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N67PS accident description

Texas map... Texas list
Crash location 34.949166°N, 101.580834°W
Reported location is a long distance from the NTSB's reported nearest city. This often means that the location has a typo, or is incorrect.
Nearest city Amarillo, TX
35.221997°N, 101.831297°W
23.6 miles away
Tail number N67PS
Accident date 14 Dec 2012
Aircraft type Beech E-90
Additional details: None

NTSB Factual Report

HISTORY OF FLIGHT

On December 14, 2012, about 1805 central standard time, a Beech E-90 airplane, N67PS, impacted terrain following an inflight break-up near Amarillo, Texas. The commercial rated pilot and passenger were fatally injured. The airplane was substantially damaged. The airplane was registered to O'Neal Aviation LLC, Colorado Springs, Colorado, and operated by a private individual. Instrument meteorological conditions prevailed and an instrument flight plan was filed for the 14 Code of Federal Regulations Part 91 personal flight. The flight originated from the Rick Husband International airport (KAMA), Amarillo, Texas, about 1750, and destined for the Fort Worth Meacham Airport (KFTW), Fort Worth, Texas.

A review of the air traffic control communications and radar data revealed that the controller transferred the airplane from AMA departure, to the Albuquerque Air Route Traffic Control Center (ARTCC). The ARTCC controller reportedly cleared the airplane to flight level 210, and gave the pilot permission to deviate east of the airplane's route for weather and traffic avoidance. Shortly thereafter, the airplane appeared to turn to the north, and the pilot did not respond to the controller's query about the turn.

The Texas Department of Public Safety located the airplane wreckage about 20 miles south of KAMA on open, rolling hill, ranch land. The airplane's outer wing sections, engines, elevators, vertical and horizontal stabilizers were separated from the fuselage and located in several directions from the main wreckage.

PILOT INFORMATION

The pilot held commercial pilot certificate with ratings for airplane single-engine land, multiengine land, and instrument-airplane. A third-class Federal Aviation Administration (FAA) medical was issued on October 2, 2012, with the limitation; must have glasses for near vision. On the application for a medical certificate the pilot listed his total time as 1,650 hours and 50 hours in the preceding six months.

AIRCRAFT INFORMATION

The Beechcraft E-90 King Air is a twin-turboprop airplane powered by two Pratt & Whitney PT6A-28 engines. The airplane is typically configured for 5-7 passengers and two pilots. The airplane was maintained under the manufacturer's maintenance program.

A review of the airplane's maintenance records revealed that the airframe's phase 3 and 4 inspections were completed on March 23, 2012. At the time of the inspection, the airframe had a total time of 8,600.2 hours. The airplane's phase 1 and 2 inspections were completed on May 23, 2012, at which time; the left engine had accumulated 8,456.7 total hours and 1,988.0 hours since overhaul; the right engine had accumulated 8,545.7total hours and 2,781.7 hours since overhaul. The airplane's total time was 8,607.3 hours, at the time of the inspection.

The airplane was equipped with a Garmin GDL 69 that can deliver XM WX satellite weather to the airplane's Garmin 530 GPS/NAV/COM navigation system. The airplane was also equipped with a Bendix/King model KGP 560 eGPWS (enhanced Ground Proximity Warning System).

METEOROLOGICAL INFORMATION

The Area Forecast for Texas panhandle area, issued at 1345 CST forecasted: scattered clouds or a broken ceiling at 8,000 feet mean sea level (msl) with cloud tops to 15,000 feet msl, surface visibility of 3-5 miles, blowing dust, widely scattered thunderstorms with light rain, thunderstorms possibly severe, cumulonimbus tops to FL350, southerly surface wind of 30 knots with gusts to 40 knots; for the eastern half of the Texas panhandle until 2000 CST – ceiling broken at 3,500 feet msl with layered clouds to FL250, scattered light rain showers and widely scattered thunderstorms with light rain developing between 1400 and 1600 CST, thunderstorms possibly severe, southerly surface wind of 20 knots with gusts to 30 knots.

Two Airmen's Meteorological Information (AIRMET) advisories were active at the accident location at the accident time. One advised of moderate turbulence below FL180 and a second advised of strong surface winds with sustained magnitudes greater than 30 knots expected.

There were three pilot reports (PIREPs) within 50 miles the accident site that were reviewed from 3 hours of the accident time; the reports included moderate turbulence and mountain wave activity.

The Aviation Weather Center in Kansas City, Missouri, issued several convective Significant Meteorological Information (SIGMETs) for Texas that were valid at the accident time. The Storm Prediction Center (SPC) in Norman, Oklahoma, also issued Convective Outlook reports that concerned the Texas panhandle.

At 1753, the automated weather observation facility located at KAMA, reported wind from 210 degrees at 10 knots, with a peak wind at 1714 CST from 260 degrees at 33 knots, visibility 10 miles, broken clouds at 10,000 feet, temperature 47 Fahrenheit (F), dew point 38 F, and a barometric pressure of 29.61 inches of mercury.

A regional Next-Generation Radar (NEXRAD) mosaic obtained for 1805 CST and identified a north-south oriented line of high (>50 dBZ) values of reflectivity east of the accident site in western Oklahoma. Only light values of reflectivity were depicted near the accident location.

Atmospheric data was retrieved from a weather balloon at 1721 CST. The AMA sounding indicated almost the entire troposphere was stable or conditionally unstable. No temperature inversions were noted below 35,000 feet. The relative humidity was greater than 90 percent between about 11,000 and 13,000 feet. The freezing level was approximately 8,400 feet. Assessments of icing made noted the potential for moderate clear icing around 12,700 feet, with a potential for light mixed and rime icing at altitudes between 10,700 and 13,500 feet. Another area of potential light rime icing was identified between 15,600 and 17,300 feet.

