Crash location | 37.652222°N, 81.450000°W |
Nearest city | Saulsville, WV
37.642891°N, 81.456771°W 0.7 miles away |
Tail number | N5691B |
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Accident date | 12 Aug 2005 |
Aircraft type | Enstrom 280C |
Additional details: | None |
On August 12, 2005, about 1330 eastern daylight time, an Enstrom 280C, N5691B, received substantial damage when it impacted terrain near Saulsville, West Virginia. The certificated commercial pilot was not injured, and the passenger received serious injuries. Visual meteorological conditions prevailed, and no flight plan was filed for the business flight, which originated at Logan County Airport (6L4), Logan, West Virginia, about 1300, and was conducted under 14 CFR Part 91.
According to the pilot, the purpose of the flight was to drop off a package at a local community college. While on approach to the landing area, the pilot did not see a windsock, and based his estimation of the wind direction by watching leaves on the trees.
During the final approach, he adjusted the flight controls to decelerate and maintain the approach angle to the touchdown point, while maintaining the rotor rpm at 2,900. The helicopter approached the intended landing area at a "normal to steep angle."
Without any further control inputs, and while stabilized at approximately 40 knots indicated airspeed, about 100 feet above the ground, the helicopter began a slow, un-commanded yaw to the right. The pilot responded by applying left anti-torque pedal; however, the helicopter continued to yaw to the right.
As the helicopter turned beyond about 90 degrees from the original flight path, the pilot realized that he would not be able to land the helicopter in the intended landing area. He then checked the rotor and engine rpm and noted that they were "out of the green and decreasing." The pilot felt that he could not enter an autorotation due to a power line that was below, and instead increased the throttle to stabilize rotor rpm and maintain altitude in order to fly to a more suitable area for landing. The helicopter "did not respond," and continued yawing to the right. About 10 feet above the ground, and after about 270 degrees of yaw from the original direction of flight, the helicopter descended rapidly and impacted the ground.
The pilot held a commercial pilot certificate with a rating for rotorcraft-helicopter and a flight instructor certificate with a rating for rotorcraft-helicopter. He reported 297 total hours of flight experience, 15 hours of which were in the accident helicopter make and model.
The helicopter was examined following the accident. The left skid was broken, and the tail rotor sustained damage to both blades consistent with impact. Additionally, the tail rotor drive shaft was fractured at the coupling hub. The coupling hub, flex pack, coupling flange, drive shaft, and associated components were forwarded to the Safety Board Materials Laboratory for further examination.
Examination of the fractured portions of the coupling hub revealed that the fracture regions on both sides of the taper pin hole displayed light circumferential smearing and distinct circumferential surface lines that were consistent with torsional overload. There was no discoloration or severe mechanical damage observed on the fracture faces to indicate that the mating fracture faces had rubbed together while the system was transmitting power. Displaced material, oriented counter to the direction of rotation, was found on the sides of the exposed taper pin hole, consistent with a torsional event.
The weather reported at Raleigh County Memorial Airport (BKW), Beckley, West Virginia, about 17 nautical miles east, at 1351, included calm winds, scattered clouds at 4,400 feet, 4 statute miles visibility in haze, temperature 82 degrees Fahrenheit, dewpoint 64 degrees Fahrenheit, and an altimeter setting of 30.10 inches of mercury.
The elevation in the area of the accident site was about 2,000 feet, and the density altitude was calculated to be about 3,900 feet around the time of the accident.
According to the Enstrom 280C Flight Manual, steep approach procedures are used to clear obstacles in the flight path when landing in a confined area, and require precision power control. The airspeed of a steep approach should be between 30 and 35 mph, and the rate of descent should be as low as possible for the desired angle of descent. A relatively high amount of power is required to control the rate of descent.
According to Federal Aviation Administration Advisory Circular (AC) 90-95, Unanticipated Right Yaw in Helicopters, loss of tail rotor effectiveness (LTE) events typically occur in a low airspeed flight regime while maneuvering, on final approach to landing, or during low-level flying. Any maneuver that requires the pilot to operate at high-power, at low airspeed, and with a left crosswind or tailwind, creates an environment where unanticipated right yaw may occur. Additional factors that can influence the severity of the onset of LTE include increases in gross weight and density altitude, low indicated airspeeds, and "power droop," or a decrease in rotor rpm that causes a corresponding decrease in tail rotor thrust.
The AC also provided guidance regarding recovery techniques following an LTE event. If a sudden unanticipated right yaw occurs, the pilot should apply full left pedal, while simultaneously moving the cyclic forward to increase speed, and altitude permitting, reduce power. Following the recovery, the controls should be adjusted for normal forward flight. A collective pitch reduction will aid in arresting the yaw rate, but may cause an increase in the rate of descent. Any large, rapid increase in collective pitch to prevent ground or obstacle contact may further increase the yaw rate, and decrease rotor rpm.
The pilot's inadequate remedial action following a loss of control during the landing approach.