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N957AT accident description

New York map... New York list
Crash location 40.777778°N, 73.875556°W
Nearest city Flushing, NY
40.765380°N, 73.817356°W
3.2 miles away
Tail number N957AT
Accident date 26 Mar 2003
Aircraft type Boeing 717-200
Additional details: None

NTSB Factual Report

HISTORY OF FLIGHT

On March 26, 2003, about 2239 eastern standard time, a Boeing 717-200, N957AT, operated by AirTran Airways as flight 356, received minor damage when the left side power control distribution power unit (PCDU) failed while on approach to land at LaGuardia Airport (LGA), Flushing, New York. During a subsequent emergency evacuation, 1 passenger was seriously injured, and 22 passengers received minor injuries. There were no injuries to the 2 pilots, 3 flight attendants, and 55 passengers. Night visual meteorological conditions prevailed for the scheduled passenger flight. An instrument flight rules (IFR) flight plan had been filed for the flight that departed from The William B Hartsfield Atlanta International Airport (ATL), Atlanta, Georgia, and was conducted under 14 CFR Part 121.

According to flightcrew interviews and documents from Air Tran airways, the en route part of the flight was without incident. Upon arrival in the New York area, the flight was radar vectored for the ILS runway 04 approach. The in-range checklist was completed and the landing weight was determined to be 97,000 pounds. The Vmin speed on approach was 135 knots, and the Vref with 40 degrees of flaps was 130 knots.

The flight was cleared for the ILS runway 4 approach, and instructed to contact LaGuardia control tower. After establishing contact with the control tower, the pilots were told that they were number 3 for the runway, following a Boeing 757, and that the braking action was reported as good by a preceding MD-80.

At 2239:16, the CVR recorded two thumps and two clicks on all channels.

The co-pilot called out the left generator was off, followed by the captain who reported they were, "...losing everything." The APU was started and the crew commented that they had lost all of their busses also. The cockpit area microphone (CAM), recorded the crew alerting and warning system (CAWS) stabilizer alert, "stabilizer motion" which repeated seven times. The co-pilot called, "select FADEC alternate" and advised the captain that he had manual throttles.

At 2239:42, the captain stated, "kill that light out of my face." The co-pilot acknowledged the captain's request, and then asked, "are you moving the stabilizer?" The captain replied that he was, "...not doing anything. I've lost everything." The co-pilot then stated, "generator left off." followed by the captain stating, "kill, kill this light...." to which, the co-pilot replied, "alright."

At 2240:00 the CAM recorded the CAWS stabilizer alert again. The co-pilot then tried to reset the generator, and the captain called, "there's the runway. I'm landing the airplane," followed by a request for landing gear down, and the landing checklist. The co-pilot reported that the auxiliary hydraulic pump had failed, followed by the captain who asked for the landing gear to be lowered. This was followed by the sound of a click and increased air noise similar to landing gear being operated.

At 2240:26, the captain questioned his Vref speed of 140 knots, and the co-pilot replied, "roger that." The captain then stated, "we don't have any idea if the gear's down, do we?", to which the co-pilot replied, "not yet, no. Weird huh."

At 2240:37, the flight was cleared to land by the control tower and told that the winds were from 010 degrees at 13 knots.

At 2240:45, the co-pilot said, "I smell something too, don't you."

At 2241:04, the captain said, "go to flaps forty." This was acknowledged by the co-pilot.

At 2241:08, the CAM recorded a sound similar to the CAWS landing gear alert, which started, and continued to the end of the recording. The CAM also recorded a mechanical voice, which stated, "one thousand [feet]."

At 2241:10, the captain stated, "you smell something burning? I think we have a fire." The co-pilot replied, "I smell something weird...no way to tell if landing gear down. A few seconds later the co-pilot stated, "we lost everything, that's for sure. Your speed's pretty damn high.", to which the captain replied, "that's all right...."

At 2241:34, the captain stated, "tell him we're declaring an emergency. We have an electrical problem." The co-pilot told the control tower that they had an electrical emergency. The captain further stated, "tell him to send the equipment", and the co-pilot transmitted to the control tower,"...we might have a possible fire...we're landing on runway four."

At 2241:58, the captain stated, "all right, we'll stay at this altitude." The co-pilot replied, "roger that. I wouldn't go any lower." At 2242:02, the CAM recorded a mechanical voice, which stated, "minimums." At 2242:04, the captain stated, "...we may have to evacuate the airplane." This was acknowledged by the co-pilot.

At 2242:09, the co-pilot stated, "I wouldn't get any lower." and the captain replied, "...we're all right...". At 2242:12, the co-pilot stated, "okay, your looking good. You're definitely fast. Don't go any faster." The captain replied, "I know, I know that." At the same time as the captain's reply, the CAM recorded a mechanical voice, which stated, "one hundred."

