Crash location | 33.180278°N, 97.828611°W |
Nearest city | Bridgeport, TX
33.210116°N, 97.754755°W 4.7 miles away |
Tail number | N5331B |
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Accident date | 07 Jul 2016 |
Aircraft type | Cessna 152 |
Additional details: | None |
On July 7, 2016, about 2030 central daylight time, Cessna 152 airplane, N5331B, was damaged during a landing at the Bridgeport Municipal Airport (KXBP), Bridgeport, Texas. The private rated pilot and pilot rated passenger were not injured and the airplane was substantially damaged. The airplane was registered to US Aviation Group LLC and was operated by a private individual under the provisions of 14 Code of Federal Regulations Part 91 as a personal flight. Visual meteorological conditions prevailed for the flight, which operated without a flight plan. The flight originated from Denton Enterprise Airport (KDTO), Denton, Texas, about 1945.
According to the pilot, on the third touch-and-go to runway 18 at KXBP, the ground run was longer and the airplane had difficultly climbing away from the runway. He saw that the flaps were still at 30° despite the flap handle being in the up position. The pilot then maneuvered to land to runway 36 at KXBP, but was higher than normal while approaching the runway. He slipped the airplane down and the airplane floated down the runway. The airplane touched down near the end of the runway and the when the brakes were applied, the pilot lost control of the airplane. Swerving left and right, the airplane exited the side of the runway. The nose wheel got stuck in the soil and the airplane nosed over coming to rest inverted.
The flap actuator motor, jackscrew, and flap tube assembly were sent to Textron Aviation for an examination. Under the auspices of inspectors from the Federal Aviation Administration, the jackscrew was unboxed and examined. The flap tube assembly on the flap actuator motor was found fully extended and bound. The tube assembly was freed mechanically, and the flap actuator motor was able to move the tube assembly normally. Further examination did not find a reason for why the tube assembly had become bound. No anomalies were detected with the jackscrew or the flap actuator
The pilot's unstabilized approach and uneven braking due to insufficient runway remaining, which resulted in a loss of directional control during landing. Contributing to the accident was the bound flap jackscrew, which jammed the flaps and led to the pilot’s inability to operate the airplane normally.