Crash location | 48.787777°N, 122.541944°W |
Nearest city | Bellingham, WA
48.759553°N, 122.488225°W 3.1 miles away |
Tail number | N917AB |
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Accident date | 06 Aug 2015 |
Aircraft type | Cleveland Allan B Nieuport 11# |
Additional details: | None |
On August 6, 2015, about 2000 Pacific daylight time, an experimental amateur-built Cleveland Nieuport #11 airplane, N917AB, experienced a partial loss of engine power during a maintenance check flight and landed short of a closed runway at Bellingham International Airport, Bellingham, Washington. The commercial pilot sustained minor injuries. The airplane was substantially damaged. The airplane was registered to and operated by the pilot under the provisions of Title 14 Code of Federal Regulations Part 91 as a personal flight. Visual meteorological conditions prevailed, and no flight plan had been filed for the local flight, which was originating at the time of the accident.
The pilot reported that the engine had just been replaced during a recent condition inspection. Prior to the flight, the engine had been run 5 times, which included the initial run, test run, engine tuning, taxi test and subsequent high-speed taxi test. The pilot stated that he intended to fly over the airport to remain within gliding distance of the runway. Just after takeoff from runway 16, at an altitude of 700 ft above ground level, a reduction in engine rpm was observed despite the throttle being at full power. The pilot noted that the engine rpm was still decaying, that he heard no unusual sounds from the engine, and that it was not running rough. The pilot further reported that he notified the tower controller that he was having engine problems and was subsequently cleared to land runway 34.
While the engine rpm continued to decrease, the pilot realized that he was unable to reach runway 34 and attempted to land on a closed runway, while observing that the engine rpm had decreased from 3,000 to 2,500, then down to 2,000, which was an rpm setting for a power off approach to landing. The pilot then observed a stand of trees directly in front of his position, at which time he maneuvered to avoid striking them, along with an adjacent airport perimeter fence. Subsequently, the airplane landed hard and nosed over in a grassy area short of the runway.
The airplane was powered by a Hummel, 76 HP, Volkswagen 2180 cc engine with dual weber carburetors, and a single point electronic ignition system. Examination of the airplane was performed by the pilot, an airframe and powerplant mechanic, and a Federal Aviation Administration (FAA) inspector. The FAA inspector reported that the examination revealed that the fuel system appeared to be in operable condition. Further examination revealed that the fuel tank was void of any fuel, and that a vent line at the top of the fuel tank was separated from the tank as a result of the accident. The fuel lines were intact to the fuel pump, which was a stock Volkswagen style fuel pump. The pump was removed and operated normally when actuated by hand. The carburetor throats were clear and clean. The throttle linkages were not damaged and moved freely. The idle and full throttle stops were intact, and the throttle linkage moved to both stops.
The Volkswagen style ignition system featured a Bosch distributor with stock ignition wires and spark plugs. In addition, the ignition coil was also stock. The FAA inspector stated that the original points and condenser were replaced when the engine was equipped with an electronic type automotive ignition system. The ignition system revealed evidence of damage.
The engine was rotated in the direction of rotation and the distributor shaft rotated correctly with a slight amount of delay. The drive gear revealed some backlash, which according to a mechanic, was normal for the engine.
Engine valve train continuity was established throughout the engine. The FAA inspector reported that they did not observe any evidence of mechanical anomalies with the airframe or engine.
A partial loss of engine power for reasons that could not be determined because postaccident examination revealed no mechanical malfunctions or anomalies that would have precluded normal operation.