Crash location | Unknown |
Nearest city | Chesapeake, VA
36.819037°N, 76.274940°W |
Tail number | N13DT |
---|---|
Accident date | 16 Mar 1999 |
Aircraft type | Cessna 340A |
Additional details: | None |
HISTORY OF FLIGHT
On March 16,1999, about 0950 eastern standard time, a Cessna 340A, N13DT, was destroyed when it impacted the ground during an emergency landing, shortly after takeoff from the Chesapeake Municipal Airport (CPK), Chesapeake, Virginia. The certificated commercial pilot and passenger were fatally injured. Visual meteorological conditions prevailed and no flight plan had been filed for the personal flight destined for the Flager County Airport, Bunnell, Florida. The flight was conducted under 14 CFR part 91.
In a telephone interview, a witness at the fixed base operator where the airplane was kept, stated she did not see or hear the airplane depart, but heard the pilot say over the unicom, "This is one three delta tango, making an emergency landing," and said the pilot sounded calm. Thirty to 45 seconds later, she heard the pilot say, "one three delta tango spiraling" or "spiral landing for runway five." Thirty to 45 seconds later, she heard someone say that the airplane had crashed.
A witness at the airport stated he observed the airplane lift off the ground about half-way down the 4,200-foot-long runway. About 3 to 5 minutes later, he heard a pulsating sound, like the throttle was being moved back and forth. He observed the airplane on the left side of the approach end to runway 5, about 500 feet above the ground. He then saw the airplane enter a 90-degree left bank, and said "I could see the entire bottom of the airplane." The flaps were extended and the gear was retracted. The airplane turned 180 degrees, maintaining altitude, and its nose dropped. The airplane then nosed up and entered a flat spin from about 200 feet above the ground.
Another witness stated he observed the airplane come over "the numbers," about 500 feet or less. The airplane then entered a left bank which increased to about a 90-degree bank angle. He noted that the airplane's left engine was feathered and that the landing gear was retracted. The airplane then entered a spin, descended, and impacted the ground.
The pilot's son also witnessed the accident. He observed the airplane slightly to the right of the runway, about 500 to 700 feet agl, as it approached the runway threshold at an angle. The airplane flew over the runway threshold, to the left of the runway. The airplane "kinda dipped up and down;" it then "nosed up a little and stalled to the left." The airplane entered a flat spin for about two revolutions and then impacted the ground.
The accident occurred during the hours of daylight approximately 36 degrees, 39 minutes north latitude, and 76 degrees, 19 minutes west longitude.
PERSONNEL INFORMATION
The pilot held a commercial pilot certificate with ratings for single and multi engine land airplanes. He was also instrument rated.
The pilot reported 4,500 hours of total flight experience on his most recent application for a Federal Aviation Administration (FAA) second class medical certificate, which was issued on December 1, 1998.
The pilot had purchased the airplane about 1 month prior to the accident. On an application for aircraft insurance dated February 20, 1999, the pilot reported 4,800 hours of total flight experience, 700 hours in multiengine aircraft, and 10 hours in the make and model of the accident airplane.
The pilot's son stated that the pilot owned a Piper Seneca prior to purchasing the accident airplane. He was not certain of how much flight experience the pilot had accumulated in a Cessna 340A.
A certified flight instructor (CFI) who had flown with the accident pilot in the accident airplane stated he was first contacted by the accident pilot in January 1998, and flew in the accident pilot's Piper Seneca on one occasion. In 1999, about one month prior to the accident he was again contacted by the pilot, who told him that he had purchased a Cessna 340A, and that he needed a CFI to fly with him in the airplane for insurance purposes. According the CFI's logbook, he flew with the accident pilot in N13DT on a cross-country flight to Ohio for 4.8 hours, and a local training flight for 1 hour. In addition, the CFI flew the accident airplane for about one hour, solo.
