Crash location | 36.196944°N, 115.182500°W |
Nearest city | North Las Vegas, NV
36.198859°N, 115.117501°W 3.6 miles away |
Tail number | N415MK |
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Accident date | 22 Aug 2008 |
Aircraft type | Killgore Velocity |
Additional details: | None |
HISTORY OF FLIGHT
On August 22, 2008, at 0628 Pacific daylight time, an experimental Killgore Velocity 173RG, N415MK, collided with a residential building after takeoff in North Las Vegas, Nevada. The airplane was registered to the owner/builder, and was being operated by the pilot under the provisions of 14 Code of Federal Regulations Part 91. The certificated airline transport pilot and two people on the ground were killed. Post impact fire destroyed the airplane and partially burned the residence. The local flight departed North Las Vegas Airport (VGT) at 0627. Visual meteorological conditions prevailed, and no flight plan had been filed.
Review of voice communications provided by the Federal Aviation Administration (FAA) revealed that the pilot initially made contact with VGT Air Traffic Control (ATC) and requested to taxi the airplane to the active runway. The ground controller asked the pilot to indicate his direction of flight and confirm that he had the current automatic terminal information service (ATIS) information. The pilot responded, stating that he would be staying within the airport traffic pattern. The ground controller proceeded to give the pilot taxi instructions to the hold short line of runway 7. Once at the hold short line the pilot switched to the tower frequency and established communications with the tower controller.
The pilot then requested, "I would like to do a take off, we're ready for takeoff 12 right we'd like to stay in the pattern and right traffic." The controller then gave the pilot taxi instructions to runway 12 right. The pilot proceeded to taxi the airplane to the runway, and during the taxi sequence, the controller cleared the pilot to takeoff and fly in a right-hand traffic pattern.
The airplane then began its takeoff roll and departed. About 1 minute 30 seconds later, the tower controller asked the pilot if he needed any assistance to which the pilot responded, "I'm going in, I'm going in, I'm going in."
The ATC ground and tower controllers reported similar observations of the airplane as it departed the airfield. They stated that after takeoff the airplane appeared to be flying lower than they expected, and not gaining altitude. Both controllers then observed the airplane descend into the residential area.
The airplane collided with a residence 1.1 miles beyond the departure end of runway 12 right. Radar data provided by the FAA indicated that the airplane reached a maximum altitude of about 300 feet above ground level (agl) and continued for approximately 30 seconds before descending into the residence.
PERSONNEL INFORMATION
The pilot, age 76, held an airline transport pilot certificate and a flight instructor certificate both with ratings for airplane single-engine land, multiengine land, and instrument airplane. He additionally held a flight engineer certificate, and a mechanic certificate with ratings for airframe and powerplant.
He held a third-class airman medical certificate issued in September 7, 2006, with the limitation that he must wear lenses for near and distant vision.
The pilot's logbook was not recovered for inspection. On his latest FAA medical application he stated that he had amassed 6,250 hours of total flight time.
FAA records indicated that the pilot owned a Velocity Elite XL airplane.
The owner/builder reported that this was the first time the pilot had flown the accident airplane. He stated that the pilot had assisted him with readying the airplane throughout the certification and flight testing process.
AIRPLANE INFORMATION
The canard configuration, four-seat, retractable gear airplane, was issued a Special Airworthiness Certificate by a Designated Airworthiness Representative (DAR) on March 9, 2008. It was powered by a four-cylinder Lycoming IO-360-C1C engine, and equipped with an MT 3-blade wood/composite electrically controlled constant speed propeller; hub model number: MTV-18-B; blade model number: LD168-101B.
Review of the engine logbooks revealed that Textron Lycoming had overhauled the engine in April 1994, 5.1 flight hours prior to the accident. At the time of the overhaul the engine had accrued 3,156.07 hours of total time. The owner/builder stated that the engine had been preserved and kept in storage until installation on the airplane in 2007. Engine records revealed that the pilot had reviewed the Airworthiness Directive (AD) compliance records for the airplane on April 7, 2008.
The owner/builder modified the engine by installing both an uncertified Aero Supercharger Solutions supercharger, and an uncertified Light Speed Engineering (LSE) PLASMA II Plus capacitive discharge ignition system. A conventional magneto remained installed on the right magneto pad. Ignition timing for the LSE ignition system was governed by a Hall Effect module mounted on the left magneto pad.
The supercharger system consisted of an automotive, belt driven, centrifugal type, Vortech Engineering supercharger, model V-1.
