Crash location | 40.850000°N, 74.060833°W |
Nearest city | Teterboro, NJ
40.859822°N, 74.059308°W 0.7 miles away |
Tail number | N703TS |
---|---|
Accident date | 08 Mar 2005 |
Aircraft type | British Aerospace BAE-125-700A |
Additional details: | None |
On March 8, 2005, at 2150 eastern standard time, a British Aerospace BAE-125-700A (Hawker 700), N703TS, sustained minor damage during an overrun, while landing at Teterboro Airport (TEB), Teterboro, New Jersey. The two certificated airline transport pilots and two passengers were not injured. Night visual meteorological conditions prevailed for the flight that departed Port Columbus International Airport (CMH), Columbus, Ohio. An instrument flight rules flight plan was filed for the personal flight conducted under 14 CFR Part 91.
The airplane was manufactured in 1978, and was not equipped with thrust reversers. The pilot reported that prior to the day of the accident, he and the copilot had not flown together. The pilot further stated that the copilot spoke broken English.
A notice to airmen (NOTAM) was issued at 1900 for Teterboro Airport, and valid for the remainder of the day. The NOTAM stated that runway 1/19 was liquid deiced 75 feet wide, and sanded/solid deiced 20 feet wide. The runway contained patchy wet snow and patchy thin ice.
Prior to departure, the pilot received a weather briefing about 1900 via a commercial weather service. The pilot retrieved the NOTAMs for TEB, but the NOTAM that was issued at 1900 was not included. The pilot further stated that the incident flight was delayed about 45 minutes due to a discrepancy with the auxiliary power unit, and it was possible that the pilot obtained the weather briefing prior to the NOTAM being issued.
According to the pilot's written statement, the departure was uneventful and the copilot obtained the most recent automated terminal information system (ATIS) information about 150 miles from TEB. The cockpit voice recorder (CVR) recorded approximately 33 minutes of data prior to the incident. Review of the CVR revealed that the copilot obtained the current ATIS information, and relayed some of the information to the pilot. However, the copilot did not relay information about the runway conditions to the pilot, nor did the pilot ask about the runway conditions. The ATIS information "Uniform" was in effect at 2051, and received by the copilot. The ATIS reported the wind from 320 degrees at 21 knots, gusting to 28 knots; visibility 10 miles, blowing snow; broken ceiling at 11,000 feet; temperature -7 degrees C; dew point -16 degrees C; altimeter 29.38 inches Hg; thin slush on all surfaces; low level wind shear advisories in effect; braking action advisories in effect; Deicing procedures in effect.
During the approach to the airport, the pilot instructed the copilot to select 15 degrees of flap extension, about 30 miles from the airport. After a landing check was completed and the landing gear was extended, the pilot instructed the copilot to select 25 degrees of flap extension. At that time, the airplane was on a right downwind leg for runway 1; a 7,000-foot-long, 150-foot-wide, asphalt runway.
The pilot's written statement referred to the turbulence as moderate during the approach; however, during a telephone interview, the pilot stated that it was the worst turbulence of his 34-year flying career. Radio communications were "very impaired" due to the turbulence, and the flightcrew missed several transmissions from air traffic control (ATC).
The pilot continued the approach, and requested a wind check from ATC. According to the pilot's written statement, ATC replied "wind 320 degrees at 27 gusting to 38." Due to the wind, the pilot did not select full flap extension on final approach, and flew the final approach at Vref (119 knots) plus 20 knots to compensate for the wind. The pilot further stated that the airspeed was slowed to Vref plus 15 knots over the runway threshold. A touchdown was made "at or no farther than 25 feet northeast of the touchdown zone," at Vref plus 10 knots, and the pilot instructed the copilot to extend full flaps.
The pilot then selected the airbrake to "Dump," and felt the airplane slowing as if the spoilers were working correctly. He was focused on runway alignment and did not divert his attention to look down at the airbrake lever. The pilot further stated that the airbrake lever could not be positioned to "Dump" unless the full flap extension was already selected. The pilot also felt the anti-skid braking system working correctly. However, about the midpoint of the runway, he felt like the airplane encountered a tailwind or ice on the runway, as it did not continue to decelerate. The airplane traveled off the end of the runway at approximately 30 knots.