A wind profile identified a west-southwesterly wind near the surface with a magnitude of 17 knots. The wind remained west-southwesterly/southwesterly but increased in magnitude to 51 knots through about 11,000 feet. Above this level the wind backed slightly and increased in magnitude to 63 knots through 20,000 feet. Calculations indicated the potential for several layers of significant clear-air turbulence below about 13,000 feet.

COMMUNICATIONS and RADAR INFORMATION

The pilot was last in contact with an Albuquerque ARTCC controller, who cleared the airplane to flight level 210, and gave the pilot permission for a course deviation. The pilot did not respond to the controller's query about a turn to the north. There was no further communications with the pilot and nor distress calls from the pilot.

A review of radar returns shows the airplane departing and climbing away from AMA. The airplane's track depicted a gentle S-type turn as the airplane headed in a southerly direction. The last several radar returns had the airplane's altitude as 14,700, 14,700, and 14,800 feet, before the airplane entered a right turn. The radar then had the airplane descending from 14,800 to 14,600 as the turn continued; then the altitude dropped to 11,200 feet, before the altitude data ends.

WRECKAGE AND IMPACT INFORMATION

The National Transportation Safety Board, inspectors from the Federal Aviation Administration (FAA), and a technical representative from the Beechcraft Corporation examined the airplane wreckage on site.

The airplane came to rest in open, rolling ranch land. All major components of the airplane were accounted for on scene. Pieces of the airplane including parts of the wings, the two engines, and tail section had separated from the fuselage, and were located within a 1 mile diameter of the fuselage.

The fuselage received heavy impact damage; the fuselage was deformed into an oval shape from its original semi cylindrical shape. The empennage section had been torn from the rear of the fuselage, the wing spar carry thru section was broken; the right inboard section of the wing remained with the fuselage. About a 9 foot section of the outboard section of the right wing was located approximately 115 feet, on a 55 degree heading from the fuselage. The right wing nacelle and engine had also separated from the wing. The right engine was about 240 feet on a 90 degree heading from the fuselage. The inboard section of the left wing separated from the fuselage near the wing root and was located adjacent to the primary fuselage ground scar. The outboard section of the left wing was located about 510 feet on a 300 degree heading from the fuselage; the left engine was located about 140 feet, on a 40 degree heading from the fuselage. Both engines turbine blades appeared bent, consistent with rotation at the time of impact.

The left and right ailerons had separated from their respective attachment points. Each aileron had been torn into pieces and was located in the debris field.

The vertical stabilizer separated from the fuselage and was located about 610 feet from the main wreckage. The rudder had separated from the vertical stabilizer and was in three pieces; with the base section located about 235 feet beyond the vertical stabilizer; the top section of the rudder, without the counterweight, was found another 315 feet beyond the rudder base section.

Both the right and left hand horizontal stabilizers were located near each other, and about 685 feet from the fuselage and 145 feet from the vertical stabilizer. The fuselage's aft bulkhead, which included the elevator torque fittings, was located just a few feet from the left and right horizontal stabilizers.

All of the examined fracture surfaces exhibited features consistent with overstress failures and no evidence of fatigue. Control cables separations were also consist with overload failure.

The airplane fragments and debris field is consistent with an in-flight break up, before impact with terrain.

MEDICAL AND PATHOLOGICAL INFORMATION

An autopsy on the pilot was not conducted.

The FAA Bioaeronautical Sciences Research Laboratory, Oklahoma City, Oklahoma, was not able to perform toxicological tests on the specimens for carbon monoxide or cyanide. The specimens were negative for ethanol in muscle and liver. Diphenhydramine was detected in the liver.

Diphenhydramine is antihistamine used to treat a number of conditions including allergic symptoms and the common cold. Diphenhydramine is available as a non-prescription drug that is commonly marketed under the trade name Benadryl.

TEST AND RESEARCH

The eGPWS unit, which was damaged in the accident, was sent to the NTSB's Vehicle Recorder Division, in Washington, DC. The unit was examined for the potential download of non-volatile memory (NVM) information on the accident flight. The eGPWS does not continuously record, but stores data to NVM only when certain criteria are met, additionally, if an alert or warning related to the EGPWS function activates, the unit retains data points for 20 seconds prior to the activation of the warning, and 10 seconds afterwards.

Data downloaded from the airplane's eGPWS revealed the unit recorded 22 seconds of information in the airplane's descent; during the right turn, the airplane descended from 13,966 feet to 5,904 feet. The airplane's decent rate was over 18,000 feet per minute (fpm), and after 19 seconds, the descent rate exceeded the eGPWS parameter of 32,000 fpm.

The airplane's remote directional gyro unit was located and had sustained impact damage during the accident. The external cover was removed exposing the gyro and gimbal. The gyro had broken from its mount and was lying inside the cover. Both the gyro and gimbal had marks consistent with the gyro's rotation at the time of impact. The airplane's attitude reference gyro was sent to the NTSB Material Laboratory in Washington DC, for examination. The examination also revealed marks on the gyro's that were consistent with rotation at the time of impact.

NTSB Probable Cause

The pilot’s loss of control of the airplane after encountering icing conditions and heavy to extreme turbulence and the subsequent exceedance of the airplane’s design limit, which led to an in-flight breakup.

© 2009-2020 Lee C. Baker / Crosswind Software, LLC. For informational purposes only.