According to the owner/builder, the engine boost control pressure was regulated by a butterfly valve located inside the inlet plenum of the supercharger compressor. The pilot controlled the position of the butterfly valve through a push/pull control cable, which terminated at the throttle quadrant. The push/pull cable was configured such that the full forward position corresponded to the butterfly valve being completely open. The diameter of the butterfly valve was constructed to be smaller than the diameter of the inlet plenum. The builder stated that this size difference allowed air to continue to be supplied into the induction system when the butterfly valve was closed.
Additionally an altitude compensating relief valve was fitted to the supercharger outlet manifold, ahead of the fuel injector servo inlet. The supercharger manufacturer stated that this valve was designed to prevent engine inlet manifold pressure from exceeding 32 inches of mercury (inHg).
The supercharger housing contained a gearbox, which drove a forward facing impeller. An automotive type pulley was mounted to the gearbox input shaft. A larger pulley was affixed to the engine crankshaft, and rotational energy was transferred between the pulleys through a ribbed automotive drive belt. Drive belt tension was maintained by the use of an idler pulley, which was attached to the supercharger housing by an idler pulley adjustment plate.
The owner/builder stated that the supercharger and electronic ignition system were already installed on the airplane at the time it was issued the special airworthiness certificate.
Weight and Balance
The National Transportation Safety Board investigator-in-charge (IIC) reviewed the airplane weight and balance documentation provided by the owner. The documentation stated a basic empty weight of 1,740 pounds, with a maximum gross weight of 2,700 pounds.
The, 'Velocity Owner's Flight Manual and Weight and Balance' documentation for the accident airplane type states:
'The normal equipped empty weight is approximately 1,275 pounds. Actual weights for each airplane will vary according to installed equipment and builder workmanship. The maximum allowable gross weight for takeoff is 2,250 pounds. (2,400 pounds for the Long Wing, LW, model) except as noted below. The strake baggage areas are structurally limited to 100 pounds each side. The airplane can structurally accommodate pilots or passengers weighing up to 250 pounds. Actual limitations of each pilot area, each baggage area and fuel load depends on the empty weight and balance of the particular airplane. Nose ballast may be required for light pilots.'
The owner stated that for the accident flight, approximately 90 pounds of ballast was installed on the forward right seat. He further stated that the night prior to the accident he serviced the airplane with the addition of 10 gallons of 100-octane aviation fuel, bringing the total fuel on board to about 35 gallons. FAA medical records indicated that the pilot's weight at the time of his last medical application was 216 pounds.
The owner reported that the accident airplane was the long wing model. He stated that the airplane had a high basic empty weight, which he attributed to the installation of additional equipment. This equipment included electrically operated seats, door seals, and a 5-gallon fuel header tank.
METEOROLOGICAL INFORMATION
The closest aviation weather observation station was located at VGT. An aviation routine weather report (METAR) for VGT was issued at 0632 PDT. It stated: winds from 360 degrees at 3 knots; visibility 10 miles; skies clear; temperature 24 degrees Celsius; dew point 02 degrees Celsius; altimeter 29.84 inHg.
WRECKAGE AND IMPACT INFORMATION
FAA personnel responded to, and documented, the accident site. The airplane came to rest in a 45-degree left wing low attitude, on a heading of about 025 degrees magnetic within the southwest rear portion of a residence. The main wreckage, along with the residence, was extensively fire damaged.
MEDICAL AND PATHOLOGICAL INFORMATION
The Clark County Nevada Medical Examiner conducted an autopsy on the pilot. The cause of death was reported as multiple injuries resulting from the airplane accident.
Toxicological tests on specimens from the pilot were performed by the FAA Civil Aeromedical Institute.
Analysis of the specimens contained the following findings:
>> 48 (%) CARBON MONOXIDE detected in Blood
>> 3.18(ug/ml) CYANIDE detected on Blood
>> NO ETHANOL detected in Vitreous
>> METOPROLOL detected in Blood
>> METOPROLOL detected in Urine
Review of the pilot's medical certificate application revealed that he had indicated the use of metoprolol for blood pressure control.
TEST AND RESEARCH
The wreckage was recovered from the accident site and moved to a storage facility at North Las Vegas airport where the Safety Board IIC, and representatives from the FAA and Textron Lycoming continued the inspection.
Airframe
The majority of the airplane was constructed with composite materials, and consumed by fire.
Examination confirmed control continuity for the canard from the push-pull tube located at the control stick through to the canard control arm. The control arm eye bolt exhibited a buckling failure with rough granular surface features at the failure point. The torque tubes were observed to continue to the remnants of the burnt canard surfaces and traced through to the canard.
Aileron control continuity was confirmed from the control stick through to the torque tube located within the center tunnel area. Four feet aft of the pilot seat, the torque tube was fractured. The fracture area exhibited buckling, with granulated surface features noted at the failure point. The remaining section of tube was still connected to the aileron center control assembly.