Between 2242:19 and 2242:25, the CAM recorded a mechanical voice calling out "fifty", "forty", "thirty", "twenty", "ten", and "five."

At 2242:25, the CAM recorded a sound similar to the airplane touching down on the runway, and at 2242:28, the CAM recorded a "thump" similar to nose landing gear contact with the runway. At 2242:36, the co-pilot called ,"reverse," and one second later he called, "eighty knots."

At 2242:50, the captain stated, "tell him we need the fire trucks out here. I think we may have a fi, some kind of fire." At 2242:52, the co-pilot transmitted to the control tower, "...tower, Citrus three fifty six, uh, please run the fire trucks out here. We are smelling electrical smoke." The local controller asked the pilots to pull all the way onto taxiway BRAVO, and acknowledged their request for fire trucks.

At 2243:04, the captain stated, "get, get the door, get the door unlocked." The local controller asked the pilots to hold short of taxiway FOXTROT, and this was acknowledged. The local controller then instructed the pilot to contact ground control, and the co-pilot replied, "sir, I can't..." The captain then transmitted, "We, we don't have time for that sir. I may have to evacuate. You're gonna have to just get some people out here. The local controller replied, "Okay, you can stop right there if you need to and do what you have to do."

At 2243:37, the captain stated, "we got some kind of fire guys. Get ready to get out of here. A flight attendant stated, "we have no lights", and the captain said, "just, just um all right just hold still, all right, just hold still, hold still."

At 2243:43, an announcement was made on the public address system which stated, "Ladies and gentlemen, we need everybody in their seats please...."

At 2243:44, the captain asked, "do you have any emergency lights?", and the co-pilot replied, "nothing." At 2243:47, the captain stated, "alright, evacuate the airplane. Tell 'em we've gotta evacuate the airplane." At 2243:48, the CAM reported a flight attendant stating, "evacuate, evacuate."

At 2243:50, the captain stated, "All right do your, lets do the checklist." The co-pilot replied, "okay."

The transcript ended at 2243:52

The captain reported that after he stopped the airplane, he exited his seat and opened the cockpit door to assess the situation. The cabin was dark. There was a stronger burning smell in the cabin than they had experienced in the cockpit. The captain then ordered an emergency evacuation of the airplane. The first officer reported that he completed the emergency evacuation checklist, which included resetting the wing flaps to 25 degrees.

The flight attendants reported that on approach, the cabin lights extinguished, and the emergency lights illuminated. Then after a few minutes, the emergency lights extinguished, and the cabin was without illumination. In addition, the L1 and R1 flight attendants noticed a burning smell. The lead flight attendant (L1) reported that when she punched the buttons for the public address system, the buttons did not illuminate on the handset used for making public address announcements and communicating with the cockpit, and she perceived that the handset was inoperative. After touchdown, the lead flight attendant exited her seat, and tried banging on the cockpit door and speaking loudly to get the attention of the flight crew. The pilots reported that they did not hear the flight attendant pounding on the door or speaking loudly.

About the same time that the captain had opened the cockpit door to check the cabin, the forward flight attendants reported hearing the aft flight attendant make an announcement using the PA system for the passengers to remain seated. The lead flight attendant then tried her handset again, and was able to make an announcement using the PA to begin the evacuation.

The L2 flight attendant at the aft station jettisoned the tail cone, but could not determine if the slide had properly inflated. She then directed the passengers in the aft part of the cabin to the forward over wing exits and forward doors. She exited the cabin at the left rear overwing exit, and then re-entered the cabin. At that time, she heard a "pop" which she associated with the inflation of the tailcone slide.

After the passengers and flight attendants exited the cabin, the captain went to the rear of the airplane and then back forward to ensure no one was still onboard. At that time, firemen were at the forward door of the airplane. The forward slide was released, and the firemen gained access to the cabin using ladders.

The accident occurred during the hours of darkness at 40 degrees, 46.67 minutes north latitude, and 73 degrees, 52.54 minutes west longitude.

PERSONNEL INFORMATION

Captain

The captain held an airline transport pilot certificate with a multi-engine airplane rating, and a commercial pilot certificate with a single engine airplane rating. He was type rated in the DC-9, which included the Boeing 717. He was last issued a first class FAA airman medical certificate on March 10, 2003. His total flight experience was 13,811 hours, with 1,677 hours in make and model. He had flown 266 hours in the preceding 90 days.

Co-pilot

The co-pilot held an airline transport pilot certificate with single and multi-engine airplane ratings. In addition, he held a commercial pilot certificate with rotorcraft and instrument helicopter ratings. He also held a flight instructor certificate with ratings for single and multi-engine airplanes and instrument airplane. He was last issued a first class FAA airman medical certificate on November 5, 2002. His total flight experience was 7,000 hours, with 873 hours in make and model. He had flown 178 hours in the preceding 90 days.

