Crash location | 39.990000°N, 75.581945°W |
Nearest city | West Chester, PA
39.960664°N, 75.605488°W 2.4 miles away |
Tail number | N306RL |
---|---|
Accident date | 15 Nov 2016 |
Aircraft type | Robinson Helicopter Company R22 |
Additional details: | None |
On November 15, 2016, about 1500 eastern standard time, a Robinson R22, N306RL, was substantially damaged during a practice autorotation landing at Brandywine Airport (OQN), West Chester, Pennsylvania. The flight instructor and a student pilot were not injured. The helicopter was privately owned and operated under the provisions of 14 Code of Federal Regulations Part 91 as an instructional flight. Day, visual meteorological conditions prevailed at the time, and no flight plan was filed. The local flight departed OQN about 1430.
The flight instructor reported that he was demonstrating straight-in autorotation landings to a power recovery using the runway. The wind was generally from the north, but shearing from the northeast to the northwest, horizontally. During an autorotation to runway 9/27, he began to flare about 40 feet above the ground. At 20 feet, a large gust with a horizontal wind shear caused the helicopter to drift to the right and lose tail rotor effectiveness. He corrected the drift and heading with flight control inputs, returned to the runway, and continued the flare. During the last portion of the flare, a vertical wind shear was encountered, and the helicopter climbed, uncommanded, about 20 feet. At that point, "all wind stopped," and the helicopter descended. He attempted a power recovery; however, the helicopter landed hard on the skids, with some sideward motion. The helicopter bounced, the left skid broke, and the aircraft rolled and came to rest on its left side. The two pilots egressed the helicopter and were met by first responders.
An inspector with the Federal Aviation Administration responded to the accident site and examined the wreckage. Structural damage to the airframe was confirmed The main rotor blades were deformed from impact forces and the tail boom was partially separated. He determined that the helicopter was operated within the aircraft's weight and balance limitations at the time of the accident; however, it was operated at the forward center of gravity limit. The pilots weighed about 200 pounds each, which placed the helicopter near the upper weight limit. His examination of the wreckage did not reveal evidence of a mechanical failure or malfunction. He reported that the surface wind at the time of the accident varied between 330 and 350 degrees at 11 to 14 knots.
The flight instructor did not report any preaccident mechanical malfunction or failures with the helicopter that would have precluded normal operation.
The flight instructor's decision to continue the practice autorotation in known gusting wind conditions, which resulted in a hard landing and roll over.