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N529AU accident description

Pennsylvania map... Pennsylvania list
Crash location 40.488055°N, 80.226389°W
Reported location is a long distance from the NTSB's reported nearest city. This often means that the location has a typo, or is incorrect.
Nearest city Pittsburgh, PA
40.440625°N, 79.995886°W
12.6 miles away
Tail number N529AU
Accident date 27 Jul 2006
Aircraft type Boeing 737-300
Additional details: None

NTSB Factual Report

HISTORY OF FLIGHT

On July 27, 2006, about 0945 eastern daylight time (EDT), US Airways flight 231, a Boeing 737-300, N529AU, experienced a nose landing gear collapse while being pushed back from gate B-27, at the Pittsburgh International Airport (PIT), Pittsburgh, Pennsylvania. The 2 certificated airline transport pilots, 3 cabin attendants, and 73 passengers were not injured. Visual meteorological conditions prevailed, and an instrument flight rules flight plan was filed. The scheduled passenger flight, destined for Palm Beach International Airport (PBI), West Palm Beach, Florida, was conducted under 14 Code of Federal Regulations (CFR) Part 121.

In a written statement, the first officer said that during her preflight inspection, a ground crewman directed her attention to the nose landing gear wheel because it was not oriented with the nose of the airplane, but "cocked to one side." The crewman said that he might have to "realign the aircraft during the pushback."

The crew completed their preflight tasks through the "Before Start Checklist." During a "normal" pushback with the airplane in motion, the crew initiated a start on the number two engine, and the nose gear collapsed.

A review of written statements from ground crew personnel revealed that when the airplane parked at the gate, the nose wheel was aligned with the nose of the airplane. The crew installed the bypass pin, and attempted to install the tow bar in preparation for the subsequent pushback, but the nose gear migrated to the airplane's right, with no steering forces applied. Once the wheel stopped turning, the tow bar was attached, oriented about 35 to 45 degrees off the airplane's centerline.

The pushback was "normal," and the tug and the airplane aligned without difficulty. In a telephone interview, one ground crewman described the pushback as "smooth" and steady with no rapid accelerations, decelerations, or turns. He said that as the airplane slowed for the eventual disconnection of the tow bar, he heard a "snap" or "crack" and the nose gear collapsed.

A Federal Aviation Administration (FAA) inspector was in the passenger area and watched the pushback as the plane cleared the Jetway. When the aircraft came into his view he did not see anything odd until he watched the nose of the accident airplane "rise up about one foot [and] then the nose dropped to the ground...The motion of the nose was similar to a horse throwing up its head rapidly."

A US Airways employee, making a delivery in the area of the departure gate, waited for the pushback, because the airplane blocked his path. He stated, "The tug appeared to jerk hard just as it passed the Jetway." He stated that the tug slowed, the airplane bounced, "the tail went upwards in two motions," and then the nose contacted the ground.

WRECKAGE INFORMATION

National Transportation Safety Board aeronautical engineers examined the airplane at the scene on July 28, 2006. The collapse of the nose landing gear resulted in substantial damage to the aft wheel well bulkhead. Examination of the gear revealed that the lower drag brace was fractured at its center, and the flanges at the break were twisted. One fracture surface was sectioned from the brace, and forwarded to the Safety Board Materials Laboratory in Washington, D.C., for examination.

The airplane was released to the operator for repair, however; parts removed from the landing gear and landing gear steering systems during repair were retained for examination at a later date.

TEST AND RESEARCH

On August 4, 2006, the drag brace section was examined in the Safety Board Materials Laboratory. Examination of the drag brace revealed that it was deformed due to compression buckling, and the fracture surfaces were consistent with overstress fracture. There was no evidence of any preexisting cracks.

The lower drag brace was reexamined and hardness testing was conducted in the Safety Board Materials Laboratory on October 12, 2006. Rockwell hardness testing revealed that the lower drag brace fell within the hardness range for tensile strength specified in the Boeing engineering drawing.

On August 16, 2006, the hydraulic components, tested under the supervision of Safety Board engineers, included the left and right steering actuators, the depressurization steering valve, the retract actuator, and the lock actuator. All five components met their individual test requirements.

On September 21, 2006, the airplane tug was examined by an engineer and a mechanic of US Airways. Initial testing revealed that shifting gears was "difficult," and that "shifting into reverse would result in long hesitation then hard jerks before [the tug] would move smoothly." The shift lever could easily move thru the neutral gate as the shifter moved back forth between forward and reverse gears. The engineer stated that there was no spring tension in the neutral gate to prevent accidental shifting from forward to reverse. The test was suspended, and the tug was quarantined for further testing under the supervision of an FAA aviation safety inspector.

Examination of the tug was repeated under the supervision of the FAA inspector. The tug was also driven forward at low speed, and the shift lever was moved thru the gate into reverse gear. According to the engineer, the force "nearly threw the driver out of the tug...This is believed to be the same violent force that acted on [the accident airplane's] nose gear." Examination also revealed that the transmission required servicing with "several cans" of transmission fluid. Following the tests, a new shifter was installed on the tug before it was placed back into service.

Examination of photographs of parallel skid marks at the scene revealed that the distance between them was identical to the tug's wheelbase, and were consistent with sudden engagement of the transmission.

The FAA inspector reviewed the operator's report, and concurred with its findings.

The flight data recorder (FDR) and the cockpit voice recorder (CVR) were forwarded to the Safety Board Recorders Laboratory in Washington, D.C. for examination. The recorders were reviewed by Safety Board staff, but no significant or pertinent details were noted. Therefore, a recorder group was not formed, and no transcripts were published.

METEOROLOGICAL INFORMATION

The weather reported at Pittsburgh International Airport included few clouds at 6,000 feet, with winds from 220 degrees at 10 knots. The temperature was 25 degrees Celsius, and the dew point was 20 degrees Celsius.

NTSB Probable Cause

The airplane tug driver's inadvertent movement of the tug gear shift lever from forward to reverse, which resulted in the nose landing gear collapse. Contributing to the accident was the defective gear shift lever.

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