Crash location | 35.008611°N, 80.368611°W |
Nearest city | Marshville, NC
34.988486°N, 80.367008°W 1.4 miles away |
Tail number | N61WB |
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Accident date | 18 Feb 2016 |
Aircraft type | Beech A36 |
Additional details: | None |
HISTORY OF FLIGHT
On February 18, 2016, about 1910 eastern standard time, a Beech A36, N61WB, made a forced landing after a total loss of engine power near Marshville, North Carolina. The airline transport rated pilot was fatally injured. The airplane was substantially damaged. The airplane was registered to and operated by Indigo Air LLC as a 14 Code of Federal Regulations Part 91 business flight. Night visual meteorological conditions existed near the accident site at the time of the accident, and the flight was operated on an instrument flight rules flight plan. The flight originated at Daytona Beach International Airport (DAB), Daytona Beach, Florida, about 1554, and was destined for Davidson County Airport (EXX), Lexington, North Carolina.
According to a representative of the operator, the pilot flew part-time for Indigo Air LLC. The flight originated earlier that day from EXX, where the airplane was based, and departed with full fuel (80 gallons total, 74 usable). The pilot flew to Piedmont-Triad International Airport (GSO), Greensboro, North Carolina, picked up the company's owner and a passenger, then flew direct to DAB. No fuel was purchased at GSO. At DAB, the pilot parked the airplane at a fixed-base operator (FBO). According to the owner, the pilot told him he was "going to put 15 [gallons of fuel] in a side." The owner went inside the FBO, paid for the fuel, and left because he "was in a rush." The lineman that fueled the airplane stated that the bladder tanks were "bulging" out of the fuel port on each tank. When the lineman, along with the FBO's safety director, pointed out the bulging tanks to the pilot, the pilot touched the bladder, then told the lineman it was okay to fuel. The FBO fueling records indicated that 30 gallons of 100LL fuel were purchased and distributed evenly between the two tanks. The flight then departed for EXX.
About 3 hours into the flight, while at a cruise altitude of 5,000 ft mean sea level, about 50 miles south of EXX, the pilot reported a loss of engine power to air traffic control and requested vectors to the nearest airport. The pilot subsequently made a forced landing about 10.5 miles east-northeast of Charlotte Executive Airport (EQY), Monroe, North Carolina. A witness, who was located about 3.5 miles east of the accident site, stated that he was in his shop when he heard the airplane. He said the engine was cutting in and out like it "ran out of gas." The witness went outside and saw the airplane in level flight about 1,000 to 1,500 ft above the ground. The airplane's landing light and navigation lights were turned on. He said the pilot tried to start the engine 4 or 5 times, but the engine would only start and run for a few seconds, then quit. On the last attempt, the engine started, and it sounded like the pilot pulled the throttle to idle. The witness watched as the airplane descended "in a gradual glide" before it disappeared from view.
PILOT INFORMATION
The pilot held an airline transport pilot certificate with a rating for airplane multiengine land, and a commercial pilot certificate with ratings for airplane single-engine land and instrument airplane. He also held numerous corporate jet type ratings. His last Federal Aviation Administration (FAA) second-class medical certificate was issued on October 13, 2015, with a restriction to wear corrective lenses. At that time, he reported a total of 17,000 flight hours. The pilot's logbooks were not located.
AIRCRAFT INFORMATION
The airplane was a single-engine, 6-seat, low-wing airplane, equipped with a Continental Motors Inc. IO-520-BB, 6-cylinder engine. The engine was equipped with a three-blade Hartzell constant-speed propeller.
The most recent annual inspection was conducted on May 15, 2015, at a total tachometer time of 1,843.60 hours.
A review of the airplane's flight and refueling history revealed that the pilot landed in DAB with about 15 gallons of total of fuel. With the fuel added at DAB about 45 gallons was onboard at the time of departure. According to the airplane's Pilot Operating Handbook, the IO-520-BB engine burned about 15.2 gallons per hour, not including taxi, takeoff and climb.
METEOROLOGICAL INFORMATION
The 1853 weather observation at Charlotte Executive Airport (EQY), Monroe, North Carolina, included clear skies, visibility 10 miles, and wind 030° at 5 knots. The temperature was 9°C, dewpoint -2°C, and the altimeter setting was 30.43 inches of mercury.