AIRCRAFT INFORMATION

The Boeing 717-200 was type certificated under A6WE. This included the original DC-9 series, the MD-80 and MD-90 series, and the Boeing 717 series of airplanes.

According to records from Air Tran, at the time of occurrence, the airplane had accumulated 6,308 hours, and 4,503 cycles, since its delivery new in January 2001.

Boeing 717 Electrical System

The Boeing 717 utilized an automatic integrated electrical power system. In-flight power sources were the batteries, and the three AC generators, one on each engine, and the APU. System operation was automatic and under control of the electrical power control unit (EPCU), which provided external power protection, automatic power transfer, emergency power automatic activation, and galley power shedding. Additional system control came from the three-power conversion and distribution units (PCDU), one with each generator. For components requiring DC power, each PCDU had an integrated transformer rectifier that converted 115-volts AC to 28-volts DC.

When an electrical system malfunction occurred, an alert was displayed on the engine and alert display (EAD). Additional information was available on the electrical synoptic page, including power sources, voltage, frequency, generator load, individual relay positions, and primary AC and DC buses.

Display Units

Flight and airplane system information was obtained from the six flat panel Display Units (DUs) on the instrument panel. They were numbered from left to right, one through six. There were four types of information the DUs were capable of displaying. These include; Primary Flight Display (PFD), Navigation Display (ND), Engine and Alert Display (EAD), and System Display (SD). The PFD display was a reserved display, and could not be manually changed to another DU. With a loss of one or more DUs, the system assumed a pre-determined configuration based upon the DUs lost. With a reconfigured, or partial display, the pilots had the option of changing a SD display to a ND display.

The standard display and source of power for each DU was as follows:

DU #1: Captain's PFD Emergency DC bus

DU #2: Captain's ND DC transfer bus

DU #3: EAD Emergency DC bus

DU #4: SD Right DC bus

DU #5: First Officer's ND Right DC bus

DU #6: First Officer's PFD Left DC bus

Cabin Emergency Lighting

The airplane was equipped with both cockpit and cabin emergency lighting whose battery power supply was independent from other airplane power sources. This system was controlled primarily by a three-position toggle switch in the cockpit overhead panel with positions of OFF, ARM, and ON. There was an additional switch on the flight attendant's Control Panel adjacent to the L-1 forward entry door. Likewise, this switch was also a three-position switch (OFF, momentary ARM, and ON.) It was normally guarded in the OFF position and was intended for use only when the flight crew did not arm or was unable to activate the cockpit switch. An alert message was displayed on the EAD DU if the switch was not in the ARM position during normal operation.

With the cockpit switch in the OFF position, the emergency lights were off and would not illuminate during a power loss. If either the cockpit or the flight attendant's switch were selected to the ON position, emergency lights would illuminate in both the cockpit and the cabin. If the flight attendant's switch was used to activate the emergency lights, they would remain illuminated even if the cockpit switch was moved to the OFF position. The flight attendant's switch must be moved to the OFF position to return system control to the cockpit switch.

With the cockpit switch in the ARM position, the cockpit and cabin emergency lights would illuminate with a loss of electrical power to the emergency DC bus. If power was restored to the bus, the emergency lights would extinguish, and the batteries would be recharged.

FLIGHT RECORDERS

Cockpit Voice Recorder

The cockpit voice recorder was examined in the Safety Board vehicle recorder laboratory. The quality of the recording was excellent and a transcript was prepared of the last 19 minutes of flight and 1 minutes of ground time.

Flight Data Recorder

The flight data recorder was examined in the Safety Board vehicle recorder laboratory. The recorder was powered by the left DC bus on the airplane's electrical system. The first indication of an anomalous condition occurred when a momentary data drop out was recorded by the three acceleration channels. Upon data return, all three channels recorded normally again for a further five seconds, when a total loss of all recorded data ensued.

The data for the display units was recorded every 4 seconds. The last data from each of the units indicated they were in operation. There was no data to indicate any anomalous data to either the display units, or any other electrical circuit on the airplane, prior to a total loss of electrical power to the flight data recorder.

WRECKAGE AND IMPACT INFORMATION

The airplane was examined by an inspector from the FAA who reported that the left side PCDU, located in the forward electronics bay, exhibited evidence of sooting, and had a burned odor about it. The unit, along with the bus tie breakers associated with it, were re

NTSB Probable Cause

A failure of the left power control distribution unit (PCDU).

© 2009-2020 Lee C. Baker / Crosswind Software, LLC. For informational purposes only.