Crash location | 40.056111°N, 118.577778°W
Reported location is a long distance from the NTSB's reported nearest city. This often means that the location has a typo, or is incorrect. |
Nearest city | Lovelock, NV
40.179354°N, 118.473481°W 10.1 miles away |
Tail number | N4YB |
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Accident date | 20 Oct 2016 |
Aircraft type | Northland Aviation Llc Ivp |
Additional details: | None |
On October 20, 2016, about 0730 Pacific daylight time, an experimental amateur-built Northland Aviation LLC Lancair IV-P airplane, N4YB, made a forced landing, following a total loss of engine power, near Lovelock, Nevada. The airline transport pilot sustained minor injuries. The airplane was substantially damaged to the wings and fuselage. The airplane was registered to Northland Aviation LLC and operated by the pilot under the provisions of Title 14 Code of Federal Regulations Part 91 as a personal cross-country flight. Visual meteorological conditions prevailed, and no flight plan was filed. The flight departed from Fallon Municipal Airport (FLX), Fallon, Nevada, about 0710, and was destined for Burns, Oregon.
The pilot reported that he was climbing to his cruise altitude of 16,500 ft when, about 9 minutes into the flight, he felt a severe shudder and the engine lost power. Simultaneous to the shudder, oil began to coat the windscreen. The pilot headed for Derby Field Airport, Lovelock, for landing, however as he neared the airport, he realized that he was not going to make the runway and elected to land the airplane in an open area of desert vegetation.
A review of maintenance records indicated that the experimental Lancair IV-P, serial number LIV-482 was issued a special airworthiness certificate on February 7, 2003. The airplane was equipped with a Continental Motors TSIO-550-E, serial number 803075, 350 hp engine. The pilot reported at the time of the accident, the engine had accumulated about 865 hours since new.
Postaccident examination of the engine revealed a hole in the crankcase above the #3 and #4 connecting rod journals. The #3 and #4 pistons were fractured into several pieces that were located within the engine. The #3 connecting rod had separated from the crankshaft. The connecting rods and crankshaft journals exhibited signs of thermal distress. The camshaft was fractured into four pieces. The top and bottom spark plugs from cylinder #3 exhibited debris damage and the electrodes were missing. The combustion chamber of cylinder #3 exhibited impact marks from debris. The intake valve in cylinder #3 was broken at the bottom of the valve guide. The broken intake valve head was not located within the engine and the fracture surface of the valve stem was severely damaged from debris. A metallurgist from Continental Motors visually examined the parts and determined that further examination would prove to be inconclusive due to the mechanical damage the parts sustained.
A total loss of engine power due to the failure of the intake valve in the No. 3 cylinder for reasons that could not be determined based on the available information.