WRECKAGE INFORMATION
The airplane came to rest upright in wooded area behind a private residence on a heading of 180° magnetic. There was no postimpact fire. Examination of the wreckage revealed that the airplane initially collided with a stand of about 60-ft-tall trees in a left-wing-low attitude and traveled about 134 ft to where it came to rest in a nose low, slightly tail-high attitude. The landing gear and flaps were fully retracted. The firewall, leading edges of both wings, a propeller blade, and the leading edge of the right horizontal stabilizer were damaged. Pieces of the windscreen were dispersed just forward of the engine. The throttle, mixture, and propeller controls were all full forward.
Examination of the airplane's fuel system revealed the fuel selector handle was set to the right tank. A visual examination inside each fuel tank revealed there was a small amount of fuel in each bladder. When electrical power was applied to the airplane, the left and right fuel gauges each indicated about 1/8 full. The remaining fuel was then drained from each fuel tank; just under 1 quart of fuel was drained from each. The fuel was absent of debris and water. The bladder tanks were inspected, and no breaches were observed; however, neither bladder tank was properly seated and they were pushing up on their respective fuel sensor.
There was no fuel staining observed on the airplane. The main fuel line to the fuel pump was removed, and no fuel was found in the line. Air was blown back through the line into each fuel tank and no obstructions were noted. The fuel pump was removed and rotated and no fuel was observed in the pump. The top of the fuel manifold was disassembled, and a small amount of fuel was noted in the manifold chamber. About 2 ounces of 100LL fuel was drained from the airframe fuel filter and the fuel was absent of debris and water. The fuel strainer screen exhibited some light corrosion, but no debris was observed.
Flight control continuity was established for all flight control surfaces. Examination of the airframe revealed no anomalies that would have precluded normal operation.
The propeller remained attached to the engine crankshaft propeller flange. The crankshaft flange appeared to be undamaged and no ladder cracking was noted. Two of the three propeller blades were undamaged, and the third propeller blade was bent rearward about 90°.
The engine was removed from the airframe and an initial examination was performed. The top spark plugs were removed and inspected. When compared to a Champion Spark Plug "Check A Plug" chart, the spark plugs appeared to be "normal" with light coloration signatures. The engine was rotated manually via the propeller; thumb compression was verified for each cylinder and spark was produced to each spark plug ignition lead. A lighted borescope inspection on each cylinder revealed that all valves were intact and exhibited normal combustion signatures.
The engine was placed on a test stand for an operational check. The engine ran through all power settings with no abnormalities. There were no mechanical discrepancies that would have precluded normal operation before the accident.
A handheld Garmin 496 GPS unit was found in the wreckage; however, the accident flight was not captured.
MEDICAL INFORMATION
Examination of the pilot's lap belt and shoulder harness assembly revealed that it remained intact, but was found unbuckled with the shoulder harness not attached. The pilot's lap belt shoulder harness attachment post elastic grommet was not installed (or found in the wreckage), and, when manually assembled, the shoulder harness attachment buckle would not seat securely to the lap belt attachment post.
According to the death investigator's notes, the pilot was found deceased, slumped over in the left seat, still wearing his seatbelt. Although the airplane was equipped with a single shoulder harness (across the left shoulder), injuries sustained by the pilot were consistent with the pilot not being restrained by the shoulder harness at the time of the impact.
According to the autopsy performed by the Mecklenburg County Medical Examiner's Office, the cause of death was blunt force injuries due to airplane crash and the manner of death was accident. No significant natural disease was identified. The pilot's injuries included contusions and abrasions of the face, fractured teeth, contusions, abrasions, and fractures of the torso, disruption of the proximal descending aorta with massive left hemothorax.
At his last FAA medical, the pilot reported hypertension and high cholesterol and was being treated with doxazosin (also called Cardura) and simvastatin (also called Zocor), respectively. Toxicological analysis was conducted by the FAA's Bioaeronautical Sciences Research Laboratory, Oklahoma City, Oklahoma. The tests were positive for doxazosin in blood and urine. Doxazosin is not considered to be an impairing medication.
The pilot's improper preflight fuel planning, which resulted in a total loss of engine power due to fuel exhaustion. Contributing to the severity of the pilot's injuries was his failure to have a properly secured shoulder harness at the time of the accident.