Crash location | 35.660833°N, 80.789444°W |
Nearest city | Mooresville, NC
35.584860°N, 80.810072°W 5.4 miles away |
Tail number | N2383C |
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Accident date | 29 Mar 2017 |
Aircraft type | Cessna R182 |
Additional details: | None |
On March 29, 2017, about 1325 eastern daylight time, a privately owned and operated Cessna R182, N2383C, was substantially damaged when it impacted a fence while attempting to depart from Atwell Airport (1NC2), Mooresville, North Carolina. The private pilot and passenger were not injured. The flight was destined for Riley Creek Airport (12TN), Kingston, Tennessee. Visual meteorological conditions prevailed, and no flight plan was filed for the personal flight, which was conducted under the provisions of 14 Code of Federal Regulations Part 91.
According to the pilot, the airplane was last flown in November 2016. On the morning of the accident, he moved the airplane out of the hangar, washed it, and performed a preflight inspection following the published manufacturer's checklist. He indicated that he was particularly careful checking for bird nests or other hazards, because the airplane had not been flown in 4 months. He found the airplane to be in good condition with no issues. He then went to a business meeting and returned to the airplane that afternoon, inspected it again, and found no discrepancies. He and his passenger boarded the airplane with a few personal items, and no baggage. After removing and stowing the gust lock, he started the engine without difficulty. He let it warm up for several minutes, then proceeded to back taxi on the turf runway to the beginning of runway 36 for a takeoff to the north.
Prior to takeoff, the pilot performed an engine run-up which he described as "everything seemed normal, the engine sounded fine." During the takeoff roll, as the airplane reached a point on the runway where it would normally lift off (about 1,200 ft down the runway), he pulled back on the yoke, and the airplane "didn't want to fly." He recalled that the airspeed at that time was "close to 60 knots." He did not recall any engine instrument indications and noted that the engine sounded "normal." Once he realized that the airplane was not going to take off and a collision appeared imminent, he advised his passenger to prepare for impact. As the airplane approached a fence just beyond the departure end of the runway, he pulled back on the yoke and the airplane lifted off, flew over the fence, then descended and struck another fence before coming to rest in the driveway of his residence. The pilot then turned off the master switch and the fuel selector. After the accident he noticed that the flaps were in the "up" position but recalled that they were "down" when he started the takeoff roll.
The turf runway at 1NC2 was 1,700 feet-long by 60 feet-wide and was located at an elevation of 830 feet mean sea level (msl). The pilot reported that the turf had recently been mowed and the grass was "very short."
Examination of the airplane by a Federal Aviation Administrator (FAA) inspector revealed that the right wing was crushed and bent aft, outboard of the wing strut. The right aileron and flap were damaged. The left wing was crushed aft near its root. The outboard section of the right horizontal stabilizer sustained impact damage consistent with striking a fence post, the right elevator balance horn was fractured and nearly separated from the elevator. The firewall and forward fuselage were buckled.
Examination of the engine by a National Transportation Safety Board investigator revealed that the two-bladed propeller remained attached to the crankshaft. One blade exhibited an s-bend and was twisted. The other blade was bent aft about 50º. Both blade surfaces exhibited chordwise scratching signatures. The carburetor was attached at the mount pad; the intake system remained partially attached to the carburetor. The intake was clear of obstructions or debris. The carburetor was removed and partially disassembled. The finger screen was absent of debris and the single plastic float was intact. The carburetor bowl contained about 2 oz. of clean, blue-colored fuel, with no water or contaminants noted. The accelerator pump was operated manually and pumped fuel from the outlet line. The fuel gascolator was also examined. The bowl was removed and contained about 2 oz. of clean, blue-colored fuel with no water or contaminants noted.
The six top spark plugs were removed for examination. The fine-wire electrodes were normal in wear and when compared to a Champion Check-A-Plug chart. The Nos. 1, 3, and 6 electrodes had surface rust on the circumferences. The Nos. 2 and 5 electrodes were dark gray in color. The other plugs exhibited gray color. The cylinder rocker covers were removed for the examination. The crankshaft was rotated by hand-turning the propeller. Compression and suction were observed on the Nos. 2, 4, 3, and 5 cylinders, and valve action was correct on all cylinders. The No. 5 cylinder pushrods were impact damaged. The Nos. 1 and 6 cylinders were examined using a lighted borescope; no anomalies were noted other than scoring on the cylinder walls. The ignition harness leads were damaged and/or severed by impact forces. The dual magneto remained attached at the mount pad. The magneto produced spark on all leads when the crankshaft was rotated manually.
According FAA records, the pilot held a private pilot certificate with ratings for airplane single-engine land and instrument airplane. His most recent FAA third-class medical certificate was issued October 28, 2015. A review of the pilot's logbook revealed that he had accrued 986 total hours of flight experience, of which 90 hours were in the accident airplane, as of January 16, 2017.
Review of the airplane's maintenance records revealed that the most recent annual inspection was completed on September 10, 2016, about 19 flight hours prior to the accident. The engine had accrued 1,822 hours since new.
At 1320, the reported weather at Statesville Municipal Airport (SVH), Statesville, North Carolina, about 10 nautical miles northwest of the accident site included wind from 080° at 5 knots, the temperature was 22° C, and the dew point was 11° C.
The pilot reported that the gross weight of the airplane at the time of the accident was 2,727 lbs. Review of takeoff performance data in a pilot operating handbook for the make and model airplane revealed that at a gross weight of 2,800 lbs, at 20°C, at 1,000 feet msl pressure altitude, the airplane required a ground roll of about 840 ft for a turf runway The data assumed the flaps were set to 20° extension.
An electronic engine monitor was retained and forwarded to the National Transportation Safety Board Vehicle Recorder Laboratory, Washington, DC. Review of downloaded data revealed that the accident takeoff was not recorded.