The right rudder cable was attached at the foot pedal. Fifteen feet aft of the attach point the cable was cut by recovery personnel. The cable then continued aft of the cut, and was attached to the thermally damaged control arm in the right winglet.
The left rudder cable was separated at the foot pedal attach point. The attach bolt and bushing were in place. The end of the rudder cable was located within the main wreckage, and was separated in a broomstraw pattern. The remaining section of the rudder cable was cut by recovery personnel and terminated at its associated control arm in the left winglet.
The thermally damaged fuel mixture, throttle, and supercharger controls were attached at the throttle quadrant, and all were observed in the full forward position. The owner/builder stated that these positions corresponded with maximum throttle, maximum supercharger boost, and full rich fuel mixture.
The electrically operated fuel pump was thermally damaged and its operation could not be ascertained.
Approximately 100 pounds of ballast material was located in the forward right foot well area.
All major sections of the airplane were accounted for during the examination.
Engine
The entire engine had sustained fire damage. The underside of the engine, including the oil sump, induction system, intake manifolds, and fuel injection servo were consumed by fire. The sump mounted engine data plate could not be located. The fuel inlet screen was recovered, and was free of contaminants. The engine driven fuel pump, right magneto, and Hall Effect sensor were affixed to their respective mounting pads and exhibited thermal damage. The engine data plate was not located.
Examination of the fuel injectors revealed that their passages were clear. The fuel flow divider and internal diaphragm were thermally damaged.
The top spark plugs were of the automotive type DENSO W27EMR-C, and connected to fire damaged automotive ignition leads. The top spark plug electrodes for cylinders 1 and 3 were sooted and black in color. The top spark plug electrodes for cylinders 2 and 4 were dark grey in color.
The bottom spark plugs were Champion aircraft type REM38E. The bottom spark plug electrodes for cylinders 1 and 3 were oil soaked. The bottom spark plug electrodes for cylinders 2 and 4 were dark grey in color.
Each spark plug was tested utilizing a pressurized spark plug tester. All plugs produced a spark.
The engine was mounted on a stand at the propeller hub. The engine was rotated, and drive train continuity was established through to the accessory case. The valves and rocker arms each moved approximately the same amount of lift. Residual oil was observed within the rocker areas.
The engine cylinders were removed. The cylinder head and piston crown for cylinders 1 and 3 were oil soaked. The cylinder head and piston crown of cylinders number 2 and 4 were dark grey in color. No mechanical deformation of the valves, cylinder walls, or cylinder heads was noted, and according to the Lycoming representative, no indications of detonation were present.
Resistance of the number 3 and 4 connecting rods at the crankshaft was noted when they were moved by hand. Both connecting rods were removed. Visual examination of the main Babbitt metal bearing surfaces of the connecting rods revealed thermal damage, which the Lycoming representative stated was consistent with post accident thermal exposure.
Supercharger
The supercharger system was removed from the engine for disassembly.
The supercharger was attached to the engine by a combination of fabricated steel plates affixed to the forward crankcase thru bolts.
The inlet plenum and outlet manifold were consumed by fire. The altitude compensating relief valve was located, and observed fire damaged; the internal valve and spring were separated from the housing and free within the valve body.
The lower portion of the inlet volute was thermally damaged, exposing the inner section of the volute chamber. The impeller wheel could not be rotated by hand.
Supercharger belt tension was maintained through the use of an idler pulley. The pulley was affixed to a sliding adjustable plate, which contained three, 2-inch-long slots. The adjustable plate was attached to the supercharger housing through the slots by three bolts. The configuration allowed for about 2 inches of adjustment travel for the idler pulley.
The upper left and lower center adjustment bolts were observed firmly in place. The third bolt, located in the upper right corner of the plate, was missing and could not be located in the airplane wreckage. The heads of the two remaining bolts were drilled for safety wire, however, no wire was present.
The idler pulley adjustment plate was observed distorted approximately 3/16 inch away from the supercharger housing in the area adjacent to the missing bolt. The idler pulley was misaligned with the crankshaft and supercharger pulleys by about 3/16 inch in the aft direction.
The two remaining idler pulley adjustment plate bolts were removed. The idler plate was noted in a position 1/4 inch short of the most slack belt setting. Bolt thread marks were noted on the right wall surfaces of the top left, and top right bolt slots. Thread marks were noted on the left slot wall surface of the lower bolt slot. Rust witness marks corresponding to the bolt heads of the left and lower bolts were noted on the a
A partial loss of engine power during initial climb due to the detachment of the engine supercharger drive belt. The detachment resulted from the owner/builder's inadequate installation of the supercharger system and belt-tensioning adjustment.