 500 flight hours. The manual calls for a mandatory annual inspection within the scope of the 500-hour inspection and special verifying inspections each 3,000 hours of operation.

According to the PZL M18 Aircraft Repair Manual, the airframe has a service life of 10,000 flight hours. The left aft center-wing-to-fuselage attach fitting has a service life of 3,000 flight hours. The manual also defines an "Airframe Service Life in Overload Version." The original airframe service life was calculated for a takeoff weight of 10,340 lbs. There are procedures to increase the takeoff weight to 11,700 lbs, which, according to the manual, "causes higher fatigue wear and drop of service life by 1.35 times." For all operations performed above the standard weight of 10,340 lbs, the operator should multiply the flight hours by 1.35 to obtain the proper flight hours for calculating the service life of the airplane.

The manufacturer issued Service Bulletin (SB) E/02.159/97 in 1997 to provide instructions for corrosion protection of the outboard wing forward spar fittings as a result of findings on four airplanes that were operated in Greece. The bulletin provides instructions for inspection of the fitting arms where they attach to the forward spar, removal of any corrosion within limits, and protection of the fittings by application of a corrosion inhibiting compound. The bulletin also provides instructions for adding an inspection panel in the lower leading edge of the outboard wing to improve access to the outboard wing forward spar fittings. The accident airplane did not have the inspection panel specified by this SB.

The manufacturer issued SB E/02.170/2000 in August 2000 to provide instructions for inspection of the wing attach joints as a result of two accidents in the United States. The accidents were caused by corrosion in the lower wing attach fittings that resulted in fatigue cracking and failure of a fitting lug. The SB provides instructions for inspection of the wing fittings for corrosion in the lug bore and on the exterior surface of the fittings, repair of minor corrosion, inspection for ovalization of the lug holes, and magnetic particle inspection of the fitting lugs for cracks. The procedures do not require removal of the outboard wings but do require removal of the expansion mandrels. Procedures are also provided for replacement of the wing fittings, if necessary, with the recommendation that both left and right pairs of lower wing fittings should be replaced, even if only one pair has damage beyond limits. There are no specific procedures for inspection of the vertical holes where the fittings attach to the spar. The provisions of this SB were subsequently mandated by airworthiness directive (AD) 2000-18-12. The manufacturer issued Service Letter M18/034/2016 in February 2016 with instructions that only the magnetic particle inspection method is applicable for the SB and suggesting that the wings be removed from the airplane to better perform the inspection.

In January 2001, the manufacturer issued SB E/02.172/2001 to provide guidelines for increasing the service life of the airframe up to 10,000 flight hours for airplanes S/N 1Z001-01 through S/N 1Z028-01, which included the accident airplane. The SB instructed operators to perform the 3,000-hour special inspection in the Service Manual with particular attention paid to incorporation of all applicable mandatory bulletins on the airplane and corrosion, cracks and wear in the outboard wing-to-center wing attach fittings.

There are two published Airplane Flight Manuals (AFM) for the airplane: a European Aviation Safety Agency (EASA)-approved version for those airplanes operating outside the United States, and an FAA-approved version. The EASA-approved AFM is used by other airworthiness authorities around the world, and provides for the operation of the airplane at increased gross weights up to 11,700 lbs, with the stipulation that a service life factor of 1.35 be applied for those flights above 10,340 lbs.

The FAA-approved AFM specifies that the airplane is certificated in the restricted category for agricultural operations and dispensing fire-fighting materials. The limitations specify a maximum takeoff and landing weight of 9,260 lbs, a maximum hopper load of 3,300 lbs, a never exceed speed of 151 knots, a maximum cruising speed of 124 knots, maneuvering load factors of +3.4g and -1.4g, and prohibits operational flights with a person in the mechanic's seat. The FAA AFM does not specify a service life factor since the airplane is certificated at a gross weight of 9,260 lbs.

FAA Information

In September 2000, the FAA issued Airworthiness Directive (AD) 2000-18-12 to address corrosion and cracking of the wing attach fittings on all PZL M-18, M-18A, and M-18B airplanes as a result of two wing separation accidents. The AD required that operators inspect the center wing-to-outboard wing attach joints for cracks in the lugs, corrosion in the main holes, and ovalization of the main holes every 1 year or 500 hours time in service (whichever occurs first), repair corrosion and apply anti-corrosion protection, replace the wing attach joints as necessary, and eliminate any ovalization of the wing main joint holes. The AD specified that the inspection of the main holes must be done using magnetic particle methods and all other procedures were to be in accordance with manufacturer SB E/02.170/2000. The procedures published in the SB and AD were focused on the main attach lug and clevis on the wing fittings and did not specifically address the vertical bolt holes where the fi

NTSB Probable Cause

The failure of the right wing due to a fatigue fracture of the right outboard wing forward spar lower fitting. Contributing to the accident was the routine operation of the airplane over its certificated maximum gross weight and the operator's improper or inadequate maintenance practices, which failed to apply a service life factor to the airplane to account for its overweight operation and also failed to detect the extensive corrosion throughout the airplane.

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