On March 11, 1999, the pilot satisfactorily completed a 4-day Cessna 340A initial training course taught by SimCom Training Centers, Orlando, Florida.
AIRCRAFT INFORMATION
Review of the airplane's maintenance records revealed it had received an annual inspection on February 18, 1999. At that time, the airplane's total airframe time was 3,563.8 hours. Additionally, at the time of the annual inspection, the left engine had accumulated 1,187.4 total hours, and the right engine had accumulated 1,176.0 total hours, since overhaul.
METEOROLOGICAL INFORMATION
A weather observation taken at CPK at 1500 reported: winds from 360 degrees at 3 knots; visibility 10 statue Miles; scattered Clouds at 8,000 and 10,000 feet; temperature 45 degrees F; dewpoint 27 degrees F; altimeter 30.14.
WRECKAGE INFORMATION
On-scene examination of the wreckage revealed that the airplane impacted a grass area about 1,000 feet northwest from the approach end of runway 5, and came to rest upright, on a magnetic course of 250 degrees. All major components of the airplane were accounted for at the scene. The main wreckage which included the cabin, both wings, and both engines, was consumed by a post crash fire. The forward portion of the airplane's nose, and the tail section aft of the airplane's rear bulkhead were not fire-damaged. The underside portions of the wreckage that were not fire-damaged revealed crushing and compression wrinkles in a vertical plane.
Flight control continuity was confirmed from the forward cockpit area to all primary control surfaces. Examination of the airplane's landing gear box indicated that the landing gear was in the retracted position.
Initial examination of the airplane's engines was conducted at the accident site. Both engines were damaged by fire. Both engines were rotated about 30 degrees using a socket inserted into an accessory drive gear, and crankshaft continuity was noted. The top spark plugs were removed from both engines. The spark plug electrodes were intact and exhibited uneven wear. The left engine propeller blades were found at or near the feathered position. The right engine propeller contained a blade with "s" bending, and a blade which was bent about 90 degrees outboard. Both engines were retained for further examination.
MEDICAL AND PATHOLOGICAL INFORMATION
Autopsies were performed on the pilot and passenger by the Office of the Chief Medical Examiner, Norfolk, Virginia.
Toxicological testing was conducted by the FAA Toxicology Accident Research Laboratory, Oklahoma City, Oklahoma.
TESTS AND RESEARCH
Engine Examinations
On May 12, 1999, the airplane's left and right engines were examined at Teledyne Continental Motors, Mobile, Alabama, under the supervision of a Safety Board Investigator. Both engines exhibited extensive fire and impact damage.
Disassembly of the airplane's right engine did not reveal any pre-impact mechanical malfunctions.
Disassembly of the left engine revealed that the camshaft was fractured in the vicinity of the rear oil distribution groove. The camshaft and drive gear were removed and forwarded to the Safety Board Materials Laboratory, Washington, DC, for further examination.
Camshaft Examination
Examination of the camshaft by a Safety Board metallurgist revealed that the camshaft separated through three of the four oil holes located in the end of the shaft adjacent to the drive gear. Examination of the fracture faces revealed features that were consistent with fatigue cracking over much of the fracture surface.
ADDITIONAL INFORMATION
Further review of the airplane's maintenance records revealed that the airplane's engines were last remanufactured to new parts limits by RAM Aircraft Corporation, Waco, Texas. At that time, work was performed on the engines which included the installation of a "RAM economy camshaft p/n 1058-3RS."
The left and right engines were remanufactured on March 14, 1991, and May 6, 1991, respectively.
Refueling
Refueling records indicated that the airplane was last fueled on March 12, 1999, when it was "topped off" with 147.5 gallons of 100LL aviation gasoline.
Wreckage Release
The airplane wreckage was released on March 19, 1999, to a representative of the owners insurance company.
The pilot's failure to maintain control of the airplane during a single engine emergency landing, after experiencing a failure of the left engine. A factor in this accident was the failure of the left engine's camshaft due to a fatigue crack.