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N7768Y accident description

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Crash location 31.817223°N, 97.569445°W
Nearest city Clifton, TX
31.782380°N, 97.576686°W
2.4 miles away
Tail number N7768Y
Accident date 13 Jul 2015
Aircraft type Piper Pa 30
Additional details: None

NTSB Factual Report

On July 13, 2015, about 1520 central daylight time, a Piper PA-30 airplane, N7768Y, was destroyed during an attempted forced landing to runway 14 at the Clifton Municipal Airport (7F7), near Clifton, Texas. The pilot, who held an airline transport pilot certificate, received minor injuries. The airplane was registered to and operated by the pilot as a 14 Code of Federal Regulations Part 91 personal flight. Visual meteorological conditions prevailed for the flight, which was not on a flight plan. The flight was originating at the time of the accident and was destined for the San Antonio International Airport (SAT), San Antonio, Texas.

The pilot reported that the accident flight was the first flight following an annual inspection of the airplane. He stated that he performed a pre-flight inspection of the airplane that included checking fuel, oil, and the replacement and securing of access panels. He stated that both of the engines started immediately and that pre-takeoff checks were normal. On takeoff the pilot noted that all of the engine instrument readings were normal with the exception of the fuel flow for the right engine. The reading was 17 gallons per hour versus the 14 gallon per hour reading expected. After becoming airborne, the fuel flow on the right engine remained the same and the engine RPM was at maximum. Under these conditions the right engine exhaust gas temperature (egt) was about 100 degrees lower than that of the left engine. He noted that his experience with the airplane was that the egt readings were normally very close to the same. He retarded the propeller control lever with no resulting change in rpm. Cycling the prop lever had no effect and he decided to return to 7F7. As he turned onto a downwind traffic pattern leg, the right engine suddenly stopped with no warning. He stated that the engine rpm reduced rapidly and the propeller would not windmill. He was unable to restart or feather the failed right engine. During the ensuing forced landing, about 20 ft above ground level, the airplane suddenly and violently rolled to the right. The airplane traveled across the taxiway parallel to the runway, onto the ramp, and came to rest behind a row of buildings on the southwest side of the runway. During the event, the airplane struck another airplane that was parked on the ramp area of the airport. The pilot reported that the airplane immediately caught fire and he exited unaided from the airplane.

A witness reported seeing the airplane in a wing down, nose down attitude heading toward the aircraft parking area. When the airplane came to rest he retrieved a fire extinguisher and began putting out fires in and around the airplane. Another witness reported that once the fires were under control, he entered the airplane's cockpit to turn off the airplane's emergency locator transmitter, and to shut off the fuel selectors. Upon shutting off the fuel selectors, the witness noted that the right fuel selector was only one detent from the off position, indicating that it was positioned for the auxiliary fuel tank.

The pilot reported that his normal procedure was to take off with the fuel selectors positioned for the main fuel tanks. He did not recall attempting to switch fuel tanks during the restart attempts on the accident flight. The pilot had reported having 58 gallons of fuel on-board the airplane prior to the accident flight. He did not remember the exact fuel loading but reported that he would typically have 2 to 5 gallons in each auxiliary tank with the remainder in the main tanks, balanced left to right.

Examination of the airplane after the accident revealed that neither propeller was in the feathered position. The dome pressure on each propeller was measured. The left propeller dome pressure was about 50 psi, but no dome pressure was able to be measured on the right propeller. Both propeller air fill valves had caps on them that were removed in order to check the charge pressure of the dome. According to Propeller manufacturer documentation, the dome charge for the installed propellers should have been 50 psi. Subsequent examination of the right propeller revealed that the air fill valve seal was contaminated by a small piece of debris. Once that debris was removed, the propeller dome was charged with air and was found to hold pressure. The examination also revealed that the propeller start locks were engaged which would prevent the propeller from feathering. Propeller manufacturers documentation stated that a low air charge could result in the propeller rpm control having little or no effect. According to the propeller manufacturer, the start lock should be set to engage when the engine rpm drops below a range of 700 to 900 rpm. Additionally, the manufacturer indicated that the propeller would still be able to feather normally if the propeller dome was not charged provided there was sufficient rpm to prevent premature engagement of the start locks.

Examination of the left engine was conducted after removal from the accident scene. The engine could be rotated by hand and compression and suction were verified on all cylinders during rotation. During rotation, spark was observed on all magneto leads. A differential compression test was then performed with readings above 65/80 observed on all cylinders except for the number 2 cylinder which measured 50/80. The number 2 cylinder was removed and examined with no defects noted. Notable is the fact that the differential compression test was performed on a cold engine that had not been operated for several months by the time the test was performed. Magneto timing was checked and found to be within specifications. The fuel control unit was removed and retained for further testing. Testing of the fuel control unit on a test flow bench at a certified repair station revealed that all measurements were within service limits.

The right engine was examined and could be rotated by hand. Suction and compression was verified on all cylinders during rotation. During rotation, spark was observed on all magneto leads. A differential compression test was performed with all cylinders exhibiting compression readings exceeding 65/80. Magneto timing was checked and found to be within specifications. The fuel control unit was removed and retained for further testing. Testing of the fuel control unit on a test flow bench at a certified repair station revealed that all measurements were within service limits.

The airplane's fuel system was examined. Compressed air was used to blow through the fuel lines with a catch bottle used to recover any expelled fuel or contaminants. The fuel recovered was a pale blue color consistent with 100LL aviation gasoline, and no contaminants were noted. The operation of the fuel selector valves was confirmed during testing and no anomalies in operation were noted. The fuel strainer bowls were removed and were found free of debris.

NTSB Probable Cause

The pilot's failure to maintain control during a precautionary landing following a total loss of power to one engine. The reason for the loss of engine power could not be determined based on available information.

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