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N474AR accident description

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Crash location Unknown
Nearest city Wichita Falls, TX
33.913708°N, 98.493387°W

Tail number N474AR
Accident date 03 Mar 1994
Aircraft type Cessna 310K
Additional details: None

NTSB description


On March 3, 1994, at 2055 central standard time, a Cessna 310K, N474AR, was destroyed following a loss of control near Wichita Falls, Texas. The commercial pilot and his three passengers were fatally injured. Visual meteorological conditions prevailed for the personal flight.

The airplane departed the Addison Airport, near Dallas, Texas, at 2003 on an IFR flight plan to the Centennial Airport, near Denver, Colorado. At 2029, while in cruise flight at 8,000 feet, the pilot was advised by ATC that they were not receiving his transponder. The pilot replied that they would recycle the transponder. Two minutes later, ATC advised the pilot that they were still not receiving the transponder, and the pilot replied that they were experiencing electrical problems, the lights were dimming out, and "just bear with us, it's a rental airplane."

Radio communications were lost at 2034, when the airplane was reported crossing the Bridgeport VOR 039 degree radial, at 34 nautical miles (NM). Fort Worth Center lost radar contact with the airplane at 2040, when the airplane was 33 NM east of Wichita Falls, Texas.

Sheppard Air Force Base (AFB) Approach was contacted by Fort Worth Center and advised that N474AR was approaching Wichita Falls; however, they were never able to establish contact with the airplane.

The airplane was located by search and rescue personnel at 0230 the next morning in an open pasture, approximately 2.8 NM east of the Sheppard AFB/Wichita Falls Municipal Airport. During the last few miles of the flight, the airplane was headed west over sparsely populated rural area that offered minimal or no visual references in the dark night environmental conditions that prevailed.

There were no reported eyewitnesses to the accident; however, several residents in the immediate area of the accident reported hearing the sound of an airplane engine revving up the engines around the time of the accident, followed by the sound of impact.


The pilot started flying in October 1973. He obtained his instrument rating on September 1984, and his multi-engine rating on August 1988. He was initially checked out in the Cessna 310 on July 17, 1988. His last local check out in the Cessna 310 was on January 28, 1993, when he received 1.9 hours of instruction.

The right seat occupant was the pilot's younger brother. He was an instrument rated ASEL private pilot. He assisted the pilot with some of the radio transmissions during the flight. A flashlight was found in his left hand.


A review of the airframe and engine records by the FAA inspector, did not reveal any anomalies or uncorrected maintenance defects prior to the flight. The baggage and personal gear for all the occupants accounted for 154 pounds, and based on weight and balance calculations performed, the airplane was within its limits at the time of the accident.

The emergency procedures card was found on the floor of the airplane between the pilot and copilot seats. A current approach plate, opened to the ILS approach for the Wichita Falls Airport was also found in the same area.


The transcripts from all communications between the airplane and and all the pertinent Air Traffic Control (ATC) facilities are enclosed in this report.


Ground scars and imprints made by the right engine, propeller, and wing tip tank were located on the left side of the initial point of impact on a measured heading of 175 degrees. Traces of the red navigational light lens were found on the right side of the initial point of impact. The magnetic compass, and most of the windshield plexiglass were found at the initial point of impact.

The wreckage came to rest in the upright position on a measured heading of 330 degrees. The landing gear was found in the extended position. The landing gear emergency extension handle was found out of the retaining clip with the handle fully engaged and locked.

Flight control continuity was established to the rudder, elevators, and ailerons.

Fuel was found in each of the wing auxiliary tanks. Both wing tip main tanks were destroyed by impact. The fuel selectors were found on their respective main tanks. According to the operator's records, the airplane was topped off with 4 gallons of 100LL Avgas prior to its departure from the Addison Airport.

Both engines were found separated from their respective mounts. Both propeller assemblies were found buried in the muddy ground at the initial point of impact, next to a pond. See wreckage diagram for details on the wreckage distribution pattern.


Autopsies and toxicological tests were ordered and performed. The autopsies were performed by Jeffrey J. Barnard, M.D, Chief Medical Examiner for the Southwestern Institute of Forensic Science, at Dallas, Texas, on March 5, 1994. Toxicological tests were negative.


A complete wreckage reconstruction and examination was accomplished on March 7, 1994. The two Concord CB-25 lead acid batteries were tested for output. The number one battery had a residual voltage of 1.8 volts while the number two battery had a residual voltage of 1.4 volts. Both batteries were placed on a battery charger for 30 minutes. Battery charging and retention were normal and no defects were observed.

A detailed examination of both engines was completed at the engine manufacturer's facility on April 21, 1994. Engine continuity was established on both engines. The ignition system was tested and the fuel injection system was flow tested. No discrepancies were found on either engine that would have prevented normal engine operation. A copy of the teardown report is enclosed.

Both generators, their respective voltage regulators, and the paralleling relay were tested at an FAA Repair Station on March 11, 1994.

The left generator (Part Number 1105057, Serial Number 27335R) exhibited signs of severe overheating. Signs of internal disintegration was evidenced by several large pieces of copper armature winding wire coming out when the inspection flange was removed. Additionally, evidence of solder being thrown into the generator case was found on the case. Due to the extent of the internal damage to the generator, the generator would not provide any electrical output. Aircraft records indicate that this generator was installed on January 19, 1994, with two other generators previously installed on October 28, 1993, and on June 21, 1993.

The right generator (Part Number 1105057, Serial Number 1030697) was tested on a test stand. Electrical output was found to be within limits and the generator was found operational; however, the electrical output dropped to zero anytime the grounding strap from the generator to the voltage regulator was disconnected. The aircraft grounding wire for the right voltage regulator was found to have a burned out terminal end.

Both voltage regulators were manufactured by Electrosystems Inc, under Part Number VR-300-28-50. Serial numbers for the voltage regulators were 3021595R for the left, and 21111538R for the right. No defects were noted in the operation of the regulators.


The wreckage was released to the owner's representative following conclusion of the field investigation.

(c) 2009-2018 Lee C. Baker / Crosswind Software, LLC. For informational purposes only.