Crash location | 45.588611°N, 122.597500°W |
Nearest city | Portland, OR
45.523452°N, 122.676207°W 5.9 miles away |
Tail number | N753FE |
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Accident date | 24 Dec 2005 |
Aircraft type | Cessna 208B |
Additional details: | None |
On December 24, 2005, at 0743 Pacific standard time, a Cessna 208B, N753FE, experienced a partial loss of engine power and collided with an antenna array and terrain during takeoff initial climb from runway 21 at Portland International Airport, Portland, Oregon. The commercial pilot, the sole occupant, sustained minor injuries. There was substantial damage to the airplane, which was registered to Federal Express Corporation of Memphis, Tennessee and operated by Empire Airlines, Inc., of Hayden, Idaho. Visual meteorological conditions prevailed and an instrument flight rules (IFR) flight plan was filed for the 14 CFR Part 135 cargo flight. The flight was originating when the accident occurred and the intended destination was Roseburg, Oregon.
According to information provided by the Portland Air Traffic Control Tower, the airplane was cleared for takeoff on runway 21 from intersection Charlie at 0742. Several of the air traffic controllers on duty at the time witnessed the accident and reported that the airplane became airborne, but failed to gain altitude and struck an antenna array and a fence off the departure end of the runway. The airplane continued across a slough, struck an embankment and came to rest about 900 feet from the departure end of the runway on a golf course located adjacent to the airport.
The pilot reported that "no abnormalities were noticed during power application and take off roll. Engine gauges indicated max power was being produced and acceleration rates seemed normal." He further reported that "at rotation speed (75 knots) the aircraft felt sluggish and slow to respond, but did become airborne." He suspected that the flaps were not down, but upon glancing at the flap position indicator, he saw that they were at the 20 degree take off setting. The pilot stated that "after becoming airborne, the airplane quit accelerating and a positive climb rate was not established." He pushed the power lever all the way forward, but did not feel a response from the airplane.
An FAA inspector and a representative from Cessna Aircraft Company examined the airplane after it was recovered to a hangar on the airport. No pre-mishap anomalies were noted to the airframe. Control cable continuity was established except for the left aileron and left flap cables. The left wing separated from the fuselage, and the left aileron and flap control cables displayed signatures consistent with tension overload; continuity was established from the separations to the cabin controls and to the surface bell cranks. The flap actuator extension measurement indicated a 20 degree flap position. First responders had moved the fuel selector valves to the "OFF" position and recovered 10 to 12 gallons of fuel from the left tank, approximately 87 gallons from the right tank, and 2 gallons from the fuel reservoir tank. Firewall fuel filter screens were clean and free of debris. No sign of fuel contamination was noted. The emergency power lever was found in the "normal" detent. The propeller remained attached to the engine. All propeller blades displayed leading edge damage and chordwise scoring. Approximately 6 inches of the tip of one blade had separated from the blade.
The Cessna representative reported that the empty weight of the airplane was 4,770 pounds. The manifest recorded 1,900 pounds of freight for the flight. Actual weight of the freight was 1,945 pounds. Just prior to the mishap flight, the airplane had been fueled with 60 gallons of Jet-A fuel, bringing the total fuel load to approximately 600 pounds per side. Takeoff weight of the airplane as calculated by the Cessna representative was approximately 8,100 pounds, and the airplane's gross weight was 8,750 pounds. According to the takeoff distance charts in the aircraft information manual, for the accident conditions, ground roll distance should be approximately 1,190 feet and the total distance to clear a 50 foot obstacle should be approximately 2,095 feet. (The available distance for takeoff on runway 21 from intersection Charlie is approximately 3,300 feet.) Normal takeoff procedure, according to the information manual, calls for 20 degrees of flaps and rotation at 70 to 75 knots indicated airspeed.
The airplane was equipped with a Power Analyzer and Recorder (PAR) manufactured by Avionics Specialties, Inc. of Charlottesville, Virginia. The PAR accumulates, stores and outputs the records of all starts, shutdowns, limit exceedences and other specified data for engine condition check and trend analysis. A Start Record is stored in memory when the NG (compressor speed) Tachometer has reached the ground idle value (51%) and the ITT (interstage turbine temperature) has gone over 200 degrees C. A Shutdown Record is recorded when the NG drops to 12%. An Exceedence Record is recorded when the "Over Limit" Condition has ended. A Power Fail record is made when the engine is running (NG over 51%) and the 28 VDC power to the computer is removed.
The PAR computer was removed from the airplane and sent to Avionics Specialties for a data extraction, which was performed under the supervision of an FAA inspector on January 4, 2006. A Power Fail record indicated that system power was removed from the unit at 07:37:50 on December 24, 2005. (This time was taken from a clock in the unit settable by the operator.) At the time of the power loss, engine ITT was 537 degrees C, engine torque was 615 foot pounds, NG was 69.3%, propeller speed was 629 rpm, fuel flow was 157 pounds per hour, and indicated airspeed was 58 knots.
The engine, a Pratt and Whitney PT6A-114A, S/N 19121, was removed from the airplane and sent to Pratt and Whitney Canada, St Hubert, Quebec, where it was examined under the supervision of an NTSB investigator on January 31 and February 1, 2006. Initial examination of the engine showed no major structural deformation. The compressor and power turbines displayed moderate circular rubbing damage to the blades suggesting engine operation at impact, likely in the low to mid power range. The compressor module, reduction and accessory gearboxes showed no damage and were free turning; they were not disassembled. The fuel pump/fuel control assembly was partially separated from the engine from fracture of the fuel pump mounting flange. The fuel pump drive coupling was fractured in overload. The remaining accessories showed minor deviations from field adjustable parameters during testing; Pratt and Whitney Canada personnel stated that these minor deviations would not have resulted in a loss of engine power.
During the examination at Pratt and Whitney Canada, the compressor discharge air (P3) reference line to the fuel control unit was found loose at the rear firewall coupling location, and the P3 line "B" nut safety wire was found broken. In a written statement, dated July 18, 2006, the operator's Director of Maintenance reported that following the accident, he had attempted to check all of the P3 air lines for tight connections. He was able to verify that all connections were tight with the exception of the connection found loose during the examination at Pratt and Whitney Canada. The Director of Maintenance stated that "later in the investigation once the cowling was off," he did check the connection and found that it was tight. He further stated that he did not see broken safety wire on the fitting. In a written statement dated July 20, 2006, the operator's 208 Fleet Manager reported that during examination of the airplane on December 27, 2005, "the P3 line was removed for access to the compressor screen. The line was reattached finger tight after we inspected the compressor."
A partial loss of engine power for an undetermined reason during the initial takeoff climb resulting in an in-flight collision with objects.