After the overrun, the pilot started to "clean up" the airplane by retracting the flaps and moving the airbrake toward closed. The first officer interrupted him and suggested an evacuation.
The copilot's written statement was consistent with the pilot's statement. However, the statements differed as the copilot reported that the airplane touched down "Vref plus 15 knots, at or no farther than 125 feet northeast of the touchdown zone."
The pilot later heard that a Gulfstream G-III, on approach ahead of the incident airplane, had performed a go-around due to turbulence. The pilot was not aware of the Gulfstream G-III go-around during his approach.
Review of the ATC communications revealed that the flightcrew was provided two wind checks during final approach. The wind checks were reported as from 340 degrees at 15 knots, and then 340 degrees at 20 knots. A Challenger flightcrew reported the braking action as "fair to good" about 20 minutes before the incident. Just prior to the incident, the Gulfstream G-III flightcrew reported the braking action as "good, but not quite as good at the end." The Challenger and Gulfstream were equipped with thrust reversers. The "good" braking action reported by the Gulfstream G-III flightcrew was relayed to the incident flightcrew by ATC.
Review of the CVR revealed that the flightcrew missed the transmission of the Gulfstream III flightcrew performing their second go-around. The incident flightcrew also missed the initial "good" braking action report by the Gulfstream III flightcrew, but they subsequently received the relayed report from ATC. In addition, a sound consistent with the incident airplane's touchdown was recorded, and a sound consistent with runway overrun was recorded approximately 20 seconds later.
Review of radar data revealed that the last radar target was recorded at 2150:23. The target indicated that the incident airplane was at an altitude of 100 feet, about 500 feet prior to the runway threshold. The groundspeed recorded was 138 knots, which revealed a true airspeed of approximately 157 knots (Vref plus 38 knots) based on the last wind check.
According to the Aeronautical Information Manual Pilot/Controller Glossary, a contaminated runway, "is considered contaminated whenever standing water, ice, snow, slush, frost in any form, heavy rubber or other substances are present."
Review of an "Effect of Slippery Runway on Landing Distance" chart, available in the FAA approved airplane flight manual, revealed that the "equivalent scheduled landing distance available," for the contaminated 7,000-foot-long runway, was approximately 3,200 feet.
Review of a takeoff and landing data (TOLD) card retrieved from the cockpit revealed that a landing weight of 20,000 pounds, with full flaps extended, at 119 knots, required 4,240 feet of runway for landing. That data assumed a dry runway.
According to the Aeronautical Information Manual, Section 4-3-9; Runway Friction Reports And Advisories:
"...MU (friction) values range from 0 to 100 where zero is the lowest friction value and 100 is the maximum friction value obtainable. For frozen contaminants on runway surfaces, a MU value of 40 or less is the level where the aircraft braking performance starts to deteriorate and directional control begins to be less responsive. The lower the MU value, the less effective braking performance becomes and the more difficult directional control becomes...."
A friction reading was taken at 22:01, about 11 minutes after the accident. The reading was taken from 500 feet beyond the approach end of runway 1, to 500 feet prior to the departure end of runway 1. The average MU value for the first one-third segment of the runway was 35. The average MU value for the second one-third segment of runway was 42, and the average MU value for the remaining one-third segment of runway was 41. The overall average MU value for the runway was 40.
The airplane came to rest approximately 230 feet beyond the departure end of runway 1. The spoilers were found in the extended position, and the flaps were found in the retracted position. Minor damage was observed on the landing gear. No damage was observed on the flaps, consistent with them being raised prior to the overrun.
The recorded weather at TEB, at 2151, was: wind from 320 degrees at 12 knots, gusting to 28 knots, with a peak wind at 320 degrees at 38 knots; visibility 10 miles; broken ceiling at 11,000 feet; temperature 19 degrees F; dew point 3 degrees F; altimeter 29.38 inches Hg.
The pilot in command's inadequate in-flight planning, which resulted in an overrun landing on a contaminated runway. Factors were inadequate crew coordination, gusty winds, and a slush covered runway.